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Well ID: 34-115-24371 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Bern Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: MAYLE P | |
License Status: Final Restoration | |
License Date: 2014-04-07 | |
Spud Date: 1994-02-25 | |
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]] | |
Final Drill Date: 1994-03-02 | |
Well Total Depth: 5068.00 ft | |
Configuration: Vertical | |
Latitude: 39.450000 | |
Longitude: -81.870000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1993-11-12 | 198 VIKING RESOURCES CORP GeoDate 11/12/93 |
Oil and Gas | 1993-11-12 | Issued Date 11/12/93 Expired Date 11/12/94 Acres 0066060 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05068 Proposed Drill Depth 05068 |
Original Spud | 1994-02-25 | |
Completed | 1994-03-02 | |
Reached Total Depth | 1994-03-02 | |
Completion Report Received | 1994-07-06 | |
Change of Owner | 1998-07-01 | Operator changed from 198, VIKING RESOURCES CORP to 3793, ENERGY SEARCH INC |
Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-04-07 | Proposed Formations:CLINTON, Issued Date:4/7/2014, Expired Date:4/6/2016 12:00:00 PM, Drilling unit acres:66, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-09-04 | |
Construction Permit Expires | 2016-04-06 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4908 | 4936 | 0 |
4908 | 4936 | 0 | |
2006-09-11 | 4922 | 4928 | 13 |
4922 | 4928 | 13 | |
4908 | 4936 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 500 Gal | 0 | WATER FRAC |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | VIKING RESOURCES LLC | 73931.00 | 264.00 | 365 |
1995 | VIKING RESOURCES LLC | 70835.00 | 101.00 | 365 |
1996 | VIKING RESOURCES LLC | 30751.00 | 102.00 | 0 |
1997 | VIKING RESOURCES LLC | 10354.00 | 0.00 | 0 |
1998 | VIKING RESOURCES LLC | 2548.00 | 0.00 | 365 |
1999 | ENERGY SEARCH INC | 7678.00 | 0.00 | 365 |
2000 | ENERGY SEARCH INC | 9244.00 | 0.00 | 365 |
2001 | ENERGY SEARCH INC | 4322.00 | 0.00 | 365 |
2002 | ENERGY SEARCH INC | 845.00 | 0.00 | 365 |
2003 | ENERGY SEARCH INC | 722.00 | 0.00 | 365 |
2004 | ENERGY SEARCH INC | 1122.00 | 0.00 | 365 |
2005 | ENERGY SEARCH INC | 1420.00 | 0.00 | 365 |
2006 | ENERGY SEARCH INC | 1391.00 | 0.00 | 365 |
2007 | ENERGY SEARCH INC | 43.00 | 0.00 | 59 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1994 | VIKING RESOURCES LLC | Brine | 159 | 365 |
1995 | VIKING RESOURCES LLC | Brine | 0 | 365 |
1996 | VIKING RESOURCES LLC | Brine | 0 | 0 |
1997 | VIKING RESOURCES LLC | Brine | 0 | |
1998 | VIKING RESOURCES LLC | Brine | 0 | 365 |
1999 | ENERGY SEARCH INC | Brine | 0 | 365 |
2000 | ENERGY SEARCH INC | Brine | 365 | |
2001 | ENERGY SEARCH INC | Brine | 58 | 365 |
2002 | ENERGY SEARCH INC | Brine | 365 | |
2003 | ENERGY SEARCH INC | Brine | 365 | |
2004 | ENERGY SEARCH INC | Brine | 0 | 365 |
2005 | ENERGY SEARCH INC | Brine | 0 | 365 |
2006 | ENERGY SEARCH INC | Brine | 0 | 365 |
2007 | ENERGY SEARCH INC | Brine | 0 | 59 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-440556692 | 2013-12-20 0:00 | PW | No Violations | 0.10 |
-6280494 | 2013-6-7 0:00:0 | PW | No Violations | 0.30 |
0000015602 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 4/11/95 INSPECTOR GERALD YOUNG DATE 04/1119/95 DATA FROM OLD VAX INFO | |
0006280494 | 2013-06-07 | Production Wells | Violations Noted | Well was found to be shut in at time of inspection and production has been reported as zero since 2007. There was an old chart in the meter in which the ink had bled through the paper. There is one 100 bbl tank and one full 50 bbl steel tank in the dike. Operator must make well capable of production within 60 days; or plugging is required in 60 days. |
0440556692 | 2013-12-20 | Production Wells | No Violations | Compliance Action Follow-up -6280494: There has been no resolution to any of the issues. The well is currently not in production. |
1394629678 | 2014-03-12 | Administrative Inspection | No Violations | I talked to Tim McConeghey and he stated they will plug the well by June 1st of this year. |
1409320033 | 2014-08-29 | Plug / Plug Back | No Violations | Witnessed 30 sacks of Class A cement set through tubing from 4900-4505 feet. Pulling tubing today. |
1409678054 | 2014-09-02 | Plug / Plug Back | No Violations | Casing ripped at 3925 and pulled to 3753 to set Rip/Lime plug in conjuction from 3750-3503. Berea Plug set from 1817-1580 with a bag of LCM, after pumping the hole was on vacuum. Asing was pulled to ensure there was no cement in the pipe. Another 200 feet of cement was placed in the hole with the intention to shut off the Lost Circulation Zone. |
1409753361 | 2014-09-03 | Plug / Plug Back | No Violations | Operator ran 4.5 down and tagged last plug at 1752. They then pumped on the hole and broke circulation. Once the hole was clean of oil, they set another plug across the Berea from 1586-1735. Operator then set the bottom of the surface casing plug from 1177-1377. They pulled all casing from the hole and set the surface plug (0-200). The cement stayed at the surface. |
1420467393 | 2015-01-05 | Final Restoration | No Violations | Location meets 1509.072 final restoration requirements. |
15602 | PL | No Violations | ||
1920016624 | 2014-08-28 | Plug / Plug Back | No Violations | Chipco, LLC was on location running the tubing back down into the hole to 4900. They will set bottom hole plug and rip the 4.5 tomorrow morning. |
1948768261 | 2013-08-30 | Production Wells | No Violations | Compliance Action Follow-up -6280494: The valves were open at the wellhead, however the same old chart was on the meter. I called Tim with Enervest and asked if the well capable of production or in production and he said he would check and get back to me on the issue. Enervest has been reporting zero production. Tim had called back and stated well was in fact idle. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0006280494 | US-OH-127111 | 2014-09-05 | Well shall be plugged | |
0006280494 | US-OH-127112 | 2014-09-05 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]