If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 37-021-20897 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.70577,"lon":-78.788931,"icon":""}]} |
Country: United States | |
State: Pennsylvania | |
County: Cambria | |
Municipality: Susquehanna Township | |
Operator Name: ALLIANCE PETRO CO LLC | |
Well Pad ID: | |
Farm/Lease Name: BUBLINEC UNIT 4 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2003-12-02 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.705770 | |
Longitude: -78.788931 |
Date | Event |
---|---|
2003-12-02 | New Permit Application |
2004-02-04 | Performed Spud Operation |
2004-02-10 | Drilling Completion |
2004-02-27 | Perforation |
2005-02-03 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2005 | CONSOL GAS CO | 9640 | 365 | 0.00 | 0 | 0.00 | 0 |
2006 | CONSOL GAS CO | 7583.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2007 | CONSOL GAS CO | 3692.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | CONSOL GAS CO | 4265.20 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | CONSOL GAS CO | 5547.47 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | CONSOL GAS CO | 4,036.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | CONSOL GAS CO | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | CNX GAS CO LLC | 3,388.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | CNX GAS CO LLC | 3,320.25 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | CNX GAS CO LLC | 3,180.33 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | CNX GAS CO LLC | 3,036.18 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | CNX GAS CO LLC | 2,275.82 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | CNX GAS CO LLC | 1,278.66 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | CNX GAS CO LLC | 1,091.03 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | ALLIANCE PETRO CO LLC | 3,056.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2005 | CONSOL GAS CO | Brine | 22.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2006 | CONSOL GAS CO | Brine | 0.00 Bbl | Other | |
2008 | CONSOL GAS CO | Brine | 89.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0026034 |
2009 | CONSOL GAS CO | Brine | 28.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095273 |
2012 | CNX GAS CO LLC | Produced Fluid | 74.50 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2015 | CNX GAS CO LLC | Produced Fluid | 29.84 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2363328 | Primary Facility | 2015-04-22 | Administrative/File Review | In Compliance with Policy | Admin inspection. |
2363744 | Primary Facility | 2015-04-23 | Incident- Response to Accident or Event | Violation(s) Noted | Inspection performed as a follow-up to a spill/discharge notification reported to the Department by the operator outlining a release of approximately 10 barrels (420 gallons) of produced fluids. Inpsection confirmed the reported details of the spill. Spill area was limited to the diked area around the brine tank. Soil excavation and sampling activities had been completed on 04/22/15. The brine tank was still disconnected from the well apparatus and otherwise appeared to be in sound condition. |
2368936 | Primary Facility | 2015-05-01 | Follow-up Inspection | Outstanding Violations - No Viols Req'd | On-site FUI in response to violations issued under inspection record 2363744 (enf ID 322365) for the 4/22/15 reportable release of 10 bbl brine water.At time of inspt, BT disconnected from well.Well label present.Area of excavation not yet backfilled.All visibly impacted materials appear removed.Dept recom'ds Opr install temp BMPs down-gradient of excavated areas as appropriate and continue to monitor/maintain shared AR as necessary in order to prevent any potential pollution events from occurring.A FUI will be conducted in future to ensure site is properly remediated and restored.Outstanding viols exist under record 2363744 (enf ID 322365), no new viols noted at this time.Requested written response to viols not yet received.Per spill policy, 15 day initial report received by Dept on 5/1/15 notifying Dept that Opr will be utilizing Alternative Remediation method for site remediation.SCR not yet received by Dept.Envir'l Trainee Cindy Witham present during inspt. |
2381690 | Primary Facility | 2015-06-12 | Compliance Evaluation | No Violations Noted | On-site CEI in response to viols issued under record 2363744 (enf ID 322365) for the 4/22/15 reportable release of 10 bbl brine.At time of inspt, BT appears re-equipped to well.Well label present.BT located on gravel pad w/in re-structured earthen dike.Previously disturbed areas backfilled,temporarily stabilized with seed/mulch,nearing 70% uniform and adequate veg growth.In accordance w/Spill Policy, 15 day initial written report received on 5/1 notifying Dept that Opr will be utilizing Alternative Remediation Method for remediation of release.SCR received by Dept on 5/11.As site is backfilled & temp stabilized & SCR submitted for review by ECB, viols issued under record 2363744 (enf ID 322365) have been corrected.Dept recom’ds Opr cont’ to mon/maintain site to ensure >70% uniform & adequate veg is attained for final perm stabilization of site & cont’ to mon/maintain shared AR as necessary.A FUI is anticipated to be conducted to ensure site is properly restored per current regs.Viols may be forthcoming pending inspts monitoring site restoration. |
2552287 | Primary Facility | 2017-01-12 | Routine/Complete Inspection | No Violations Noted | At time of inspection no E&S issues observed on access road or on site. Well appears equipped for production. Well tag present. Brine tank located in earthen dike appears structurally sound.
On 4-22-15 the Operator reported a release of 10 bbl of brine into the dike. At this time the excavated area appears permanently stabilized. Vegetation appears to have reached >70% uniform growth. |
2628795 | Primary Facility | 2017-08-24 | Routine/Complete Inspection | No Violations Noted | Well appears equipped for production. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2363744 | 720854 | 04/23/2015 | 2015-04-23 | 78.57(a) - CONTROL, STORAGE AND DISPOSAL OF PRODUCTION FLUIDS - Operator failed to collect the brine and other fluids produced during operation, service and plugging of the well in a tank, pit or a series of pits or tanks, or other device approved by | Environmental Health & Safety |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
720854 | 322365 | NOV - Notice of Violation | |||||
720854 | 369521 | CACP - Consent Assessment of Civil Penalty | Comply/Closed | 2018-11-15 | 2018-11-15 | $8,350.00 | $8,350.00 |
For data sources see[7]