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37-005-01279

Well Details

Well ID: 37-005-01279
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Kittanning Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: S D RUFFNER 1
License Status: INACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.777770
Longitude: -79.416786

For data sources see[1][2][3]

Well History

Date Event
1931-01-01 Drilling Completion
1986-01-01 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 894.00 365 0.00 0 0.00 0
1996 977 365 0.00 0 0.00 0
1998 1229 365 0.00 0 0.00 0
1999 CONSOL GAS CO 1026 365 0.00 0 0.00 0
2000 CONSOL GAS CO 740 365 0.00 0 0.00 0
2001 CONSOL GAS CO 819 365 0.00 0 0.00 0
2002 CONSOL GAS CO 883 365 0.00 0 0.00 0
2003 CONSOL GAS CO 757 365 0.00 0 0.00 0
2005 CONSOL GAS CO 806 365 0.00 0 0.00 0
2006 CONSOL GAS CO 789.00 365 0.00 0 0.00 0
2007 CONSOL GAS CO 225.00 365 0.00 0 0.00 0
2008 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2009 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2010 CONSOL GAS CO 0.00 0 0.00 0 0.00 0
2011 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2012 CNX GAS CO LLC 1.00 366 0.00 0 0.00 0
2013 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2014 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2015 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2016 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2017 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0
2018 CNX GAS CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2006 CONSOL GAS CO Brine 0.00 Bbl Other

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2205849 Primary Facility 2013-09-10 Routine/Complete Inspection No Violations Noted inactive status review
2466838 Primary Facility 2016-03-14 Routine/Complete Inspection No Violations Noted Well is tagged and shut in on approved inactive status 7/19/13. Spoke with operator and requested corroded well head casing be cleaned-painted to preserve mechanical integrity.
2816192 Primary Facility 2018-12-17 Compliance Evaluation Violation(s) Noted This well is tagged, shut in, not equipped for production as the sales line meter was removed and it is in violation of section 3220(a) failure to plug an abandoned well.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2816192 836741 2018-12-17 OGA3220(A) Environmental Health & Safety

For data sources see[7]

References