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37-031-01015

Well Details

Well ID: 37-031-01015
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Country: United States
State: Pennsylvania
County: Clarion
Municipality: Millcreek Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: MIDLAND 48
License Status: ACTIVE
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 41.304799
Longitude: -79.228451

For data sources see[1][2][3]

Well History

Date Event
1928-08-01 Drilling Completion
1987-08-11 OLD WELL

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 HANLEY & BIRD INC 747.00 365 0.00 0 0.00 0
1996 HANLEY & BIRD INC 332.31 365 0.00 0 0.00 0
1997 HANLEY & BIRD INC 265.58 365 0.00 0 0.00 0
1998 HANLEY & BIRD INC 643.58 365 0.00 0 0.00 0
1999 HANLEY & BIRD INC 470.06 365 0.00 0 0.00 0
2000 HANLEY & BIRD INC 438.81 365 0.00 0 0.00 0
2001 HANLEY & BIRD INC 431.13 365 0.00 0 0.00 0
2002 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2003 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2004 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2005 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2006 HANLEY & BIRD INC 0.00 0 0.00 0 0.00 0
2008 HANLEY & BIRD INC 317.62 365 0.00 0 0.00 0
2009 HANLEY & BIRD INC 311.57 365 0.00 0 0.00 0
2010 HANLEY & BIRD INC 314.75 365 0.00 0 0.00 0
2011 EXCO RESOURCES PA LLC 230.00 365 0.00 0 0.00 0
2012 EXCO RESOURCES PA LLC 241.00 180 0.00 0 0.00 0
2013 EXCO RESOURCES PA LLC 703.00 365 0.00 0 0.00 0
2014 EXCO RESOURCES PA LLC 309.00 365 0.00 0 0.00 0
2015 EXCO RESOURCES PA LLC 208.72 273 0.00 0 0.00 0
2016 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 HANLEY & BIRD INC Produced Fluid 2.39 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0101508

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2814069 Primary Facility 2018-12-12 Routine/Complete Inspection Violation(s) Noted Well is abandoned. Well tag needs replaced. Site id sign needs replaced. Well production casing has dropped down the hole. Production submitted for 2017 shows zero flow.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2814069 836040 2018-12-12 2019-03-07 OGA3220(A) Environmental Health & Safety
2814069 836041 2018-12-12 2019-03-07 78.86 Environmental Health & Safety

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
836040 369711 NOV - Notice of Violation 2019-03-07
836040 372946 COA - Consent Order and Agreement
836041 369711 NOV - Notice of Violation 2019-03-07

For data sources see[7]

References