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34-119-20933

Well Details

Well ID: 34-119-20933
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Country: United States
State: Ohio
County: Muskingum
Municipality: Hopewell Township
Operator Name: JOHNSON MIKE
Well Pad ID:
Farm/Lease Name: DENNY E M HEIRS
License Status: Final Restoration
License Date: 2012-08-10
Spud Date: 1980-11-03
Spud Drilling Contractor:
Final Drill Date: 1980-12-11
Well Total Depth: 3110.00 ft
Configuration: Vertical
Latitude: 39.920000
Longitude: -82.230000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-09-12 347 MIDLAND OIL CO GeoDate 9/12/80
Original Spud 1980-11-03 REOPEN COR IN LOC. 9/18/1980
Completed 1980-12-11 REOPEN COR IN LOC. 9/18/1980
Reached Total Depth 1980-12-11 REOPEN COR IN LOC. 9/18/1980
Change of Owner 2000-07-14 Operator changed from 347, MIDLAND OIL CO to 1, HOPEWELL OIL & GAS
Change of Owner 2002-12-24 Operator changed from 1, HOPEWELL OIL & GAS to 5460, JOHNSON MIKE
APP 2012-08-10 Proposed Formations:, Issued Date:8/10/2012, Expired Date:8/10/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2012-10-12 REOPEN COR IN LOC. 9/18/1980
Construction Permit Expires 2014-08-10 REOPEN COR IN LOC. 9/18/1980
Record Last Modified 2019-06-14 REOPEN COR IN LOC. 9/18/1980

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 MIDLAND OIL CO 0.00 301.00 365
1985 MIDLAND OIL CO 0.00 218.00 365
1986 MIDLAND OIL CO 0.00 224.00 365
1987 MIDLAND OIL CO 0.00 149.00 315
1988 MIDLAND OIL CO 0.00 0.00 100
1989 MIDLAND OIL CO 0.00 155.00 365
1990 MIDLAND OIL CO 0.00 68.00 320
1991 MIDLAND OIL CO 0.00 0.00 365
1992 MIDLAND OIL CO 0.00 0.00 38
1993 MIDLAND OIL CO 0.00 69.00 300

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 MIDLAND OIL CO Brine 0 365
1985 MIDLAND OIL CO Brine 27 365
1986 MIDLAND OIL CO Brine 15 365
1987 MIDLAND OIL CO Brine 7 315
1988 MIDLAND OIL CO Brine 0 100
1989 MIDLAND OIL CO Brine 7 365
1990 MIDLAND OIL CO Brine 9 320
1991 MIDLAND OIL CO Brine 0 365
1992 MIDLAND OIL CO Brine 0 38
1993 MIDLAND OIL CO Brine 0 300

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1288261903 2012-10-11 0:00 PB No Violations 11.00
-2077030605 2012-6-19 0:00: PW No Violations 2.00
0216035995 2012-10-03 Plug / Plug Back No Violations Mark Hines was setting bottom hole plug of 2.5 tons of clay and trying to get ripped off. Jake Glasscock and I were present as this was being performed.
0236450404 2012-10-04 Plug / Plug Back No Violations MH well service on site, 500 bottom plug is done, 4.5 casing ripped at 2170. They are placing the Lime plug.
0409249345 2012-10-09 Plug / Plug Back No Violations Jake Glasscock and I stopped by and Mark Hines has pulled 20of 7out and tried to go in with bullnose center spear. The 7casing was split and would not let a steel dye nipple go down or would let the pipe come up thru the 8casing. We decided to rip holes on every collar from 800up to 250. 275 is bottom of the Big Injun. They were going to set clay from lime plug up to the bottom of the 7seat.
0997674143 2013-03-21 Final Restoration No Violations Final Restoration passed on 3-21-13 by Patrick Shreve.
1247714496 2012-10-09 Plug / Plug Back No Violations I accompanied Pat Shreve to plug job where we witnessed the 4 1/2 casing pulled and stacked on location. Operator plans to fill hole with clay from top of last plug to 7 casing seat.
1288261903 2012-10-11 Plug / Plug Back No Violations Clay has placed up to 170, I spoke with Pat Shreve concerning the remainder of the plug from 170 to surface. Mark Hines has ripped holes in the 7 casing to allow cement to exit the ripped holes and fill the annulus between the 7 and the 8 casings, this will prevent any communication between zones. Cement is set up for 10/12/2012.
1343652928 2012-06-19 Production Wells No Violations On day of inspection met with land owner on well and walked in to the well. Well is supplied with pump jack and a 100 barrel tank. All valves are shut on well head and there is no domestic or commercial hookup.
1347625668 2012-09-14 Administrative Inspection No Violations I called Mike Johnson on well that was a complaint. He stated he will call back after talking to Mark Hines. They will move rig to plug in 1 week.
1349265852 2012-10-01 Plug / Plug Back No Violations I was on location to witness plug job. At the time of arrival, operator began pulling tubing. Valley Clay dropped off 20+ tons of clay which was then covered with tarp due to onset of rain.
1349291930 2012-10-03 Plug / Plug Back No Violations I accompanied Pat Shreve to plug job where we witnessed operator run in and tag bottom at 2923. Total depth of the well was 3110. The bottom of the tubing, rods, and mud anchor was located at 2993. We witnessed the placement of the 2.5 ton bottom hole plug. Operator is currently ripping the 4 1/2 casing.
1358286182 2012-10-12 Plug / Plug Back No Violations Well was plugged on this date and Compliance Notice is resolved. Patrick Shreve
1762215518 2012-10-12 Plug / Plug Back No Violations MH well service on site, they have ripped holes in the 7 casing from 180 to surface, class A cement was used from 180 to surface to finish the plug.
2077030605 2012-06-19 Production Wells Violations Noted Well is idle. No Production filed. No id . Plug well
216035995 2012-10-3 0:00: PB No Violations 7.50
236450404 2012-10-4 0:00: PB No Violations 4.00
409249345 2012-10-9 0:00: PB No Violations 4.00
997674143 2013-3-21 0:00: FR No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
2077030605 US-OH-121194 2013-01-15 Failure to legibly identify well
2077030605 US-OH-121195 2013-01-15 Well shall be plugged
2077030605 US-OH-121196 2013-01-15 Nonproduction; well shall be plugged or placed in temporary inactive status
2077030605 US-OH-121197 2013-01-15 Statement of annual production not filed

For data sources see[7]

References