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34-121-21579

Well Details

Well ID: 34-121-21579
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Country: United States
State: Ohio
County: Noble
Municipality: Noble Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: SMITH C
License Status: Final Restoration
License Date: 2016-06-23
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.760000
Longitude: -81.560000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1974-03-04 2143 CARLESS RESOURCES INC GeoDate 3/4/74
Change of Owner 1998-07-06 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2016-06-23 Proposed Formations:CLINTON, Issued Date:6/23/2016, Expired Date:6/23/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-09-07 UPDATE SURFACE LOCATION PER INSPECTION 06/23/2016-ALE. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/10/16 ALE.
Record Last Modified 2017-02-10 UPDATE SURFACE LOCATION PER INSPECTION 06/23/2016-ALE. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/10/16 ALE.
Construction Permit Expires 2018-06-23 UPDATE SURFACE LOCATION PER INSPECTION 06/23/2016-ALE. UPDATED SURFACE LOCATION PER SURVEYORS COORDINATES 11/10/16 ALE.

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 2564.00 0.00 200
1987 ZILKHA ENERGY INC 1546.00 0.00 166
1988 CARLESS RESOURCES INC 1361.00 26.00 176
1989 CARLESS RESOURCES INC 1940.00 163.00 350
1995 CARLESS RESOURCES INC 894.00 157.00 365
1996 CARLESS RESOURCES INC 790.00 77.00 365
1997 CARLESS RESOURCES INC 660.00 0.00 365
1998 EXCO - NORTH COAST ENERGY INC 1303.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 1302.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 1315.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 912.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 824.00 94.00 365
2003 EXCO - NORTH COAST ENERGY INC 1437.00 81.00 365
2004 EXCO - NORTH COAST ENERGY INC 1434.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 667.00 0.00 365
2006 EXCO - NORTH COAST ENERGY INC 260.00 0.00 365
2007 EXCO - NORTH COAST ENERGY INC 466.00 0.00 365
2008 EXCO - NORTH COAST ENERGY INC 4.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 8
2016 ENERVEST OPERATING LLC 0.00 0.00 30

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 0 200
1987 ZILKHA ENERGY INC Brine 0 166
1988 CARLESS RESOURCES INC Brine 0 176
1989 CARLESS RESOURCES INC Brine 22 350
1995 CARLESS RESOURCES INC Brine 0 365
1996 CARLESS RESOURCES INC Brine 27 365
1997 CARLESS RESOURCES INC Brine 0 365
1998 EXCO - NORTH COAST ENERGY INC Brine 0 365
1999 EXCO - NORTH COAST ENERGY INC Brine 64 365
2000 EXCO - NORTH COAST ENERGY INC Brine 14 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 18 365
2004 EXCO - NORTH COAST ENERGY INC Brine 0 365
2005 EXCO - NORTH COAST ENERGY INC Brine 30 365
2006 EXCO - NORTH COAST ENERGY INC Brine 0 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 365
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 8
2016 ENERVEST OPERATING LLC Brine 52 30

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1276417309 2016-1-25 0:00: PW No Violations 1.00
-1350022227 2012-6-6 0:00:0 PW No Violations
-1597411629 2016-9-6 0:00:0 PB No Violations 7.50
0314182936 2016-09-07 Plug / Plug Back No Violations I am onsite to witness the plugging operations. Chipco pulled the tubing out of the well and attempted to find free pipe prior to my arrival. Appalachian was dispatched to cut the casing at 1760. The 4.5 casing was pulled to 1736 and a 60 sack plug was circulated in place. The casing was pulled up to 660 and a 60 sack bottom of surface casing plug was placed. A plug was then placed from 200 to surface. The company was instructed to reclaim the site in accordance with 1509.072(B).
1276417309 2016-01-25 Production Wells No Violations My inspection today finds the well is still shut in. A 210 barrel tank and horizontal separator remain in place 170 from the well The area around the well was covered by six inches of snow. I called Tim McConaha with Enervest at 3:50 pm. I Mr. McConaha indicated that no pipeline for gas was available and that the land owner has shown an interest in acquiring the well. Photos were taken.
1350022227 2012-06-06 Production Wells No Violations Inspection of the well head found 4.5 production casing -1.5 tubing -plunger lift well -with the production valves closed and no reported production since 2008. A 210 barrel tank and separator are present with no gas meter on site . Inspector will note A house has been built within 100 of the well head .
1466862340 2015-09-01 Production Wells Violations Noted At 2:21 pm on 8/31/2015, I received a telephone call from Mike Muffet the new owner of the property on which the well is situated. Mr. Muffet requested that I inspect the well. My inspection of the well finds the well is equipped with 4.5 casing and 1.5 tubing with a plunger lift system. All production valves are closed at the wellhead. The tank battery is comprised of one 210 barrel tank and a production unit. There is no meter at the tank battery, though there are two orifice meter runs. The well has reported zero gas and oil production since 2009. I called and spoke to Al Tarleton, production foreman for Enervest Operating. Mr. Tarleton indicated that the company was unable to utilize the well due to high line pressures and that the landowner was interested in buying the well. Plug the well within 180 days
1475513181 2016-09-29 Final Restoration No Violations My inspection today finds the well site meets the final restoration requirements of 1509.072(B).
1523405206 2016-05-17 Administrative Inspection No Violations I called and spoke to Mike Muffet, the landowner, and made him aware of the state of the violation against the well after he called Michelle Miller. I called and spoke to Tim McConaha with Enervest at 4:06 pm, and he stated that Enervest will be plugging the well, but a timeframe has not yet been established.
1597411629 2016-09-06 Plug / Plug Back No Violations I am onsite to witness the plugging operations. Appalachian cut the tubing at 5600. Chipco spotted a 30 sack class A plug from 5600 to 5200. Chipco could not pull the tubing so Appalachian cut the tubing off at 4300. Chipco pulled up to 4235 and set a 60 sack plug to 4000. Chipco pulled 2000 of tubing out of the well.
314182936 2016-9-7 0:00:0 PB No Violations 8.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1466862340 US-OH-113474 2016-09-30 Well shall be plugged

For data sources see[7]

References