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Well ID: 37-047-23841 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Elk | |
Municipality: Ridgway Township | |
Operator Name: DIVERSIFIED OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: FEE HEARTWOODS FORESTLAND FUND II 38244 | |
License Status: ACTIVE | |
Spud Date: | |
Permit Date: 2007-03-07 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.493374 | |
Longitude: -78.651586 |
Date | Event |
---|---|
2007-03-07 | New Permit Application |
2007-04-23 | Performed Spud Operation |
2007-04-25 | Drilling Completion |
2007-10-26 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2007 | SENECA RESOURCES CO LLC | 4739.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2008 | SENECA RESOURCES CO LLC | 3310.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2009 | SENECA RESOURCES CO LLC | 1867.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2010 | SENECA RESOURCES CO LLC | 1,296.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | SENECA RESOURCES CO LLC | 2,661.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | SENECA RESOURCES CO LLC | 2,227.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2013 | SENECA RESOURCES CO LLC | 1,261.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | SENECA RESOURCES CO LLC | 1,312.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | SENECA RESOURCES CO LLC | 1,210.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | DIVERSIFIED OIL & GAS LLC | 1,409.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2017 | DIVERSIFIED OIL & GAS LLC | 326.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | DIVERSIFIED OIL & GAS LLC | 1,612.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | DIVERSIFIED OIL & GAS LLC | 1,058.00 | 334 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2008 | SENECA RESOURCES CO LLC | Brine | 58.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0101508 |
2009 | SENECA RESOURCES CO LLC | Servicing Fluid | 25.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0102784 |
2013 | SENECA RESOURCES CO LLC | Produced Fluid | 80.00 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123NW005 |
2015 | SENECA RESOURCES CO LLC | Produced Fluid | 50.00 Bbl | REUSE OTHER THAN ROAD SPREADING | |
2017 | DIVERSIFIED OIL & GAS LLC | Produced Fluid | 45.00 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NW005 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2682428 | Primary Facility | 2018-01-12 | Incident- Response to Accident or Event | Violation(s) Noted | On 1/12/18 at 1028 hrs. I conducted an incident inspection in response to possible storage tank release at Diversified's 38244 well site (API 047-23841) in Ridgway, Elk Co. Upon inspection of the tank and surrounding areas, I discovered a small area of soil in the containment berm with conductivity over the range of my conductivity meter (over 20 mS/cm). The storage tank also appeared to have a small pinhole leak in the bottom. The tank had been disconnected and tipped on its side. The overall release was most likely less than a barrel of fluid, given the small amount of impacted soil. A visual cleanup/screened cleanup of the berm is required.
The release was unreported to the Department and constitutes violations of 91.33(a) and 78.66(a) which have been immediately resolved. Violations of 78.57(a), CSL 402(b), and SWMA 301 will be resolved upon cleanup of the release area and submission of disposal receipts to the Department. |
2726323 | Primary Facility | 2018-05-04 | Compliance Evaluation | No Violations Noted | On 5/4/18 at 0945 hrs., I conducted a compliance evaluation inspection of Diversified's 38244 well site (API 047-23841) in Ridgway Twp., Elk Co. Of particular concern was the status of the violations from inspection ID 2682428, which were cited due to a small brine release from the production fluids tank. On 4/26/18, I received an email notification from Kirk Elkin with Diversified stating that the cleanup had been completed for several months and that the production fluid tank had been repaired and re-connected for production. Upon inspection, the impacted soil from the containment berm had been removed and the berm was temporarily stabilized. The production fluids tank was repaired and re-connected for service. This inspection resolves violation ID numbers 805947, 805948, and 805949 from inspection ID 2682428. |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2682428 | 805945 | 2018-01-12 | 2018-01-12 | 91.33(A) | Environmental Health & Safety | The operator failed to report a brine release to the Department. |
2682428 | 805946 | 2018-01-12 | 2018-01-12 | 78.66(b) | Environmental Health & Safety | The operator failed to report a brine release to the Department. |
2682428 | 805947 | 2018-01-12 | 2018-05-04 | CSL 402(b) | Environmental Health & Safety | Unreported release of brine from a storage tank. |
2682428 | 805948 | 2018-01-12 | 2018-05-04 | SWMA 301 | Environmental Health & Safety | Unreported brine release from a storage tank. |
2682428 | 805949 | 2018-01-12 | 2018-05-04 | 78.57(a) | Environmental Health & Safety | Unreported brine release from a storage tank. |
Violation ID | Penalty ID | Penalty Code | Penalty Status | Penalty Date | Enforcement Date | Penalty Amount | Amount Collected |
---|---|---|---|---|---|---|---|
805945 | 362359 | NOV - Notice of Violation | 2018-05-04 | ||||
805946 | 362359 | NOV - Notice of Violation | 2018-05-04 | ||||
805947 | 362359 | NOV - Notice of Violation | 2018-05-04 | ||||
805948 | 362359 | NOV - Notice of Violation | 2018-05-04 | ||||
805949 | 362359 | NOV - Notice of Violation | 2018-05-04 |
For data sources see[7]