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37-015-22226

Well Details

Well ID: 37-015-22226
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Country: United States
State: Pennsylvania
County: Bradford
Municipality: Albany Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 145323
Farm/Lease Name: SCHLAPFER S BRA 2H
License Status:
Spud Date:
Permit Date: 2012-05-23
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.602150
Longitude: -76.400764

For data sources see[1][2][3]

Well History

Date Event
2012-05-23 New Permit Application
2012-06-11 Performed Spud Operation
2012-12-28 Perforation
2014-01-28 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2013-01-12 2013-01-12 8,141 4,627,770

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 CI-150, FE-100L, FRW-600 FTS International Corrosion Inhibitor, Friction Reducer, Iron Control Agent Proprietary Corrosion Inhibitor Additive (CI-150)
Proprietary Friction Reducer Additive (FRW-600)
Water 7732-18-5
100 Mesh Sand FTS International Proppant - Natural Quartz 14808-60-7 100.00 1.32
Recycled Produced Water Carrier/Base Fluid 26.47
Northern White Sand FTS International Proppant - Natural Quartz 14808-60-7 100.00 12.14
10.1 - 15 HCL FTS International Acid Hydrochloric acid 7647-01-0 15.00 0.03
Water 7732-18-5 85.00 0.19
B-84 X-Chem Antibacterial Agent Didecyl dimethyl ammonium chloride 7173-51-5 8.00 0.00220000
Quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl, chlorides
68424-85-1 5.50 0.00151000
Glutaraldehyde 111-30-8 27.00 0.00742000
Ethanol 64-17-5 4.00 0.00110000
CI-150 (Corrosion Inhibitor) FTS International Corrosion Inhibitor Proprietary Aromatic Aldehyde 10.00 0.00011000
Proprietary Organic Amine Resin Salt 30.00 0.00032000
Isopropanol 67-63-0 60.00 0.00063000
N,N-Dimethylformamide 68-12-2 10.00 0.00011000
Proprietary Quaternary Ammonium Compound 10.00 0.00011000
FE 100L (Iron Chelator) FTS International Iron Control Agent Citric acid 77-92-9 55.00 0.00042000
B84, SC30 X-Chem Anti-Bacterial Agent, Scale Inhibitor Water 7732-18-5
Fresh Water Carrier/Base Fluid 59.72
FRW-600 FTS International Friction Reducer Distillates, petroleum, hydrotreated light 64742-47-8 30.00 0.01
Additional Ingredients Not Listed on MSDS
SC-30 X-Chem Scale Inhibitor Sodium polyacrylate 9003-04-7 100.00 0.00905000

For data sources see[5]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2012 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2013 CHESAPEAKE APPALACHIA LLC 1,540,277.00 227 0.00 0 0.00 0
2014 CHESAPEAKE APPALACHIA LLC 1,420,060.00 358 0.00 0 0.00 0
2015 CHESAPEAKE APPALACHIA LLC 1,067,079.00 364 0.00 0 0.00 0
2016 CHESAPEAKE APPALACHIA LLC 962,964.00 344 0.00 0 0.00 0
2017 CHESAPEAKE APPALACHIA LLC 770,960.00 326 0.00 0 0.00 0
2018 CHESAPEAKE APPALACHIA LLC 738,020.00 351 0.00 0 0.00 0
2019 CHESAPEAKE APPALACHIA LLC 637,093.00 365 0.00 0 0.00 0

For data sources see[6]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2012 CHESAPEAKE APPALACHIA LLC Drill Cuttings 922.31 Tons LANDFILL 8-0728-0004/013
2012 CHESAPEAKE APPALACHIA LLC Drill Cuttings 559.86 Tons LANDFILL THR029
2012 CHESAPEAKE APPALACHIA LLC Produced Fluid 54.00 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 216.00 Bbl RESIDUAL WASTE PROC FAC (GENERAL PERMIT) WMGR123
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 52.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE WMGR119
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 7,124.60 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 771.67 Bbl REUSE OTHER THAN ROAD SPREADING
2015 CHESAPEAKE APPALACHIA LLC Produced Fluid 260.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 67.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC010
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 157.00 Bbl REUSE OTHER THAN ROAD SPREADING
2018 CHESAPEAKE APPALACHIA LLC Produced Fluid 108.00 Bbl REUSE (AT WELL PAD)
2018 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 8.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2018 CHESAPEAKE APPALACHIA LLC Produced Fluid 46.50 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008
2018 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 2.18 Tons LANDFILL 301626
2019 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 0.03 Tons LANDFILL 301626
2019 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 10.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008

For data sources see[7]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2086714 Primary Facility 2012-07-26 Drilling/Alteration No Violations Noted NOMAC 112, Comp. Man - Dustin Smith, checked drillers log, @492'
2090789 Primary Facility 2012-08-08 Drilling/Alteration No Violations Noted NOMAC 112, Comp. Man - Brad Merryfield, drilling @ 10478'
2094342 Primary Facility 2012-08-21 Routine/Complete Inspection Pending Rig has moved off. Crew is washing mats. Conductor has water in it and there appears to be bubbles. Need to investigate further.
2095680 Primary Facility 2012-08-28 Follow-up Inspection Pending Cap has not been installed on the 20" x 13 3/8" annulus yet. The annulus is still bubbling.
2096543 Primary Facility 2012-08-31 Follow-up Inspection Violation(s) Noted Used bubble sampler & Altair MSA 5X multi-meter to sample bubbles in 20" X 13 3/8" annulus - got reading of 50% methane. This is a violation of PA Code 25 Chap 78.81 & 78.86. Had been pending until I was able to confirm bubbles were methane. ( Ches. notified the Dept of bubbles after The Dept. had already discovered them.)
2104539 Primary Facility 2012-09-27 Follow-up Inspection Outstanding Violations - No Viols Req'd Cap and vent have been installed on the cond x 13 3/8" annulus. Checked with MSA Altair multi-meter 9 5/8" x 13 3/8" annulus , reading of XXX combustible(excedes 100% LEL) and 10% methane, and 13 3/8 x 20" annulus reading of xxx comb(excedes 100% LEL) and 52% methane
2109989 Primary Facility 2012-10-15 Follow-up Inspection Outstanding Violations - No Viols Req'd Tested annular vents for comb gas and methane using MSA Altair 5x multi meter.
2140087 Primary Facility 2013-01-31 Routine/Complete Inspection Outstanding Violations - No Viols Req'd Frac tanks on site. Some water in cellar.
2146536 Primary Facility 2013-03-07 Follow-up Inspection Outstanding Violations - No Viols Req'd On site to monitor csg annuli for gas.
2307896 Primary Facility 2014-09-24 Routine/Complete Inspection No Violations Noted
2505907 Primary Facility 2016-07-27 Routine/Complete Inspection No Violations Noted

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2096543 648114 08/31/2012 2012-08-31 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
648114 288384 NOV - Notice of Violation

For data sources see[8]

References