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Well ID: 34-075-60946 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Paint Township | |
Operator Name: KENOIL LLC | |
Well Pad ID: | |
Farm/Lease Name: MILLER LEVI J (MIZER) | |
License Status: Final Restoration | |
License Date: 2014-10-07 | |
Spud Date: 1936-01-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1936-04-30 | |
Well Total Depth: 4130.00 ft | |
Configuration: Vertical | |
Latitude: 40.660000 | |
Longitude: -81.670000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1936-01-13 | QUADRANGLE=NAVARRE, GL=1040.7 |
Completed | 1936-04-30 | QUADRANGLE=NAVARRE, GL=1040.7 |
Reached Total Depth | 1936-04-30 | QUADRANGLE=NAVARRE, GL=1040.7 |
CO | 1984-09-19 | 185 HILL WILLIAM F GeoDate |
CO | 1984-09-19 | 22 COLUMBIA GAS TRANSMISSION |
CO | 1993-09-28 | 2772 HILL DRILLING INC GeoDate |
CO | 1995-04-12 | 627 KENOIL GeoDate |
APP | 2014-10-07 | Proposed Formations:CLINTON, Issued Date:10/7/2014, Expired Date:10/6/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-11-24 | QUADRANGLE=NAVARRE, GL=1040.7 |
Construction Permit Expires | 2016-10-06 | QUADRANGLE=NAVARRE, GL=1040.7 |
Record Last Modified | 2017-02-10 | QUADRANGLE=NAVARRE, GL=1040.7 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 0 | 40 Qts | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | KENOIL LLC | 906.00 | 0.00 | 0 |
1996 | KENOIL LLC | 1744.00 | 0.00 | 0 |
1997 | KENOIL LLC | 1350.00 | 0.00 | 365 |
1998 | KENOIL LLC | 1711.00 | 0.00 | 365 |
1999 | KENOIL LLC | 1280.00 | 14.00 | 0 |
2000 | KENOIL LLC | 1602.00 | 0.00 | 365 |
2001 | KENOIL LLC | 1431.00 | 0.00 | 365 |
2002 | KENOIL LLC | 1312.00 | 0.00 | 365 |
2003 | KENOIL LLC | 1389.00 | 0.00 | 365 |
2004 | KENOIL LLC | 1141.00 | 0.00 | 365 |
2005 | KENOIL LLC | 1196.00 | 0.00 | 365 |
2006 | KENOIL LLC | 980.00 | 0.00 | 365 |
2007 | KENOIL LLC | 803.00 | 19.00 | 365 |
2008 | KENOIL LLC | 999.00 | 0.00 | 365 |
2009 | KENOIL LLC | 1023.00 | 0.00 | 365 |
2010 | KENOIL LLC | 871.00 | 0.00 | 365 |
2011 | KENOIL LLC | 740.00 | 0.00 | 0 |
2012 | KENOIL LLC | 387.00 | 0.00 | 366 |
2014 | KENOIL LLC | 79.00 | 13.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1995 | KENOIL LLC | Brine | 0 | 0 |
1996 | KENOIL LLC | Brine | 0 | 0 |
1997 | KENOIL LLC | Brine | 0 | 365 |
1998 | KENOIL LLC | Brine | 0 | 365 |
1999 | KENOIL LLC | Brine | 0 | |
2000 | KENOIL LLC | Brine | 365 | |
2001 | KENOIL LLC | Brine | 0 | 365 |
2002 | KENOIL LLC | Brine | 0 | 365 |
2003 | KENOIL LLC | Brine | 0 | 365 |
2004 | KENOIL LLC | Brine | 0 | 365 |
2005 | KENOIL LLC | Brine | 0 | 365 |
2006 | KENOIL LLC | Brine | 0 | 365 |
2007 | KENOIL LLC | Brine | 10 | 365 |
2008 | KENOIL LLC | Brine | 0 | 365 |
2009 | KENOIL LLC | Brine | 0 | 365 |
2010 | KENOIL LLC | Brine | 0 | 365 |
2011 | KENOIL LLC | Brine | 0 | |
2012 | KENOIL LLC | Brine | 15 | 366 |
2014 | KENOIL LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1482914376 | 2014-11-13 0:00 | PB | No Violations | |
-1660544381 | 2014-11-6 0:00: | PB | No Violations | |
-1826028201 | 2014-11-12 0:00 | PB | No Violations | |
-925815838 | 2014-11-8 0:00: | PB | No Violations | |
0029019275 | 2014-11-19 | Plug / Plug Back | No Violations | The 5-1/2 casing has been ripped at 2325. They pulled 10 joints and then washed in 1 ton of clay. The balance of the casing is being pulled. |
0365022286 | 2014-11-18 | Plug / Plug Back | No Violations | The plugging conteractor is ripping on the 5-1/2 casing. |
0466743810 | 2014-11-24 | Plug / Plug Back | No Violations | The 8 was pulled from the hole and the rig crew washed in 18 tons of fireclay from 980 to the surface. The plug stayed up. See the plugging report for the details. |
0542567604 | 2014-11-21 | Plug / Plug Back | No Violations | Set a brush and stone bridge plug at 980. Ripping on 8 at 910. |
0578187907 | 2014-02-06 | Production Wells | No Violations | This is a producing pump jack well. There were no problems noted at the time of the inspection. |
0925815838 | 2014-11-08 | Plug / Plug Back | No Violations | Attemped to release the 3-1/2packer after having it set all night with the string weight off of it. It failed to come loose and it was decided to shoot it off. Washed in 200 feet of clay to shut off the formation inside the 3-1/2 and will shoot of the packer on Monday Noon. |
1229581900 | 2011-01-03 | Final Restoration | No Violations | Final restoration approved. |
1482914376 | 2014-11-13 | Plug / Plug Back | No Violations | The balance of the 3-1/2 tubing was pulled form the well. The head was cut and there is 5-1/2 casing in the well as well as some either 8 or 10. The ripping tools were run in the hole and there was no set down or telegraph below 2350. Will attempt to rip off the casing above 2350. |
1660544381 | 2014-11-06 | Plug / Plug Back | No Violations | Moved the rig on and rigged up. Started pulling 1-1/2 tubing. |
1726585184 | 2014-11-03 | Plug / Plug Back | No Violations | They are moving equipment onto the location in preparation to plug this well. This well is a reentry and has two strings of caing on hookwall packers. |
1826028201 | 2014-11-12 | Plug / Plug Back | No Violations | Petroset cementing Services spotted cement plugs thru tubing in the 3 -1/2 casing. The first, from 3600-3400, is just above the clay already washed in the well . The second from 2775-2375 is across some perfs shot 50 below the base of the Oriskany sand. This was necessary after the 3-1/2 casing parted high after being shot off at 2730 the day before (Veterans Day). See the plugging report for more details. |
29019275 | 2014-11-19 0:00 | PB | No Violations | |
365022286 | 2014-11-18 0:00 | PB | No Violations | |
466743810 | 2014-11-24 0:00 | PB | No Violations | |
542567604 | 2014-11-21 0:00 | PB | No Violations | |
578187907 | 2014-2-6 0:00:0 | PW | No Violations |
For data sources see[8]