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Well ID: 34-119-28095 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Madison Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: CONSOLIDATION COAL CO | |
License Status: Final Restoration | |
License Date: 2013-02-27 | |
Spud Date: 1997-06-10 | |
Spud Drilling Contractor: KELT DRILLING | |
Final Drill Date: 1997-07-20 | |
Well Total Depth: 5880.00 ft | |
Configuration: Vertical | |
Latitude: 40.110000 | |
Longitude: -81.980000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1997-03-17 | Issued Date 3/17/97 Expired Date 3/17/98 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON-TPLU Proposed Depth Proposed Drill Depth |
Original Spud | 1997-06-10 | RBDMS Rec |
Completed | 1997-07-20 | RBDMS Rec |
Reached Total Depth | 1997-07-20 | RBDMS Rec |
Completion Report Received | 1997-12-03 | RBDMS Rec |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2013-02-27 | Proposed Formations:ROSE RUN, Issued Date:2/27/2013, Expired Date:2/27/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-07-25 | RBDMS Rec |
Construction Permit Expires | 2015-02-27 | RBDMS Rec |
Record Last Modified | 2017-02-15 | RBDMS Rec |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 2000 Gal | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | CARLESS RESOURCES INC | 1282.00 | 0.00 | 72 |
1998 | EXCO - NORTH COAST ENERGY INC | 10627.00 | 3290.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 14155.00 | 1977.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 23508.00 | 1512.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 27698.00 | 911.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 12369.00 | 394.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 14919.00 | 348.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 9865.00 | 295.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 0.00 | 22.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 1363.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2008 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0.00 | 0.00 | 0 |
2010 | ENERVEST OPERATING LLC | 0.00 | 3.00 | 365 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 294 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1997 | CARLESS RESOURCES INC | Brine | 100 | 72 |
1998 | EXCO - NORTH COAST ENERGY INC | Brine | 40 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | Brine | 365 | |
2000 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | Brine | 309 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | Brine | 62 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | Brine | 687 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | Brine | 950 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 294 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1116706422 | 2012-11-1 0:00: | PW | No Violations | 1.00 |
-1809256060 | 2014-7-25 0:00: | PB | No Violations | 6.50 |
-844873200 | 2010-9-9 0:00:0 | WR | No Violations | |
-917044231 | 2014-7-23 0:00: | PB | No Violations | 2.00 |
0262691999 | 2013-04-10 | Administrative Inspection | No Violations | Per Request of Enervest on the status of the well. Well is not in compliance with 1509. Waiting on Enervest to Plug well. Plug permit in hand. |
0485255462 | 2004-02-18 | Preliminary Restoration | No Violations | |
0536526114 | 2014-07-24 | Plug / Plug Back | No Violations | I stopped back at site to find out what had plugged the tubing off. It was a red sand and a gray shale. Could be the Red Medina and the Queenston. Chipco is running 1.5tubing in and circulating on every 30 joints. |
0844873200 | 2010-09-09 | Work Over Reconditioning | No Violations | FOLLOW UP TO NOV # 985074867 Pulled tubing to use to plug another well. This well is not producing. |
0917044231 | 2014-07-23 | Plug / Plug Back | No Violations | On the date of inspection I accompanied ODNR Inspector Patrick Shreve to check the status of the well plugging. The production casing had been ripped and the service rig was pulling casing at the time of my inspection. Refer to Patrick Shreves report for further details. |
0985074867 | 2010-09-09 | Work Over Reconditioning | No Violations | Pulled tubing to use to plug another well. This well is not producing. |
1110816583 | 2005-03-14 | Production Wells | No Violations | Not selling gas at present time |
1116706422 | 2012-11-01 | Production Wells | No Violations | Well is still idle with no tubing present in well. There are two flanges that are bolted together with 2 bolts. The flow line has been un hooked and is laying on site. I called Tim McConahae and he will check on this well. |
1177157089 | 2003-04-08 | Production Wells | No Violations | |
1357245521 | 2013-01-03 | Production Wells | Violations Noted | Idle well with two flanges bolted together. The flow line is disconnected from the well head. There are 2-100barrel tanks and no production has been reported since 2010 of only 3 barrels of oil. There is a large gap of time from 2006-2010 that there was n |
1406027748 | 2014-07-22 | Plug / Plug Back | No Violations | Chipco is plugging for Enervest and is spotting bottom plug thru 1.5tubing. The tubing depth is at 5800-5400. Chipco is running 50 sacks of regular class A cement in 5.5 casing. Good circulation. |
1406293247 | 2014-07-24 | Plug / Plug Back | No Violations | Chipco had ripped 5.5casing off and ran 1.5 tubing in to 4368. The pump truck could not pump on the tubing because the tubing was plugged off. They would pull the tubing out and round trip back in. |
1418228073 | 2014-12-09 | Final Restoration | No Violations | Final restoration passed on 12-9-14 by Patrick Shreve. Vegetation has been established to prevent erosion. |
1469193576 | 2010-01-05 | Production Wells | No Violations | Well is shut in and has been for some time. |
1617206024 | 2007-11-05 | Production Wells | No Violations | Well is shut in. Well is on plug list recently sent to WVA. (per Jeff Murrey) |
1809256060 | 2014-07-25 | Plug / Plug Back | No Violations | Chipco has ran 1.5tubing in to depth of 3952-3536 and set the clinton/ Rip plug of 120 sacks of regular class A cement. The lime plug was set at 2657-2457. They ran 60 sacks of regular Class A cement. The Bottom of the surface plug was at 1170-970. They ran 60 sacks of regular class A cement . The surface plug was at 200-0. They ran 60 sacks of regular class A cement. All plugs circulated. |
2132821366 | 2014-07-25 | Plug / Plug Back | No Violations | Well has been plugged in compliance with OAC 1501:9-11. This has resolved the Compliance Notices # 985074867,1357245521 and -1116706422. |
262691999 | 2013-4-10 0:00: | AM | No Violations | |
485255462 | 2004-2-18 0:00: | PL | No Violations | |
536526114 | 2014-7-24 0:00: | PB | No Violations | 1.00 |
985074867 | 2010-9-9 0:00:0 | WR | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1357245521 | US-OH-110331 | 2013-01-03 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1357245521 | US-OH-110332 | 2013-01-03 | Statement of annual production not filed |
For data sources see[8]