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34-075-61519

Well Details

Well ID: 34-075-61519
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Country: United States
State: Ohio
County: Holmes
Municipality: Washington Township
Operator Name: AM-TEK OIL INC
Well Pad ID:
Farm/Lease Name: FRANK JJ
License Status: Producing
License Date:
Spud Date: 1930-06-07
Spud Drilling Contractor:
Final Drill Date: 1930-08-08
Well Total Depth: 2999.00 ft
Configuration: Vertical
Latitude: 40.610000
Longitude: -82.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1930-06-07 GL=1080.8
Completed 1930-08-08 GL=1080.8
Reached Total Depth 1930-08-08 GL=1080.8
Change of Owner 2005-02-04 Operator changed from 2936, COLUMBIA NATURAL RES INC to 7774, AMERICAN OIL & GAS LLC
Change of Owner 2007-01-25 Operator changed from 7774, AMERICAN OIL & GAS LLC to 8154, AB RESOURCES OH LLC
Change of Owner 2010-09-21 Operator changed from 8154, AB RESOURCES OH LLC to 8685, M & R INVESTMENTS OHIO LLC
Change of Owner 2015-10-14 Operator changed from 8685, M & R INVESTMENTS OHIO LLC to 7859, MALLETT LUKE-DBA MALLET ENERGY
Change of Owner 2017-05-03 Operator changed from 7859, MALLETT LUKE-DBA MALLET ENERGY to 9651, AM-TEK OIL INC
Record Last Modified 2017-05-03 GL=1080.8

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 30 Qts 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 COLUMBIA GAS TRANSMISSION LLC 1383.00 0.00 365
1992 CHESAPEAKE APPALACHIA LLC 879.00 0.00 365
1994 CHESAPEAKE APPALACHIA LLC 779.00 0.00 365
1995 CHESAPEAKE APPALACHIA LLC 775.00 0.00 365
1996 CHESAPEAKE APPALACHIA LLC 754.00 0.00 366
1997 CHESAPEAKE APPALACHIA LLC 589.00 0.00 365
1998 CHESAPEAKE APPALACHIA LLC 625.00 0.00 365
1999 CHESAPEAKE APPALACHIA LLC 707.00 0.00 365
2000 CHESAPEAKE APPALACHIA LLC 774.00 0.00 366
2001 CHESAPEAKE APPALACHIA LLC 673.00 0.00 365
2002 CHESAPEAKE APPALACHIA LLC 700.00 0.00 365
2003 CHESAPEAKE APPALACHIA LLC 478.00 0.00 365
2004 CHESAPEAKE APPALACHIA LLC 183.00 0.00 150
2005 AMERICAN OIL & GAS LLC 0.00 0.00 0
2006 AMERICAN OIL & GAS LLC 0.00 0.00 0
2007 AB RESOURCES OH LLC 0.00 0.00 0
2008 AB RESOURCES OH LLC 0.00 0.00 0
2009 AB RESOURCES OH LLC 0.00 0.00 0
2010 AB RESOURCES OH LLC 0.00 0.00 365
2011 M & R INVESTMENTS OHIO LLC 0.00 0.00 365
2012 M & R INVESTMENTS OHIO LLC 0.00 0.00 366
2013 M & R INVESTMENTS OHIO LLC 0.00 0.00 365
2014 M & R INVESTMENTS OHIO LLC 0.00 0.00 365
2016 MALLETT LUKE-DBA MALLETT ENERG 210.00 0.00 365
2017 AM-TEK OIL INC 351.00 0.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 COLUMBIA GAS TRANSMISSION LLC Brine 0 365
1992 CHESAPEAKE APPALACHIA LLC Brine 20 365
1994 CHESAPEAKE APPALACHIA LLC Brine 0 365
1995 CHESAPEAKE APPALACHIA LLC Brine 0 365
1996 CHESAPEAKE APPALACHIA LLC Brine 0 366
1997 CHESAPEAKE APPALACHIA LLC Brine 0 365
1998 CHESAPEAKE APPALACHIA LLC Brine 1 365
1999 CHESAPEAKE APPALACHIA LLC Brine 1 365
2000 CHESAPEAKE APPALACHIA LLC Brine 0 366
2001 CHESAPEAKE APPALACHIA LLC Brine 60 365
2002 CHESAPEAKE APPALACHIA LLC Brine 0 365
2003 CHESAPEAKE APPALACHIA LLC Brine 0 365
2004 CHESAPEAKE APPALACHIA LLC Brine 0 150
2005 CHESAPEAKE APPALACHIA LLC Brine 0 0
2006 AMERICAN OIL & GAS LLC Brine 0 0
2007 AB RESOURCES OH LLC Brine 0 0
2008 AB RESOURCES OH LLC Brine 0 0
2009 AB RESOURCES OH LLC Brine 0 0
2010 AB RESOURCES OH LLC Brine 0 365
2011 M & R INVESTMENTS OHIO LLC Brine 0 365
2012 M & R INVESTMENTS OHIO LLC Brine 0 366
2013 M & R INVESTMENTS OHIO LLC Brine 0 365
2014 M & R INVESTMENTS OHIO LLC Brine 0 365
2016 MALLETT LUKE-DBA MALLETT ENERG Brine 0 365
2017 AM-TEK OIL INC Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0672683411 2010-02-03 Production Wells No Violations Arrived on location and found violation corrected, Gas leak at wellhead reparied. Case closed
1294321439 2011-01-03 Production Wells Violations Noted Repair wellhead so gas cant escape , Repair pipeline and pressure test, send in production reports, for four years. Call inspestor grimm when repairs are to be made.
1300216679 2011-01-06 Production Wells Violations Noted arrived on location and met with mr frank, he advised well has been leaking gas for 2 years. At wellhead I found a gas leak. Repair casing and all gas leaks at wellhead
1300288001 2011-01-21 Production Wells No Violations Arrived on location and found violation corrected, gas leak repaired.
672683411 2010-2-3 0:00:0 PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1294321439 US-OH-108281 2011-01-06 Inadequate pipeline strength
1294321439 US-OH-108282 2011-01-06 Well insufficiently equipped to prevent escape of oil and gas
1294321439 US-OH-108283 2011-01-06 Statement of annual production not filed
1300216679 US-OH-108441 2011-03-15 Defective casing, leaking well

For data sources see[8]

References