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Difference between revisions of "37-129-00667"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-129-00667
 
| Well ID: 37-129-00667
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.234786, -79.787361 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.234786, -79.787361 | width=100% | height=100% }}
 
|-
 
|-
 
| Country: United States
 
| Country: United States
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| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name: D M CURRY 670100
+
| Farm/Lease Name: D M CURRY
 
|-
 
|-
| License Status: Plugged OG Well
+
| License Status: Plugged and Abandoned
 
|-
 
|-
| Spud Date: 1800-01-01
+
| Spud Date:  
 
|-
 
|-
 
| Permit Date:  
 
| Permit Date:  
 +
|-
 +
| Well Type: GAS
 
|-
 
|-
 
| Unconventional Well: N
 
| Unconventional Well: N
 
|-
 
|-
 
| Configuration: Vertical Well
 
| Configuration: Vertical Well
 +
|-
 +
| Conservation: No
 
|-
 
|-
 
| Latitude: 40.234786
 
| Latitude: 40.234786
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  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 
  | accessdate = 2019-05-21 }}</ref>
 
  | accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Date
 +
!scope="col" | Event
 +
|-
 +
| 1902-08-27
 +
| Drilling Completion
 +
|-
 +
| 1902-12-30
 +
| Old Well
 +
|-
 +
| 2017-06-29
 +
| Begin Plugging
 +
|-
 +
| 2017-07-17
 +
| Finished Plugging
 +
|-
 +
| 2019-05-16
 +
| Fully Plugged
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Compiled from multiple data sources - see Pennsylvania Oil and Gas Data Sources
 +
| date = 2020-02-27
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
 +
| accessdate = 2020-02-27 }}</ref>
 
<!--== Fracking Activities ==
 
<!--== Fracking Activities ==
 
==== Fracking Jobs ====
 
==== Fracking Jobs ====
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!scope="col" | Job Percentage by Mass
 
!scope="col" | Job Percentage by Mass
 
!scope="col" | Mass Used (lb)
 
!scope="col" | Mass Used (lb)
 +
|-
 +
|}-->
 +
 +
<!--== Stimulation Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | Stimulation Date
 +
!scope="col" | Phase Number
 +
!scope="col" | Chemical Agent
 +
!scope="col" | Volume (gal)
 +
!scope="col" | Treating Pressure (psi)
 +
!scope="col" | Breakdown Pressure (psi)
 
|-
 
|-
 
|}-->
 
|}-->
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!scope="col" | Water Quantity (bbl)
 
!scope="col" | Water Quantity (bbl)
 
!scope="col" | Water Production Days
 
!scope="col" | Water Production Days
 +
|-
 +
| 1991
 +
| [[COLUMBIA NATURAL RES INC]]
 +
| style="text-align: right;" | 34.00
 +
| style="text-align: right;" | 21
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0.00
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
| 1996
 
| 1996
 
| [[CASTLE GAS CO INC]]
 
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 427.00
+
| style="text-align: right;" | 427
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 1997
 
| 1997
 
| [[CASTLE GAS CO INC]]
 
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 245.00
+
| style="text-align: right;" | 245
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 1998
 
| 1998
 
| [[CASTLE GAS CO INC]]
 
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 235.00
+
| style="text-align: right;" | 235
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 1999
 
| 1999
 
| [[CASTLE GAS CO INC]]
 
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 217.00
+
| style="text-align: right;" | 217
 
| style="text-align: right;" | 348
 
| style="text-align: right;" | 348
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2000
 
| 2000
 
| [[CASTLE GAS CO INC]]
 
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 268.00
+
| style="text-align: right;" | 268
 
| style="text-align: right;" | 351
 
| style="text-align: right;" | 351
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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|-
 
|-
 
| 2001
 
| 2001
| [[VIKING RESOURCES CORP]]
+
| [[CASTLE GAS CO INC]]
| style="text-align: right;" | 51.00
+
| style="text-align: right;" | 239
| style="text-align: right;" | 365
+
| style="text-align: right;" | 304
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0
 
| style="text-align: right;" | 0
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| 2002
 
| 2002
 
| [[VIKING RESOURCES CORP]]
 
| [[VIKING RESOURCES CORP]]
| style="text-align: right;" | 346.00
+
| style="text-align: right;" | 346
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2003
 
| 2003
 
| [[VIKING RESOURCES CORP]]
 
| [[VIKING RESOURCES CORP]]
| style="text-align: right;" | 316.00
+
| style="text-align: right;" | 316
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2004
 
| 2004
 
| [[VIKING RESOURCES CORP]]
 
| [[VIKING RESOURCES CORP]]
| style="text-align: right;" | 275.00
+
| style="text-align: right;" | 275
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2005
 
| 2005
 
| [[VIKING RESOURCES CORP]]
 
| [[VIKING RESOURCES CORP]]
| style="text-align: right;" | 22.00
+
| style="text-align: right;" | 22
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 365
 
| style="text-align: right;" | 0.00
 
| style="text-align: right;" | 0.00
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| 2017
 
| 2017
 
| [[CHEVRON APPALACHIA LLC]]
 
| [[CHEVRON APPALACHIA LLC]]
| Synthetic Liner Materials (in Tons) RWC 806
+
| Synthetic Liner Materials
 
| style="text-align: right;" | 4.43 Tons
 
| style="text-align: right;" | 4.43 Tons
 
| LANDFILL
 
| LANDFILL
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| 2017
 
| 2017
 
| [[CHEVRON APPALACHIA LLC]]
 
| [[CHEVRON APPALACHIA LLC]]
| Drilling Fluid Waste (in Barrels) RWC 803
+
| Drilling Fluid Waste
 
| style="text-align: right;" | 38.30 Bbl
 
| style="text-align: right;" | 38.30 Bbl
 
| LANDFILL
 
| LANDFILL

Latest revision as of 10:19, 2 June 2020

Well Details

Well ID: 37-129-00667
Loading map...
Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Sewickley Township
Operator Name: CHEVRON APPALACHIA LLC
Well Pad ID:
Farm/Lease Name: D M CURRY
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.234786
Longitude: -79.787361

For data sources see[1][2][3]

Well History

Date Event
1902-08-27 Drilling Completion
1902-12-30 Old Well
2017-06-29 Begin Plugging
2017-07-17 Finished Plugging
2019-05-16 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 COLUMBIA NATURAL RES INC 34.00 21 0.00 0 0.00 0
1996 CASTLE GAS CO INC 427 365 0.00 0 0.00 0
1997 CASTLE GAS CO INC 245 365 0.00 0 0.00 0
1998 CASTLE GAS CO INC 235 365 0.00 0 0.00 0
1999 CASTLE GAS CO INC 217 348 0.00 0 0.00 0
2000 CASTLE GAS CO INC 268 351 0.00 0 0.00 0
2001 CASTLE GAS CO INC 239 304 0.00 0 0.00 0
2002 VIKING RESOURCES CORP 346 365 0.00 0 0.00 0
2003 VIKING RESOURCES CORP 316 365 0.00 0 0.00 0
2004 VIKING RESOURCES CORP 275 365 0.00 0 0.00 0
2005 VIKING RESOURCES CORP 22 365 0.00 0 0.00 0
2006 VIKING RESOURCES CORP 0.00 0 0.00 0 0.00 0
2007 VIKING RESOURCES CORP 0.00 0 0.00 0 0.00 0
2008 VIKING RESOURCES LLC 0.00 0 0.00 0 0.00 0
2009 VIKING RESOURCES LLC 0.00 0 0.00 0 0.00 0
2010 VIKING RESOURCES LLC 0.00 0 0.00 0 0.00 0
2011 VIKING RESOURCES LLC 0.00 0 0.00 0 0.00 0
2012 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2013 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2014 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2015 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2016 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0
2017 CHEVRON APPALACHIA LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2017 CHEVRON APPALACHIA LLC Synthetic Liner Materials 4.43 Tons LANDFILL 100172
2017 CHEVRON APPALACHIA LLC Drilling Fluid Waste 38.30 Bbl LANDFILL 100663

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2539651 Primary Facility 2016-11-29 Complaint Inspection No Violations Noted At the time of inspection the well appeared to be drilled and equipped for production. The well apparatus appeared to be in sound condition. The well tag was present. No observation of accelerated erosion or sedimentation.
2613470 Primary Facility 2017-07-10 Routine/Complete Inspection No Violations Noted At the time of inspection the Operator was actively plugging the well. The coil tubing rig was on site and placed on secondary containment. No observation of accelerated erosion or sedimentation in relation to the well pad or access road.
2615760 Primary Facility 2017-07-17 Incident- Response to Accident or Event Violation(s) Noted Response to spill reported to the Department on 7/16/2017 at 8pm. The Operator indicated that approximately 10 barrels of concrete was lost under the secondary containment at 6pm. The Operator indicated that they were pumping concrete into the production casing and lost circulation. The Operator observed concrete on the edge of the well pad. Plugging activity was stopped. The Operators inspection revealed concrete was returning to the surface via the annular casing under secondary containment. The well permit was on site. ERP onsite. The PPC plan was on site. SDS on site. E& S plan was on site. Operator representatives onsite during inspection B.A Lambie, Ronnie Venghaus and Mark Manning. The Departments inspection confirmed that concrete was last lost to the well pad and appeared to be under the containment. Waters of the Commonwealth were not impacted. The cement solidified prior to leaving the perimeter controls. The Department observed two open top tanks. One of the tanks had less than 2 feet of freeboa
2616547 Primary Facility 2017-07-19 Follow-up Inspection In Compliance with Schedule Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator removed the secondary containment in the area of the release. The impacted area appeared to be remediated, the concrete removed was placed on containment awaiting disposal. The Operator indicated that confirmation samples were collected. The attached photo contains flags indicating the confirmation sample locations. The open top tanks located on site had more than 2 feet of freeboard.
2625428 Primary Facility 2017-08-14 Follow-up Inspection In Compliance with Schedule Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. Secondary containment removed and placed in two open top roll off boxes. The contents of an additional three roll off boxes also located on site could not be verified. Well plugged. The berm located on two sides of the well site appeared to have small erosion rills but no evidence that suggests the sedimentation is leaving the location or impacting waters of the Commonwealth. The Department recommends the Operator continue to monitor the site weekly and after significant precipitation events.
2635228 Primary Facility 2017-09-11 Follow-up Inspection In Compliance with Schedule Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. The site appears to be unchanged since 8/14/2017 follow up inspection. Well plugged. Roll off boxes with containment on site. Temporary erosion and sedimentation BMPs in place and functioning. The Department recommends the Operator continue to monitor the site weekly and after significant precipitation events.
2642481 Primary Facility 2017-10-02 Follow-up Inspection In Compliance with Schedule Follow up inspection to violations issued in relation to a release reported on 7/17/2017. The Operator was not actively working on the site during the inspection. The Operator has removed four open top roll off boxes from the well site. One new roll off boxes has been delivered to the site and one closed, residual waste box remains on site. Well plugged. Temporary erosion and sedimentation BMPs in place and functioning. The Department recommends the Operator continue to monitor the site.
2654643 Primary Facility 2017-10-31 Administrative/File Review In Compliance with Schedule Administrative inspection. On 10/31/2017 the Department received the Operators Site Characterization and soil excavation report associated with the release of cement which occurred on7/16/2017.
2667578 Primary Facility 2017-12-05 Compliance Evaluation No Violations Noted Well plugged. No monument observed. Site regraded, seeded and mulched. Temporary E&S BMP site sox appears to be installed and functions as designed. The Department recommends that the Operator continue to monitor the site until the site is returned to previous use or 70% uniform vegetative coverage is established. The Violation associated with inspection report 2615760, relating to the release of cement, have been corrected and the Operator has complied with the Departments spill policy.
758513 Primary Facility 1991-01-24 Routine/Complete Inspection No Violations Noted E&S OK; NO TANK

Violations Commited

Inspection ID Violation ID Violation Date Date Resolved Violation Code Violation Type Violation Comments
2615760 791904 2017-07-17 2017-12-05 78.57(a) Environmental Health & Safety Operator failed to control.
2615760 791905 2017-07-17 2017-12-05 78.56(a)2 Environmental Health & Safety Operator failed to maintain 2 feet of freeboard.

Penalties Applied

Violation ID Penalty ID Penalty Code Penalty Status Penalty Date Enforcement Date Penalty Amount Amount Collected
791904 356552 NOV - Notice of Violation 2017-12-05
791905 356552 NOV - Notice of Violation 2017-12-05

For data sources see[7]

References