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34-075-60946

Well Details

Well ID: 34-075-60946
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Country: United States
State: Ohio
County: Holmes
Municipality: Paint Township
Operator Name: KENOIL LLC
Well Pad ID:
Farm/Lease Name: MILLER LEVI J (MIZER)
License Status: Final Restoration
License Date: 2014-10-07
Spud Date: 1936-01-13
Spud Drilling Contractor:
Final Drill Date: 1936-04-30
Well Total Depth: 4130.00 ft
Configuration: Vertical
Latitude: 40.660000
Longitude: -81.670000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1936-01-13 QUADRANGLE=NAVARRE, GL=1040.7
Completed 1936-04-30 QUADRANGLE=NAVARRE, GL=1040.7
Reached Total Depth 1936-04-30 QUADRANGLE=NAVARRE, GL=1040.7
CO 1984-09-19 185 HILL WILLIAM F GeoDate
CO 1984-09-19 22 COLUMBIA GAS TRANSMISSION
CO 1993-09-28 2772 HILL DRILLING INC GeoDate
CO 1995-04-12 627 KENOIL GeoDate
APP 2014-10-07 Proposed Formations:CLINTON, Issued Date:10/7/2014, Expired Date:10/6/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2014-11-24 QUADRANGLE=NAVARRE, GL=1040.7
Construction Permit Expires 2016-10-06 QUADRANGLE=NAVARRE, GL=1040.7
Record Last Modified 2017-02-10 QUADRANGLE=NAVARRE, GL=1040.7

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 40 Qts 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1995 KENOIL LLC 906.00 0.00 0
1996 KENOIL LLC 1744.00 0.00 0
1997 KENOIL LLC 1350.00 0.00 365
1998 KENOIL LLC 1711.00 0.00 365
1999 KENOIL LLC 1280.00 14.00 0
2000 KENOIL LLC 1602.00 0.00 365
2001 KENOIL LLC 1431.00 0.00 365
2002 KENOIL LLC 1312.00 0.00 365
2003 KENOIL LLC 1389.00 0.00 365
2004 KENOIL LLC 1141.00 0.00 365
2005 KENOIL LLC 1196.00 0.00 365
2006 KENOIL LLC 980.00 0.00 365
2007 KENOIL LLC 803.00 19.00 365
2008 KENOIL LLC 999.00 0.00 365
2009 KENOIL LLC 1023.00 0.00 365
2010 KENOIL LLC 871.00 0.00 365
2011 KENOIL LLC 740.00 0.00 0
2012 KENOIL LLC 387.00 0.00 366
2014 KENOIL LLC 79.00 13.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1995 KENOIL LLC Brine 0 0
1996 KENOIL LLC Brine 0 0
1997 KENOIL LLC Brine 0 365
1998 KENOIL LLC Brine 0 365
1999 KENOIL LLC Brine 0
2000 KENOIL LLC Brine 365
2001 KENOIL LLC Brine 0 365
2002 KENOIL LLC Brine 0 365
2003 KENOIL LLC Brine 0 365
2004 KENOIL LLC Brine 0 365
2005 KENOIL LLC Brine 0 365
2006 KENOIL LLC Brine 0 365
2007 KENOIL LLC Brine 10 365
2008 KENOIL LLC Brine 0 365
2009 KENOIL LLC Brine 0 365
2010 KENOIL LLC Brine 0 365
2011 KENOIL LLC Brine 0
2012 KENOIL LLC Brine 15 366
2014 KENOIL LLC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1482914376 2014-11-13 0:00 PB No Violations
-1660544381 2014-11-6 0:00: PB No Violations
-1826028201 2014-11-12 0:00 PB No Violations
-925815838 2014-11-8 0:00: PB No Violations
0029019275 2014-11-19 Plug / Plug Back No Violations The 5-1/2 casing has been ripped at 2325. They pulled 10 joints and then washed in 1 ton of clay. The balance of the casing is being pulled.
0365022286 2014-11-18 Plug / Plug Back No Violations The plugging conteractor is ripping on the 5-1/2 casing.
0466743810 2014-11-24 Plug / Plug Back No Violations The 8 was pulled from the hole and the rig crew washed in 18 tons of fireclay from 980 to the surface. The plug stayed up. See the plugging report for the details.
0542567604 2014-11-21 Plug / Plug Back No Violations Set a brush and stone bridge plug at 980. Ripping on 8 at 910.
0578187907 2014-02-06 Production Wells No Violations This is a producing pump jack well. There were no problems noted at the time of the inspection.
0925815838 2014-11-08 Plug / Plug Back No Violations Attemped to release the 3-1/2packer after having it set all night with the string weight off of it. It failed to come loose and it was decided to shoot it off. Washed in 200 feet of clay to shut off the formation inside the 3-1/2 and will shoot of the packer on Monday Noon.
1229581900 2011-01-03 Final Restoration No Violations Final restoration approved.
1482914376 2014-11-13 Plug / Plug Back No Violations The balance of the 3-1/2 tubing was pulled form the well. The head was cut and there is 5-1/2 casing in the well as well as some either 8 or 10. The ripping tools were run in the hole and there was no set down or telegraph below 2350. Will attempt to rip off the casing above 2350.
1660544381 2014-11-06 Plug / Plug Back No Violations Moved the rig on and rigged up. Started pulling 1-1/2 tubing.
1726585184 2014-11-03 Plug / Plug Back No Violations They are moving equipment onto the location in preparation to plug this well. This well is a reentry and has two strings of caing on hookwall packers.
1826028201 2014-11-12 Plug / Plug Back No Violations Petroset cementing Services spotted cement plugs thru tubing in the 3 -1/2 casing. The first, from 3600-3400, is just above the clay already washed in the well . The second from 2775-2375 is across some perfs shot 50 below the base of the Oriskany sand. This was necessary after the 3-1/2 casing parted high after being shot off at 2730 the day before (Veterans Day). See the plugging report for more details.
29019275 2014-11-19 0:00 PB No Violations
365022286 2014-11-18 0:00 PB No Violations
466743810 2014-11-24 0:00 PB No Violations
542567604 2014-11-21 0:00 PB No Violations
578187907 2014-2-6 0:00:0 PW No Violations

For data sources see[8]

References