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34-031-22657

Well Details

Well ID: 34-031-22657
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Country: United States
State: Ohio
County: Coshocton
Municipality: Tiverton Township
Operator Name: ELKHEAD GAS & OIL CO
Well Pad ID:
Farm/Lease Name: VALES
License Status: Final Restoration
License Date: 2013-08-05
Spud Date: 1975-09-23
Spud Drilling Contractor:
Final Drill Date: 1975-10-24
Well Total Depth: 3395.00 ft
Configuration: Vertical
Latitude: 40.410000
Longitude: -82.120000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1975-09-17 125 ELKHEAD GAS & OIL CO GeoDate 9/17/75
Original Spud 1975-09-23 FDT=RED ROCK
Completed 1975-10-24 FDT=RED ROCK
Reached Total Depth 1975-10-24 FDT=RED ROCK
APP 2007-05-07 Proposed Formations:CLINTON, Issued Date:5/7/2007, Expired Date:5/6/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2013-08-05 Proposed Formations:CLINTON, Issued Date:8/5/2013, Expired Date:8/5/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-09-23 FDT=RED ROCK
Record Last Modified 2014-07-10 FDT=RED ROCK
Construction Permit Expires 2015-08-05 FDT=RED ROCK

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1200 Bbl 19500

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ELKHEAD GAS & OIL CO 0.00 290.00 0
1985 ELKHEAD GAS & OIL CO 232.00 288.00 343
1986 ELKHEAD GAS & OIL CO 161.00 146.00 307
1987 ELKHEAD GAS & OIL CO 27.00 117.00 293
1988 ELKHEAD GAS & OIL CO 35.00 62.00 182
1989 ELKHEAD GAS & OIL CO 30.00 68.00 73
1990 ELKHEAD GAS & OIL CO 0.00 125.00 323
1992 ELKHEAD GAS & OIL CO 0.00 66.00 46
1993 ELKHEAD GAS & OIL CO 0.00 0.00 150
1994 ELKHEAD GAS & OIL CO 0.00 36.00 350
1995 ELKHEAD GAS & OIL CO 0.00 35.00 350
1996 ELKHEAD GAS & OIL CO 0.00 32.00 350
1997 ELKHEAD GAS & OIL CO 0.00 0.00 365
1998 ELKHEAD GAS & OIL CO 0.00 72.00 365
1999 ELKHEAD GAS & OIL CO 0.00 0.00 365
2000 ELKHEAD GAS & OIL CO 0.00 60.00 365
2001 ELKHEAD GAS & OIL CO 0.00 0.00 365
2002 ELKHEAD GAS & OIL CO 0.00 63.00 365
2003 ELKHEAD GAS & OIL CO 0.00 0.00 365
2004 ELKHEAD GAS & OIL CO 0.00 60.00 365
2005 ELKHEAD GAS & OIL CO 0.00 0.00 365
2006 ELKHEAD GAS & OIL CO 0.00 0.00 365
2007 ELKHEAD GAS & OIL CO 0.00 72.00 365
2008 ELKHEAD GAS & OIL CO 0.00 0.00 365
2009 ELKHEAD GAS & OIL CO 0.00 0.00 365
2010 ELKHEAD GAS & OIL CO 0.00 0.00 365
2011 ELKHEAD GAS & OIL CO 0.00 44.00 365
2012 ELKHEAD GAS & OIL CO 0.00 93.00 366

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ELKHEAD GAS & OIL CO Brine 0 0
1985 ELKHEAD GAS & OIL CO Brine 17 343
1986 ELKHEAD GAS & OIL CO Brine 45 307
1987 ELKHEAD GAS & OIL CO Brine 5 293
1988 ELKHEAD GAS & OIL CO Brine 35 182
1989 ELKHEAD GAS & OIL CO Brine 130 73
1990 ELKHEAD GAS & OIL CO Brine 580 323
1992 ELKHEAD GAS & OIL CO Brine 100 46
1993 ELKHEAD GAS & OIL CO Brine 70 150
1994 ELKHEAD GAS & OIL CO Brine 77 350
1995 ELKHEAD GAS & OIL CO Brine 20 350
1996 ELKHEAD GAS & OIL CO Brine 17 350
1997 ELKHEAD GAS & OIL CO Brine 10 365
1998 ELKHEAD GAS & OIL CO Brine 0 365
1999 ELKHEAD GAS & OIL CO Brine 0 365
2000 ELKHEAD GAS & OIL CO Brine 0 365
2001 ELKHEAD GAS & OIL CO Brine 0 365
2002 ELKHEAD GAS & OIL CO Brine 70 365
2003 ELKHEAD GAS & OIL CO Brine 55 365
2004 ELKHEAD GAS & OIL CO Brine 0 365
2005 ELKHEAD GAS & OIL CO Brine 0 365
2006 ELKHEAD GAS & OIL CO Brine 0 365
2007 ELKHEAD GAS & OIL CO Brine 70 365
2008 ELKHEAD GAS & OIL CO Brine 0 365
2009 ELKHEAD GAS & OIL CO Brine 40 365
2010 ELKHEAD GAS & OIL CO Brine 0 365
2011 ELKHEAD GAS & OIL CO Brine 120 365
2012 ELKHEAD GAS & OIL CO Brine 200 366

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1074871207 2014-6-17 0:00: FR No Violations
-1344547193 2013-9-17 0:00: PB No Violations
-367810726 2013-9-10 0:00: PB No Violations
-474162163 2013-9-18 0:00: PB No Violations
-596001657 2013-9-13 0:00: PB No Violations
-888413978 2007-5-22 0:00: PB No Violations
0224609246 2013-08-29 Production Wells No Violations I received a phone call from Mike Chapman of Elkhead Gas & Oil Co on 8/28/13 claiming that they wanted to plug this well, but the landowner was blocking their access. On the day of my inspection I met Mr. Daryl Zimmerman at the property. He took me back to the well and stated that he also wanted it plugged. Mr. Zimmerman agreed to let Elkhead on the property to plug the well. I contacted Mr. Chapman to let him know that they should be able to get in there without having to get a restraining order.
0367810726 2013-09-10 Plug / Plug Back No Violations On the day of my inspection Randy Moran was moving in with a 100 barrel tank and excavating equipment.
0474162163 2013-09-18 Plug / Plug Back No Violations On the day of my inspection Randy Moran was having trouble pulling the 5.5 casing. They loaded the casing with fresh water, which enabled them to pull it. They pulled 45 joints and washed 8 tons of clay into the well.
0596001657 2013-09-13 Plug / Plug Back No Violations On the day of my inspection Randy Moran pulled the remaining tubing, removed the well head and washed 2 tons of clay down the 5.5 casing.
0888413978 2007-05-22 Plug / Plug Back No Violations Rig at site to plug well . Randy Moran of Moran well service .
1074871207 2014-06-17 Final Restoration No Violations FOLLOW UP TO CA #1397575985. This inspection correlates with complaint #4574. On the day of my inspection I found that the site exhibited approximately 80% coverage with established short grasses. I found no signs of erosion. The former lease road is currently in use to access agricultural fields. This site passes final restoration.
1178723030 2007-05-09 Production Wells No Violations Well equipped for production . 2-100 bl. Storage tanks
1291548013 2013-09-11 Plug / Plug Back No Violations On the day of my inspection Randy Moran removed the pumping unit, and pulled the rods and tubing. I met with Mike Chapman of Elkhead Gas & Oil and the landowner, Daryl Zimmerman to discuss the plugging the well.
1344547193 2013-09-17 Plug / Plug Back No Violations On the day of my inspection Randy Moran ripped the 5.5 casing at 2770. They had to make rig repairs before attempting to pull the casing.
1372092773 2014-05-28 Final Restoration No Violations FOLLOW UP TO CA #1397575985: On the day of my inspection I found that all requirements of the final restoration were completed except erosion control through adequate grass coverage. The disturbed areas were only starting to grow grass. They will need better coverage for this violation to be resolved.
1379000518 2013-09-12 Plug / Plug Back No Violations On the day of my inspection Randy Moran was pulling the tubing from the well.
1379617735 2013-09-19 Plug / Plug Back No Violations On the day of my inspection Randy Moran finished pulling the 5.5 casing from the well.
1379689061 2013-09-20 Plug / Plug Back No Violations On the day of my inspection Randy Moran set a pre-cast cement plug at 998 and washed 4 tons of clay down the 8.625 casing to plug across the Berea. They pulled all of the 8.625 casing, set a pre-cast cement plug at 478 and washed 4 tons of clay into the well. It will be allowed to settle over the weekend.
1379958073 2013-09-23 Plug / Plug Back No Violations On the day of my inspection Randy Moran washed another 4 tons of clay into the well to fill it to surface.
1389376584 2014-01-10 Final Restoration No Violations I received a complaint by mail from Daryl Zimmerman that the restoration was not complete at this plug well site. The final restoration is not due till 3/23/14. I contacted Mr. Zimmerman to expalin that the well owner has 6 months from the plug date to complete the restoration. In his letter he also expressed concern over the ownership of the oil in the storage tank. I explained that it was a legal matter between him and Elkhead Gas & Oil Co.
1397575985 2014-04-15 Final Restoration Violations Noted This inspection correlates with complaint #4574. On the day of my inspection I found that nothing has been done to complete this final restoration. The landowner, Daryl Zimmerman, has expressed that he wants the flow line removed. The flow line has not been removed at this time. The tank battery has not been removed at this time and the well site still needs to be graded and seeded. The restoration was due on 3/23/14. I spoke with Mike Chapman of Elkhead Gas & Oil Co. who claimed that they received a letter from Mr. Zimmermans attorney prohibiting them from entering the property. I met with Mr. Zimmerman and established that Elkhead is required to enter the property and complete the restoration before the planting season. Mr. Zimmerman agreed to Memorial Day as a deadline.
1399305403 2014-05-05 Final Restoration No Violations FOLLOW UP TO CA #1397575985: This inspection pertains to complaint #4574. On the day of my inspection I found that the flow line had been removed from the well site to the tank battery site. The production equipment had been removed. The soil at the well site and tank battery site had been graded out to the approximate original contour, seeded with grass seed and covered with straw. I met the landowner, Mr. Daryl Zimmerman. He claimed to be satisfied with the work that was done.
1761395590 2014-04-24 Final Restoration No Violations FOLLOW UP TO CA #1397575985: This inspection pertains to complaint #4574. On the day of my inspection Elkhead removed the remaining flow line. They also had the oil removed from the tank. I met with Mr. Zimmerman to clarify that he wants Elkhead to grade and seed the well site and tank battery site. Elkhead is to grade the access road but no seeding will be required.
1967302951 2014-04-23 Final Restoration No Violations FOLLOW UP TO CA #1397575985: This inspection pertains to complaint #4574. Mike Chapman requested that I be present during the restoration work, as there has been a history of hostilities between the landowner and Elkhead. They removed the flow line and graded the disturbed soil back out to the approximate original contour.
224609246 2013-8-29 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1397575985 US-OH-111754 2014-06-30 Failure to complete final restoration within six months

For data sources see[8]

References