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34-127-25485

Well Details

Well ID: 34-127-25485
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Country: United States
State: Ohio
County: Perry
Municipality: Jackson Township
Operator Name: JOHNSON MIKE
Well Pad ID:
Farm/Lease Name: STOLTZ DONALD
License Status: Final Restoration
License Date: 2013-09-23
Spud Date: 1982-01-29
Spud Drilling Contractor:
Final Drill Date: 1982-02-23
Well Total Depth: 2811.00 ft
Configuration: Vertical
Latitude: 39.720000
Longitude: -82.350000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-31 3110 APPALACHIAN WELL SUPPLY GeoDate 12/31/81
Oil and Gas 1981-12-31 Issued Date 12/31/81 Expired Date 12/31/82 Acres 0000000 Tool Type Proposed Formation Proposed Depth Proposed Drill Depth
Original Spud 1982-01-29
Completed 1982-02-23
Reached Total Depth 1982-02-23
CO 1991-12-09 37 HOPCO RESOURCES INC GeoDate 12/31/81
CO 1994-02-23 2573 JOHNSON M & GINGERICH M GeoDate 12/31/81
CO 1996-04-18 5460 JOHNSON MIKE GeoDate 12/31/81
APP 2013-09-23 Proposed Formations:CLINTON, Issued Date:9/23/2013, Expired Date:9/23/2015 12:00:00 PM, Drilling unit acres:115, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2013-11-15
Construction Permit Expires 2015-09-23
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2778 2780 0
2006-09-11 2776 2778 12
2776 2778 12
2776 2778 12
2006-09-11 2782 2784 0
2006-09-11 2788 2790 0
2006-09-11 2786 2788 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DORAN & ASSOCIATES 0.00 378.00 365
1985 DORAN & ASSOCIATES 0.00 304.00 365
1986 DORAN & ASSOCIATES 0.00 130.00 26
1987 DORAN & ASSOCIATES 0.00 0.00 0
1988 DORAN & ASSOCIATES 0.00 0.00 0
1992 JOHNSON M & GINGERICH M 0.00 114.00 365
1993 JOHNSON M & GINGERICH M 0.00 81.00 365
1994 JOHNSON M & GINGERICH M 0.00 155.00 365
1996 JOHNSON MIKE 0.00 143.00 365
1999 JOHNSON MIKE 0.00 0.00 0
2000 JOHNSON MIKE 0.00 91.00 0
2001 JOHNSON MIKE 0.00 40.00 365
2002 JOHNSON MIKE 0.00 0.00 365
2003 JOHNSON MIKE 0.00 32.00 365
2004 JOHNSON MIKE 0.00 0.00 365
2005 JOHNSON MIKE 0.00 0.00 365
2006 JOHNSON MIKE 0.00 22.00 365
2007 JOHNSON MIKE 0.00 51.00 365
2008 JOHNSON MIKE 0.00 0.00 365
2009 JOHNSON MIKE 0.00 0.00 365
2010 JOHNSON MIKE 0.00 0.00 365
2011 JOHNSON MIKE 0.00 15.00 365
2012 JOHNSON MIKE 0.00 13.00 366
2013 JOHNSON MIKE 0.00 0.00 289

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DORAN & ASSOCIATES Brine 0 365
1985 DORAN & ASSOCIATES Brine 290 365
1986 DORAN & ASSOCIATES Brine 2 26
1987 DORAN & ASSOCIATES Brine 0 0
1988 DORAN & ASSOCIATES Brine 0 0
1992 JOHNSON M & GINGERICH M Brine 0 365
1993 JOHNSON M & GINGERICH M Brine 0 365
1994 JOHNSON M & GINGERICH M Brine 0 365
1996 JOHNSON MIKE Brine 0 365
1999 JOHNSON MIKE Brine 0
2000 JOHNSON MIKE Brine 0
2001 JOHNSON MIKE Brine 0 365
2002 JOHNSON MIKE Brine 0 365
2003 JOHNSON MIKE Brine 0 365
2004 JOHNSON MIKE Brine 0 365
2005 JOHNSON MIKE Brine 0 365
2006 JOHNSON MIKE Brine 0 365
2007 JOHNSON MIKE Brine 0 365
2008 JOHNSON MIKE Brine 0 365
2009 JOHNSON MIKE Brine 0 365
2010 JOHNSON MIKE Brine 0 365
2011 JOHNSON MIKE Brine 0 365
2012 JOHNSON MIKE Brine 0 366
2013 JOHNSON MIKE Brine 0 289

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1369467434 2006-6-7 0:00:0 AD No Violations
-1534384738 2013-10-28 0:00 PB No Violations 1.00
-1572514110 2013-11-5 0:00: PB No Violations 2.00
-1749643484 2013-11-15 0:00 PB No Violations 2.00
-1970149390 2013-11-6 0:00: PB No Violations 1.00
-523108142 2013-10-31 0:00 PB No Violations 1.00
0072530162 2006-03-08 Annular Disposal Violations Noted An inspection of the well revealed no production since 2003, well is idle, trees and brush growing up in pump jack. No ID at the well head or tanks.
0523108142 2013-10-31 Plug / Plug Back No Violations I stopped by the well to see how they were getting along. They have got the 4 out of the well. The rig crew shut down do to the weather.
0882897780 2013-11-04 Plug / Plug Back No Violations The rig crew was on location working on plugging this well. They had to run some 4 back in the well to wash clay down. The fluid had come to the surface. They tagged the plug at 750ft in the morning.
1039777938 2007-11-09 Annular Disposal No Violations Follow-up on NOV, In-Compliance.
1099322380 2004-11-01 Production Wells No Violations
1231546257 2014-05-27 Final Restoration No Violations The final restoration meets 1509.072.
1358111111 2006-08-30 Annular Disposal No Violations Follow-up on NOV, Non-Compliance, took photos of violations, well still idle, no bridle and motor on pump jack.
1369467434 2006-06-07 Annular Disposal No Violations Follow-up on NOV, Non-Compliance.
1383673033 2013-11-01 Plug / Plug Back No Violations The rig crew set a brush and stone plug at 975ft. They then worked on putting plugging clay down on the plug.
1534384738 2013-10-28 Plug / Plug Back No Violations Mark Hines has moved in on well to plug it. They are rigged up and are getting ready to pull rods and tubing. The rig crew pulled out the rods and tubing.
1572514110 2013-11-05 Plug / Plug Back No Violations I stopped at the well to check how far the clay had settled. Mark tagged the plug at 150ft down. They washed in more clay and let it settle out. The rig crew rigged down to get the rig off of the hill before it rained.
1749643484 2013-11-15 Plug / Plug Back No Violations I stopped at this well to give them permission to cap off the well. The clay was still at the surface. I told Mark he could cut the well down and put the plate on the well. They started reclaiming the location.
1793615128 2014-04-23 Plug / Plug Back No Violations I stopped by this well to check the status of the restoration. The ground has been put back and reclaimed. There is seed and mulch spread across the location. The grass has started to grow. I will check back at a later date with the intern to do a final restoration on the well.
1970149390 2013-11-06 Plug / Plug Back No Violations The rig crew has moved everything off of location. The pit has been filled in. They left a pile of plugging clay next to the well to top it off again if it settles.
1993078222 2013-10-30 Plug / Plug Back No Violations Mark Hines has his rig on location. They washed in the bottom 500ft with plugging clay. They set up to rip 4 after that. The 4 was ripped at 1955ft. The rig crew pulled out 97ft to make sure they were free then washed in the Lime plug. They shut down for the day.
72530162 2006-3-8 0:00:0 AD No Violations
882897780 2013-11-4 0:00: PB No Violations 5.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0072530162 US-OH-128257 2006-03-13 Well shall be plugged

For data sources see[9]

References