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Well ID: 34-013-21321 | Loading map...
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Country: United States | |
State: Ohio | |
County: Belmont | |
Municipality: Mead Township | |
Operator Name: XTO ENERGY INC. | |
Well Pad ID: US-OH-001341 | |
Farm/Lease Name: KRNYAICH UNIT B | |
License Status: Cancelled | |
License Date: 2018-01-11 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Horizontal | |
Latitude: 39.960000 | |
Longitude: -80.840000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2018-01-11 | Proposed Formations:POINT PLEASANT, Issued Date:1/11/2018, Expired Date:1/11/2020 12:00:00 PM, Drilling unit acres:638.828, Proposed Well Type:OG, Proposed Well Class:POOL |
Record Last Modified | 2018-09-12 | |
Construction Permit Expires | 2020-01-11 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1438730513 | 2018-8-7 0:00:0 | DD | No Violations | 0.20 |
-417370625 | 2018-8-15 0:00: | DD | No Violations | 0.50 |
-821273161 | 2018-8-23 0:00: | DD | No Violations | 1.00 |
0417370625 | 2018-08-15 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed that the 30- |
0821273161 | 2018-08-23 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I witnessed that Appalachian Drilling was currently conditioning the well bore at 532 feet depth. After speaking with company man Steve Guile, he informed me that they encountered a mine void from 470 feet to 476 feet depth and had to switch from a 24-inch diameter percussion bit to a 24-inch diameter Tri-Cone bit. Steve also informed me that they intend on running 542 feet of 87.5 pound per foot J-55 casing with a cement basket at 441 feet depth and cement to surface. I informed Steve that he needed to send me a cement report, and pipe tally and upon completion of pumping cement they are required to wait until cement reaches a compressive strength of 500 pounds per square inch before any further action can be taken. |
1438730513 | 2018-08-07 | Drill / Deepen / Reopen | No Violations |
For data sources see[3]