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Well ID: 34-007-22666 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: VIKING RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: HUEY UNIT | |
License Status: Not Drilled | |
License Date: 1984-03-15 | |
Spud Date: 1984-06-16 | |
Spud Drilling Contractor: | |
Final Drill Date: 1984-06-19 | |
Well Total Depth: 2919.00 ft | |
Configuration: Vertical | |
Latitude: 41.900000 | |
Longitude: -80.700000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1984-03-15 | 198 VIKING RESOURCES CORP GeoDate 3/15/84 |
Oil and Gas | 1984-03-15 | Issued Date 3/15/84 Expired Date 9/11/84 Acres 0020000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1984-06-16 | |
Completed | 1984-06-19 | |
Reached Total Depth | 1984-06-19 | |
Construction Permit Expires | 1984-09-11 | |
Record Last Modified | 2009-12-11 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2759 | 2839 | 14 |
2759 | 2839 | 14 | |
2759 | 2839 | 14 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1352 Bbl | 50000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2133058445 | 2015-8-26 0:00: | PW | No Violations | |
1440610170 | 2015-08-24 | Production Wells | No Violations | I was on location at the request of the well company. The 4.5 production casing has rusted through just above the 8 5/8 surface casing. There is a tubing packer set at an unknown depth in the well. The company has hired Autumn Ridge to bring in their service rig and perform the work. The company plans to repair the 4.5 and replace the wellhead with a new one. I will check back on 8/26/15 to see if the work has been completed. |
2133058445 | 2015-08-26 | Production Wells | No Violations | My inspection found the 4.5 production casing has been repaired and the company has installed a new wellhead. Circle M is on location repairing the domestic gas supply that is plumbed into the well. The company is going to replace the existing flow line with a new 2 coated steel flow line before turning the well back on. |
For data sources see[5]