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Well ID: 34-013-20587 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Pultney Township | |
Operator Name: EQUITY OIL & GAS FUNDS INC | |
Well Pad ID: | |
Farm/Lease Name: GIFFIN D | |
License Status: Final Restoration | |
License Date: 2007-01-12 | |
Spud Date: 2007-02-01 | |
Spud Drilling Contractor: WARREN DRLG | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.030000 | |
Longitude: -80.770000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2007-01-12 | Proposed Formations:BEREA THRU ORISKANY, Issued Date:1/12/2007, Expired Date:1/12/2008 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:EDPW |
Construction Permit Expires | 2008-01-12 | |
Record Last Modified | 2018-11-06 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1559403113 | 2007-2-4 0:00:0 | DD | No Violations | |
-46964772 | 2007-2-6 0:00:0 | DD | No Violations | |
-765468845 | 2007-2-21 0:00: | PW | No Violations | |
-992656808 | 2011-2-9 0:00:0 | FR | No Violations | 0.50 |
0046964772 | 2007-02-06 | Drill / Deepen / Reopen | No Violations | 7 PILLS OF MUD CIRCULATED. NO RETURNS TO SURFACE. RAN DOWNHOLE CAMERA.FLUID LEVEL AT 495 SAW SEVERAL PLACES WHERE WATER WAS COMING IN HOLE AT 366 AND AT 402. DECIDED TO REAM HOLE WITH 17.75 BIT TO 615 AND RUN 11.75 CONDUCTOR AND CEMENT IN HOLE. STARTING TO REAM HOLE. |
0409395899 | 2007-02-01 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. DRILLING SURFACE HOLE AT 300 |
0765468845 | 2007-02-21 | Production Wells | No Violations | PIT MTD CLOSED LOCATION ROUGHED IN. TO FRAC WELL NEXT MONTH OR SOONER. |
0992656808 | 2011-02-09 | Final Restoration | No Violations | On day of inspection well was plugged due to lost surface hole per conversation withJohn Murphy. Mike Kavage let them use a cement mixer and grout off.Vegetation back 100%.Final Restoration passed. |
1170289852 | 2007-01-31 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. MOVE ON RIG UP |
1170940673 | 2007-02-08 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. REAMING HOLE WITH 14.75 BIT. STARTE TO RUN 11.75 PIPE 4 JOINTS IN RIG CONTROL BANK MALFUNCTIONED. FLEXED HOURS AT HOUSE FROM 3-8 P.M. FINISHED RUNNING 11.75 IN HOLE. UNIVERSAL CEMENT 525SX.IN HOLE BASKET SET AT 125. BALANCED PLUG ON BOTTOM 380 |
1559403113 | 2007-02-04 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING. STILL MIXING MUD AND PUMPING DOWNHOLE. NO CIRCULATION YET. 700BBLS. PUMPED AWAY DOWNHOLE.SHOULD HAVE HAD CIRCULATION AT 270 BBLS. |
1700824460 | 2007-02-05 | Drill / Deepen / Reopen | No Violations | WARREN DRILLING.STILL MIXING MUD AND PUMPING DOWNHOLE. FLUID LEVEL AT 360 |
409395899 | 2007-2-1 0:00:0 | DD | No Violations |
For data sources see[3]