If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-099-22012 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.94,"lon":-80.79,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Green Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: R& B CAREY COMM | |
License Status: Producing | |
License Date: 1985-12-24 | |
Spud Date: 1986-06-27 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1986-07-02 | |
Well Total Depth: 5856.00 ft | |
Configuration: Vertical | |
Latitude: 40.940000 | |
Longitude: -80.790000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-12-24 | 182 BELDEN & BLAKE CO GeoDate 12/24/85 |
Oil and Gas | 1985-12-24 | Issued Date 12/24/85 Expired Date 12/24/86 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05856 Proposed Drill Depth 05856 |
Original Spud | 1986-06-27 | DUPLICATE TYPED 4-25-96 |
Completed | 1986-07-02 | DUPLICATE TYPED 4-25-96 |
Reached Total Depth | 1986-07-02 | DUPLICATE TYPED 4-25-96 |
Completion Report Received | 1986-07-16 | DUPLICATE TYPED 4-25-96 |
Construction Permit Expires | 1986-12-24 | DUPLICATE TYPED 4-25-96 |
Change of Owner | 2007-04-27 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC |
Record Last Modified | 2017-02-15 | DUPLICATE TYPED 4-25-96 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5614 | 5757 | 0 |
5614 | 5757 | 0 | |
2006-09-11 | 5654 | 5756 | 45 |
5654 | 5756 | 45 | |
5614 | 5757 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 126000 Gal | 70000 | FRAC W/126M GAL WATER & 70M# SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | BELDEN & BLAKE CORPORATION | 2179.00 | 293.00 | 365 |
1987 | BELDEN & BLAKE CORPORATION | 12312.00 | 362.00 | 365 |
1988 | BELDEN & BLAKE CORPORATION | 5498.00 | 291.00 | 332 |
1990 | BELDEN & BLAKE CORPORATION | 4962.00 | 96.00 | 343 |
1991 | BELDEN & BLAKE CORPORATION | 4199.00 | 38.00 | 365 |
1992 | BELDEN & BLAKE CORPORATION | 2808.00 | 130.00 | 366 |
1993 | BELDEN & BLAKE CORPORATION | 2372.00 | 165.00 | 365 |
1994 | BELDEN & BLAKE CORPORATION | 1695.00 | 0.00 | 360 |
1995 | BELDEN & BLAKE CORPORATION | 1257.00 | 128.00 | 351 |
1996 | BELDEN & BLAKE CORPORATION | 1951.00 | 0.00 | 366 |
1997 | BELDEN & BLAKE CORPORATION | 1061.00 | 145.00 | 365 |
1998 | BELDEN & BLAKE CORPORATION | 886.00 | 0.00 | 365 |
1999 | BELDEN & BLAKE CORPORATION | 1012.00 | 94.00 | 365 |
2000 | BELDEN & BLAKE CORPORATION | 532.00 | 0.00 | 349 |
2001 | BELDEN & BLAKE CORPORATION | 1089.00 | 60.00 | 351 |
2002 | BELDEN & BLAKE CORPORATION | 1242.00 | 50.00 | 365 |
2003 | BELDEN & BLAKE CORPORATION | 1146.00 | 58.00 | 364 |
2004 | BELDEN & BLAKE CORPORATION | 1251.00 | 24.00 | 366 |
2005 | BELDEN & BLAKE CORPORATION | 1227.00 | 44.00 | 365 |
2006 | BELDEN & BLAKE CORPORATION | 1114.00 | 0.00 | 365 |
2007 | ENERVEST OPERATING LLC | 765.00 | 26.00 | 365 |
2008 | ENERVEST OPERATING LLC | 564.00 | 0.00 | 365 |
2009 | ENERVEST OPERATING LLC | 614.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 1121.00 | 110.00 | 365 |
2011 | ENERVEST OPERATING LLC | 636.00 | 58.00 | 0 |
2012 | ENERVEST OPERATING LLC | 883.00 | 0.00 | 366 |
2013 | ENERVEST OPERATING LLC | 945.00 | 31.00 | 365 |
2014 | ENERVEST OPERATING LLC | 919.00 | 0.00 | 365 |
2015 | ENERVEST OPERATING LLC | 701.00 | 0.00 | 365 |
2016 | ENERVEST OPERATING LLC | 845.00 | 0.00 | 366 |
2017 | ENERVEST OPERATING LLC | 740.00 | 0.00 | 365 |
2018 | ENERVEST OPERATING LLC | 816.00 | 23.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-362448743 | 2012-7-24 0:00: | PW | No Violations | 2.00 |
-63048909 | 2013-7-23 0:00: | PW | No Violations | 2.00 |
000PL12759 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0063048909 | 2013-07-23 | Production Wells | No Violations | I was notified by Joe Tippert Field Supervisor from Entervest that the 210 barrel tank on the above location has a hole on the bottom of the tank and that there was a release of some oil in the dike. The tank had 64 ( 74.24 barrels of fluid ) Due to the thick oil in the bottom of the tank the release was estimated to be 6 barrels by the gauging of the tank. When I arrived on location they had dug some holes in the tank battery for the oil to collect in and the water truck was vacuuming it up. Sutton Pump was coming to the location to use hot water to clean the area before removing the contaminated stone and soil. I instructed them to clean up all contimated stone and soil and dispose of in an approved manner. I will reinspected at a later date. This is a 4.5 swab well. |
0289017620 | 2013-07-30 | Production Wells | No Violations | I performed a status check on the above location. Up on my inspection this location has not been completed at this time. I called Joe Tippered and informed him of this, he said that it would be completed tomorrow 7/31/2013. |
0362448743 | 2012-07-24 | Production Wells | No Violations | I performed a follow inspection on the clean up operation of this location. Sutton Pump will be returning tomorrow to hot water the location one more time before removing the stone and soil. |
1099661013 | 2004-11-01 | Production Wells | No Violations | The tank battery consists of 1-210 bbl storage tank, 1-buried concrete salt water tank, 1-separator and a dike. |
1222257461 | 2008-09-23 | Production Wells | No Violations | I performed a random field inspection. Both the wellhead and the tank battery were GPSd. I walked around the tank battery area and found it to be in good shape. The ID sign was posted. There were no violations at this time. |
1378304218 | 2013-08-02 | Production Wells | No Violations | I received a phone call from Joe Tipperd and he stated that the above clean up of this location has been completed. Up on my inspection the 210 barrel tank had been replaced with a 100 barrel tank. Site is clean ID signs are posted, No violations noted at this time. |
289017620 | 2013-7-30 0:00: | PW | No Violations | 1.00 |
PL12759 | PL | No Violations |
For data sources see[9]