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34-153-23095

Well Details

Well ID: 34-153-23095
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2009-10-12
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 40.9481568439
Longitude: -81.6231152991

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-724292814 2009-10-22 Whipstock is still on site for maintenance. The 7" annular pressure was 0 psi and is still vented into a 300 bbl frac tank.
-787777382 2009-10-28 The well will be fraced in the near future. The tank battery is under construction and the salesline is being installed.
1156595749 2009-10-17 Ran cement bond log. Highest evidence of cement at 1370'. Top of cement at 1704'. DV tool at 2360'. Pressure on 7 dia annulus was 350 psi. Will drill out cement and DV tool with 6-1/4 dia bit.
1255538837 2009-10-13 Cemented surface casing. The drilling pits are fenced off and the pit liners are intact.
1256052744 2009-10-15 Whipstock hit a solution mine void at 2846'. Will set 7 dia casing and will do a 2-stage cement job using a DV tool.
1256053556 2009-10-16 Cemented 7 casing (3208' set at 3220' KB) using a DV tool set at 2366'. Lost circulation 40 bbls into the 2nd stage of displacement. Did not circulate cement to surface. Will wait on cement 12 hrs and run a cement bond log to determine height of cement on the back side of the 7.
1256310312 2009-10-20 Drilling is completed but Whipstock is still on site for maintenance. The drilling pits are lined, fenced and in good condition. The 7" casing annulus is plumbed into a 300 bbl frac tank and open to prevent pressure build up.
1356617280 2012-12-26 I inspected this location on 12/26/2012. This well is operated on a Plunger Lift System. All piping and fittings were found to be leak free and in working order. I found 580psi on the casing, 340 psi on the tubing, and 8 psi on the 8.625" annulus. Signage was in place and legible. The Tank battery consisted of a 140 Bbl. Stock tank, a 35 Bbl. Brine tank, 2408 Separator and Gas measuring station. All piping and tankage was found to be leak-free and in working order. No violations were identified at this time.
228511595 2010-08-16 Preliminary restoration is approved.