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37-015-22202

Well Details

Well ID: 37-015-22202
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Country: United States
State: Pennsylvania
County: Bradford
Municipality: Albany Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 145323
Farm/Lease Name: SCHLAPFER N BRA 2H
License Status:
Spud Date:
Permit Date: 2012-05-02
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: Yes
Latitude: 41.602181
Longitude: -76.400728

For data sources see[1][2][3]

Well History

Date Event
2012-05-02 New Permit Application
2012-06-11 Performed Spud Operation
2012-12-28 Perforation
2013-02-05 New Permit Application
2014-01-28 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2013-01-12 2013-01-12 8,038 5,460,126

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 100 Mesh Sand FTS International Proppant - Natural Quartz 14808-60-7 100.00 1.40
10.1 - 15 HCL FTS International Acid Hydrochloric acid 7647-01-0 15.00 0.03
Water 7732-18-5 85.00 0.18
Recycled Produced Water Carrier/Base Fluid
Water 7732-18-5 100.00 28.12
B84, SC30 X-Chem Anti-Bacterial Agent, Scale Inhibitor Water 7732-18-5
B-84 X-Chem Antibacterial Agent Quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl, chlorides
68424-85-1 6.00 0.00149000
Glutaraldehyde 111-30-8 27.00 0.00733000
Didecyl dimethyl ammonium chloride 7173-51-5 8.00 0.00217000
Ethanol 64-17-5 4.00 0.00109000
FRW-600 FTS International Friction Reducer Distillates, petroleum, hydrotreated light 64742-47-8 30.00 0.01
Fresh Water Carrier/Base Fluid Water 7732-18-5 100.00 57.22
CI-150 (Corrosion Inhibitor) FTS International Corrosion Inhibitor N,N-Dimethylformamide 68-12-2 10.00 0.00007000
Isopropanol 67-63-0 60.00 0.00040000
Proprietary Organic Amine Resin Salt 30.00 0.00020000
Proprietary Aromatic Aldehyde 10.00 0.00007000
CI-150, FE-100L, FRW-600 FTS International Corrosion Inhibitor, Friction Reducer, Iron Control Agent Proprietary Corrosion Inhibitor Additive (CI-150)
Proprietary Friction Reducer Additive (FRW-600)
Water 7732-18-5
SC-30 X-Chem Scale Inhibitor Sodium polyacrylate 9003-04-7 100.00 0.00891000
Northern White Sand FTS International Proppant - Natural Quartz 14808-60-7 100.00 12.93
FE 100L (Iron Chelator) FTS International Iron Control Agent Citric acid 77-92-9 55.00 0.00064000
Additional Ingredients Not Listed on MSDS

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2012 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2013 CHESAPEAKE APPALACHIA LLC 1,739,725.00 227 0.00 0 0.00 0
2014 CHESAPEAKE APPALACHIA LLC 1,736,934.00 362 0.00 0 0.00 0
2015 CHESAPEAKE APPALACHIA LLC 1,432,420.00 365 0.00 0 0.00 0
2016 CHESAPEAKE APPALACHIA LLC 1,236,298.00 345 0.00 0 0.00 0
2017 CHESAPEAKE APPALACHIA LLC 1,005,467.00 331 0.00 0 0.00 0
2018 CHESAPEAKE APPALACHIA LLC 954,144.00 352 0.00 0 0.00 0
2019 CHESAPEAKE APPALACHIA LLC 862,331.00 365 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 CHESAPEAKE APPALACHIA LLC Drill Cuttings 719.43 Tons LANDFILL 8-0728-0004/013
2012 CHESAPEAKE APPALACHIA LLC Produced Fluid 1,206.62 Bbl REUSE OTHER THAN ROAD SPREADING
2012 CHESAPEAKE APPALACHIA LLC Drilling Fluid Waste 1,329.29 Bbl REUSE OTHER THAN ROAD SPREADING
2012 CHESAPEAKE APPALACHIA LLC Drill Cuttings 521.07 Tons LANDFILL THR029
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 7,124.60 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 216.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 52.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 771.67 Bbl REUSE OTHER THAN ROAD SPREADING
2015 CHESAPEAKE APPALACHIA LLC Produced Fluid 260.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 67.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 157.00 Bbl REUSE OTHER THAN ROAD SPREADING
2018 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 2.18 Tons LANDFILL 301626
2018 CHESAPEAKE APPALACHIA LLC Produced Fluid 108.00 Bbl REUSE (AT WELL PAD)
2018 CHESAPEAKE APPALACHIA LLC Produced Fluid 46.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2018 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 8.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2019 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 0.03 Tons LANDFILL 301626
2019 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 10.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2070322 Primary Facility 2012-05-23 Routine/Complete Inspection No Violations Noted
2084459 Primary Facility 2012-07-12 Drilling/Alteration No Violations Noted NOMAC 112, Comp. Man - Brad Merryfield drilling @ 6480'
2084577 Primary Facility 2012-07-19 Drilling/Alteration No Violations Noted NOMAC 112, Comp. Man - Dustin Smith, drilling at 12,083' TD @ 13,988'
2103342 Primary Facility 2012-09-27 Follow-up Inspection Violation(s) Noted Recieved notification of bubbles in cond X 13 3/8" annular space on Sept 24, 2012(e-mail from Jennifer Hoffman, Chesapeake). Bubbles are visible. Was able to get a reading of 11% LEL on MSA Altair multi-meter. (cellar is about 15' deep). I got a reading of XXX LEL(100%) and 100% methane from the 9 5/8 X 13 3/8" vent. Plastic containment with waste needs to be removed from site.
2109994 Primary Facility 2012-10-15 Follow-up Inspection Outstanding Violations - No Viols Req'd Cap has been installed on cond x surf = 20 X 13 3/8" annulus.
2140079 Primary Facility 2013-01-31 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Frac tanks on site. Some water on site.
2146531 Primary Facility 2013-03-07 Follow-up Inspection Outstanding Violations - No Viols Req'd On site to monitor csg annuli for gas.
2307895 Primary Facility 2014-09-24 Routine/Complete Inspection No Violations Noted
2505904 Primary Facility 2016-07-27 Routine/Complete Inspection No Violations Noted
2569024 Primary Facility 2017-03-08 Routine/Complete Inspection No Violations Noted Two Wells in production phase. To each sand and water separators. No leaks detected from production equipment. Site stable. No violations noted.
2712082 Primary Facility 2018-03-29 Routine/Complete Inspection No Violations Noted Two wells staged for production phase. Two each sand and water separators. No leaks detected from production equipment. No violations noted.
2712085 Primary Facility 2018-03-29 Routine/Complete Inspection No Violations Noted Two wells staged for production phase. Two each sand and water separators. No leaks detected from production equipment. No violations noted.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2103342 650315 09/27/2012 2012-09-27 78.81D1 - Failure to maintain control of anticipated gas storage reservoir pressures while drilling through reservoir or protective area Administrative

For data sources see[8]

References