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Well ID: 34-121-21948 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Enoch Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: BIG C RANCH | |
License Status: Final Restoration | |
License Date: 2012-08-29 | |
Spud Date: 1977-01-07 | |
Spud Drilling Contractor: | |
Final Drill Date: 1977-02-21 | |
Well Total Depth: 5994.00 ft | |
Configuration: Vertical | |
Latitude: 39.740000 | |
Longitude: -81.470000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-01-06 | 2143 CARLESS RESOURCES INC GeoDate 1/6/76 |
Original Spud | 1977-01-07 | |
Completed | 1977-02-21 | |
Reached Total Depth | 1977-02-21 | |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
APP | 2003-09-18 | Proposed Formations:CLINTON, Issued Date:9/18/2003, Expired Date:9/17/2004 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
APP | 2005-02-25 | Proposed Formations:CLINTON, Issued Date:2/25/2005, Expired Date:2/25/2006 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2012-08-29 | Proposed Formations:CLINTON, Issued Date:8/29/2012, Expired Date:8/29/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2012-09-28 | |
Construction Permit Expires | 2014-08-29 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5765 | 5836 | 11 |
5765 | 5836 | 11 | |
5765 | 5836 | 11 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1680 Bbl | 62900 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1914833968 | 2013-7-5 0:00:0 | FR | No Violations | 2.00 |
-319069882 | 2012-6-4 0:00:0 | PW | No Violations | |
-331423653 | 2012-6-6 0:00:0 | PW | No Violations | |
-35511708 | 2012-6-6 0:00:0 | PW | No Violations | |
0035511708 | 2012-06-06 | Production Wells | Violations Noted | Inspection revealed that well is shut in and equipped with 8 surface casing and 4.5 production casing and tubing string possibly set on packer it was stated by pumper that well had hole in casing and previous owner ran a packer in hole to try and repair with no avail,last production reported on said well was back in 2002.
Plug well within required time frame. Failure to comply may result in bond forfieture. |
0319069882 | 2012-06-04 | Production Wells | No Violations | Inspection of the well head found the following equipment -8.625 surface casing -4.5 production casing -1.5 tubing . A 100 barrel tank and separator are present also .Inspector will note 4.5 casing has a 1 hole in it just above the casing slips and is leaking gas ,well is shut in and is incapable of production due to general disrepair of all the equipment and a plugging permit was applied for but ran out in 2-25 2006,well has no reported production since 2001 . |
0331423653 | 2012-06-06 | Production Wells | No Violations | FOLLOW UP TO NOV # -35511708 Inspection revealed that well is shut in and equipped with 8 surface casing and 4.5 production casing and tubing string possibly set on packer it was stated by pumper that well had hole in casing and previous owner ran a packer in hole to try and repair with no avail,last production reported on said well was back in 2002.
Plug well within required time frame. Failure to comply may result in bond forfieture. |
1144594475 | 2006-04-07 | Production Wells | No Violations | Well is idle well owner had plug permit it expired 2/25/06 will contact company and try and determine if a reissued permit has been applied for before NOV is issued.
Suspect hole in casing.possibly yubing set on packer above hole in casing. |
1348697074 | 2012-09-26 | Plug / Plug Back | No Violations | Onsite with local inspector to go over plugging procedure for said well, we had operator pull tubing string and then Appalachian Well Services went in hole to perforate casing 200 into lime formation and then rig crew began to run tubing back into well they will set bottom hole and lime plug tomorrow. |
1348775788 | 2012-09-27 | Plug / Plug Back | No Violations | On site to assist local inspector with witnessing setting of bottom hole plug and lime plug, trace amounts of sulfur odor detected but no H2S reading on this day. |
1348871281 | 2012-09-28 | Production Wells | No Violations | Well has been plugged resolving previous Compliance Notice. |
1349106472 | 2012-09-26 | Plug / Plug Back | No Violations | My inspection today finds the well is equipped with 8.625 surface pipe, 4.5 casing, and 1.5 tubing. Chipco has moved a service rig on site to plug the well. |
1351859590 | 2012-11-02 | Final Restoration | No Violations | My inspection today finds the pit has been closed, and the all equipment has been removed. The site has been seeded and mulched. Some vegetation is growing. |
1914833968 | 2013-07-05 | Final Restoration | No Violations | Final restoration is complete. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0035511708 | US-OH-123733 | 2012-06-07 | General Safety | |
0035511708 | US-OH-123734 | 2012-06-07 | Well insufficiently equipped to prevent escape of oil and gas | |
0035511708 | US-OH-123735 | 2012-06-07 | Well shall be plugged | |
0035511708 | US-OH-123736 | 2012-06-07 | Defective casing, leaking well |
For data sources see[9]