If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-153-23095 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.9481568439,"lon":-81.6231152991,"icon":""}]} |
County: | |
Municipality: | |
Operator Name: | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2009-10-12 | |
Unconventional: | |
Horizontal: | |
Producing: No | |
Violations: 0 | |
Latitude: 40.9481568439 | |
Longitude: -81.6231152991 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION_COMMENT |
---|---|---|---|---|---|---|
-724292814 | 2009-10-22 | Whipstock is still on site for maintenance. The 7" annular pressure was 0 psi and is still vented into a 300 bbl frac tank. | ||||
-787777382 | 2009-10-28 | The well will be fraced in the near future. The tank battery is under construction and the salesline is being installed. | ||||
1156595749 | 2009-10-17 | Ran cement bond log. Highest evidence of cement at 1370'. Top of cement at 1704'. DV tool at 2360'. Pressure on 7 dia annulus was 350 psi. Will drill out cement and DV tool with 6-1/4 dia bit. | ||||
1255538837 | 2009-10-13 | Cemented surface casing. The drilling pits are fenced off and the pit liners are intact. | ||||
1256052744 | 2009-10-15 | Whipstock hit a solution mine void at 2846'. Will set 7 dia casing and will do a 2-stage cement job using a DV tool. | ||||
1256053556 | 2009-10-16 | Cemented 7 casing (3208' set at 3220' KB) using a DV tool set at 2366'. Lost circulation 40 bbls into the 2nd stage of displacement. Did not circulate cement to surface. Will wait on cement 12 hrs and run a cement bond log to determine height of cement on the back side of the 7. | ||||
1256310312 | 2009-10-20 | Drilling is completed but Whipstock is still on site for maintenance. The drilling pits are lined, fenced and in good condition. The 7" casing annulus is plumbed into a 300 bbl frac tank and open to prevent pressure build up. | ||||
1356617280 | 2012-12-26 | I inspected this location on 12/26/2012. This well is operated on a Plunger Lift System. All piping and fittings were found to be leak free and in working order. I found 580psi on the casing, 340 psi on the tubing, and 8 psi on the 8.625" annulus. Signage was in place and legible. The Tank battery consisted of a 140 Bbl. Stock tank, a 35 Bbl. Brine tank, 2408 Separator and Gas measuring station. All piping and tankage was found to be leak-free and in working order. No violations were identified at this time. | ||||
228511595 | 2010-08-16 | Preliminary restoration is approved. |