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34-075-24357

Well Details

Well ID: 34-075-24357
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Country: United States
State: Ohio
County: Holmes
Municipality: Washington Township
Operator Name: CHRYSTAL ENERGY INC
Well Pad ID:
Farm/Lease Name: NESTA
License Status: Producing
License Date: 1984-07-06
Spud Date: 1984-08-12
Spud Drilling Contractor: CHRYSTAL ENERGY
Final Drill Date: 1984-08-17
Well Total Depth: 642.00 ft
Configuration: Vertical
Latitude: 40.640000
Longitude: -82.170000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-07-06 1846 CHRYSTAL ENERGY INC GeoDate 7/6/84
Oil and Gas 1984-07-06 Issued Date 7/6/84 Expired Date 1/2/85 Acres 0001000 Tool Type RTAF Proposed Formation BEREA Proposed Depth 00642 Proposed Drill Depth 00642
Original Spud 1984-08-12 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.
Completed 1984-08-17 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.
Reached Total Depth 1984-08-17 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.
Completion Report Received 1984-11-14 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.
Construction Permit Expires 1985-01-02 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.
Record Last Modified 2017-02-15 FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 10/6/03.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 535 642 0
535 642 0
2006-09-11 550 610 0
550 610 0
535 642 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
NITR 0 1 Qts 0 SHOT: 1 QT NITRO PER FOOT

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1978433694 2003-10-7 0:00: PW No Violations
000PL15356 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1155196982 2012-09-17 Production Wells Violations Noted This is a pump jack well. There is no prime mover. The well is shut in. There has been no reported production from this well for years. There is no ID on the well. There was no tank found. The well shall be plugged, produced or sold. In the interim affix a valid legible ID to the well which includes the well owner name, the well name, the permit number, county, and emergency phone number. Failure to comply with this request may result in forfeiture of bond.
1978433694 2003-10-07 Production Wells Violations Noted Check well for columbus ( sherry young )
PL15356 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1155196982 US-OH-104076 2012-09-18 Failure to legibly identify well
1155196982 US-OH-104077 2012-09-18 Nonproduction; well shall be plugged or placed in temporary inactive status
1978433694 US-OH-120009 2004-05-04 Failure to legibly identify well
1978433694 US-OH-120010 2004-05-04 Well shall be plugged

For data sources see[5]

References