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37-131-20169

Well Details

Well ID: 37-131-20169
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Country: United States
State: Pennsylvania
County: Wyoming
Municipality: Meshoppen Township
Operator Name: CHESAPEAKE APPALACHIA LLC
Well Pad ID: 147744
Farm/Lease Name: AUKEMA 7H
License Status:
Spud Date: 2011-07-29
Permit Date: 2011-05-10
Well Type: GAS
Unconventional Well: Y
Configuration: Horizontal Well
Conservation: No
Latitude: 41.627828
Longitude: -76.073867

For data sources see[1][2][3]

Well History

Date Event
2011-05-10 New Permit Application
2011-07-16 Performed Spud Operation
2011-08-16 Drilling Completion
2011-09-01 Perforation
2011-09-01 Performed Stimulation
2012-08-15 DEVIATED

For data sources see[4]

Fracking Activities

Fracking Jobs

Job Number Job Start Date Job End Date True Vertical Depth (ft) Total Water Volume (gal) Total Non-Water Volume (gal)
1 2011-09-28 2011-09-28 7,587 3,964,926

Fluid Composition Data

Job Number Trade Name Supplier Purpose Ingredient Name CAS Number Additive Percentage by Mass Job Percentage by Mass Mass Used (lb)
1 Scale Inhibitor - Gyptron T-390 Champion Technologies Scale Inhibitor Methanol 67-56-1 10.00 0.00110000
Biocide - Bactron K 139 Champion Technologies Antibacterial Agent Quaternary ammonium compounds,
benzyl-C12-16-alkyldimethyl, chlorides
68424-85-1 10.00 0.00297000
Ethanol 64-17-5 5.00 0.00148000
Glutaraldehyde 111-30-8 5.00 0.00148000
CI-150 (Corrosion Inhibitor) Frac Tech Services (FTS) Corrosion Inhibitor Organic Amineresin Salt 30.00 0.00041000
Aromatic Aldehyde 10.00 0.00014000
N,N-Dimethylformamide 68-12-2 10.00 0.00014000
Quaternary Ammonium Compounds 10.00 0.00014000
Isopropanol 67-63-0 60.00 0.00083000
FRW-200 Frac Tech Services (FTS) Friction Reducer No Hazardous Components 0.00
FE 100L (Iron Chelator) Frac Tech Services (FTS) Iron Control Agent No Hazardous Components 0.00
10.1 - 15 HCL Frac Tech Services (FTS) Acid Water 7732-18-5 85.00 0.45
Hydrochloric acid 7647-01-0 15.00 0.08
Recycled Produced Water Carrier/Base Fluid 14.47
Fresh Water Carrier/Base Fluid 70.36
Sand (Proppant) Proppant 14.49

For data sources see[5]

Stimulation Data

Stimulation Date Phase Number Chemical Agent Volume (gal) Treating Pressure (psi) Breakdown Pressure (psi)
2011-09-01 0 0 0

For data sources see[6]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 CHESAPEAKE APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2012 CHESAPEAKE APPALACHIA LLC 1,878,361.00 240 0.00 0 0.00 0
2013 CHESAPEAKE APPALACHIA LLC 2,512,601.00 365 0.00 0 0.00 0
2014 CHESAPEAKE APPALACHIA LLC 1,644,507.00 360 0.00 0 0.00 0
2015 CHESAPEAKE APPALACHIA LLC 1,018,184.00 316 0.00 0 0.00 0
2016 CHESAPEAKE APPALACHIA LLC 1,041,961.00 360 0.00 0 0.00 0
2017 CHESAPEAKE APPALACHIA LLC 839,365.00 364 0.00 0 0.00 0
2018 CHESAPEAKE APPALACHIA LLC 721,120.00 358 0.00 0 0.00 0
2019 CHESAPEAKE APPALACHIA LLC 576,108.00 365 0.00 0 0.00 0

For data sources see[7]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2011 CHESAPEAKE APPALACHIA LLC Drilling Fluid Waste 2,370.00 Bbl REUSE OTHER THAN ROAD SPREADING
2012 CHESAPEAKE APPALACHIA LLC Produced Fluid 816.39 Bbl REUSE OTHER THAN ROAD SPREADING
2013 CHESAPEAKE APPALACHIA LLC Produced Fluid 946.05 Bbl REUSE OTHER THAN ROAD SPREADING
2014 CHESAPEAKE APPALACHIA LLC Produced Fluid 494.55 Bbl REUSE OTHER THAN ROAD SPREADING
2015 CHESAPEAKE APPALACHIA LLC Produced Fluid 241.00 Bbl REUSE OTHER THAN ROAD SPREADING
2016 CHESAPEAKE APPALACHIA LLC Produced Fluid 320.00 Bbl REUSE OTHER THAN ROAD SPREADING
2018 CHESAPEAKE APPALACHIA LLC Waste Water Treatment Sludge 1.00 Tons LANDFILL 301626
2018 CHESAPEAKE APPALACHIA LLC Other Oil & Gas Wastes 412.20 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NC008

For data sources see[8]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1990382 Primary Facility 2011-07-22 Drilling/Alteration No Violations Noted Still working on site, E & S. Comp. man - Wes Nix
1992498 Primary Facility 2011-08-01 Drilling/Alteration No Violations Noted Drillers log checked, at 962', Patterson 259, Comp. Man - Wes Nix
1994087 Primary Facility 2011-08-08 Drilling/Alteration No Violations Noted Patterson 259, Co. Man - Dalen Burr, checked drillers log - at 4174'
1995313 Primary Facility 2011-08-12 Drilling/Alteration No Violations Noted Patterson UTI 259 Checked drillers log - good, at 7971' Comp Man - Dalen
1996382 Primary Facility 2011-08-17 Drilling/Alteration No Violations Noted Patterson UTI 259, David Nix - Comp. Man
1998207 Primary Facility 2011-08-24 Drilling/Alteration No Violations Noted Moving equipment off site and cleaning up.
2002560 Primary Facility 2011-09-14 Routine/Complete Inspection Pending Cellar full of water. Bubbles coming out of a vent (can't tell which). See video.
2003132 Primary Facility 2011-09-15 Routine/Complete Inspection Pending Cellar is pumped out as requested. Vent where bubbles had been coming out has been extended up higher, but comes from 13 3/8 X 9 5/8" annulus. ( I don't have gas meter)
2004639 Primary Facility 2011-09-20 Follow-up Inspection Violation(s) Noted
2004650 Primary Facility 2011-09-22 Follow-up Inspection Violation(s) Noted Returned to this site to take more photos. A Ches. emp. was on site monitoring this well. He confirmed the bubbles I saw was 'venting' and that it was coming from the 9 5/8 X 13 3/8" annulus.Vio. as per Title 25 Chapter 78. 86 - Defective Casing or Cementing. It is a vio. for not finding and reporting defective cementing within 24 hours. It is also a vio. of 78.86 for not taking action to correct this defect. You shall correct defect or submit a plan to correct this defect within 30 days(by Oct 21, 2011).
2009544 Primary Facility 2011-10-11 Routine/Complete Inspection Pending Well appears to have been fraced. 14 tanks on site, 5 fresh water, 9 brine. Also a pile of sand and a hoe. Tanks and sand on plastic.
2044431 Primary Facility 2012-02-21 Routine/Complete Inspection No Violations Noted
2051089 Primary Facility 2012-03-16 Administrative/File Review No Violations Noted Reviewed Inspection Reports 11/7 thru 12/12/2011
2102760 Primary Facility 2012-09-13 Routine/Complete Inspection No Violations Noted Well is drilled, fraced, and producing.
2751450 Primary Facility 2018-07-12 Administrative/File Review No Violations Noted Received and reviewed Post-Drilling Well Site Restoration Report.

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2004639 620672 09/20/2011 2011-09-20 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative
2004650 620676 09/20/2011 2011-09-20 78.86* - Failure to report defective, insufficient, or improperly cemented casing w/in 24 hrs or submit plan to correct w/in 30 days Administrative

For data sources see[9]

References