If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 37-015-20055 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":41.987858,"lon":-76.474448,"icon":""}]} |
Country: United States | |
State: Pennsylvania | |
County: Bradford | |
Municipality: Litchfield Township | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: WARNER 1 | |
License Status: PLUGGED & ABANDONED | |
Spud Date: | |
Permit Date: 2005-01-14 | |
Well Type: GAS | |
Unconventional Well: Y | |
Configuration: Vertical Well | |
Conservation: Yes | |
Latitude: 41.987858 | |
Longitude: -76.474448 |
Date | Event |
---|---|
2005-01-14 | New Permit Application |
2005-10-16 | Performed Spud Operation |
2006-08-25 | NEWLY DRILLED |
2014-03-03 | FULLY PLUGGED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | CHESAPEAKE APPALACHIA LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1735358 | Primary Facility | 2008-09-15 | Routine/Complete Inspection | No Violations Noted | Chesapeake was on site reworking a previously drilled well during the inspection. No violations were observed. |
2161773 | Primary Facility | 2013-04-23 | Follow-up Inspection | No Violations Noted | Cellar is dry. Filed for inactive status 3/29/06. Has expired. Talked to Eric Haskins of Ches. and he is submitting paperwork to continue inactive status. |
2203553 | Primary Facility | 2013-09-11 | Follow-up Inspection | No Violations Noted | 9 5/8 shut in, 0 psi |
2208622 | Primary Facility | 2013-09-25 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | progress downhole stopped 8114'. Encountered obstruction in open hole, tried to turn string with tongs, no success. Will set up top drive and attempt to make target depth.. |
2208626 | Primary Facility | 2013-09-26 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | circulate and drill ahead to 8350'. Encountered more obstructions. Change in procedure OK'd for 2 balance plugs, one @ deepest attained and the second across the 9 5/8 shoe. |
2208628 | Primary Facility | 2013-09-30 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | the cement balance plug @ 9 5/8 shoe tagged up short. O-tech to location to pump another balance plug to cover the 9 5/8 shoe with 19.5 bbls. of cement from 7820' to 7570'. |
2209379 | Primary Facility | 2013-10-02 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | wireline set CIBP in 9 5/8 @ 2960'. Pressure test to 4000 psi, test OK. run in hole to cut casing @ 2017'. 9 5/8 casing seemed free to pull, the casing jack crew was on site as I left. |
2219783 | Primary Facility | 2013-11-04 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Cellar has been dug out. Cap has been welded on - solid weld. Also, cut off 4+ feet below ground level. Check on restortation of pad plans - too deep? |
For data sources see[6]