X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-089-21901

Well Details

Well ID: 34-089-21901
Loading map...
Country: United States
State: Ohio
County: Licking
Municipality: Madison Township
Operator Name: R H PENICK CO LTD
Well Pad ID:
Farm/Lease Name: BOYLAN GEORGE E
License Status: Producing
License Date: 1958-04-25
Spud Date: 1958-04-26
Spud Drilling Contractor:
Final Drill Date: 1958-05-25
Well Total Depth: 2095.00 ft
Configuration: Vertical
Latitude: 40.040000
Longitude: -82.370000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Completed 1958-05-25
Reached Total Depth 1958-05-25
Original Spud 1961-11-01
Record Last Modified 2017-02-15

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1999 R H PENICK CO LTD 0.00 193.00 365
2014 R H PENICK CO LTD 0.00 0.00 0
2015 R H PENICK CO LTD 0.00 0.00 0
2016 R H PENICK CO LTD 0.00 0.00 0
2017 R H PENICK CO LTD 0.00 0.00 0
2018 R H PENICK CO LTD 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1999 R H PENICK CO LTD Brine 0 365
2014 R H PENICK CO LTD Brine 0 0
2015 R H PENICK CO LTD Brine 0 0
2016 R H PENICK CO LTD Brine 0 0
2017 R H PENICK CO LTD Brine 0 0
2018 R H PENICK CO LTD Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1467465739 2009-3-19 0:00: PW No Violations
-1527560402 2020-5-15 0:00: PW No Violations 0.50
-19569291 2009-3-19 0:00: PW No Violations
-904156053 2016-5-11 0:00: PW No Violations
0019569291 2009-03-19 Production Wells No Violations FOLLOW UP TO NOV # 1239636552 Jeff Fry and I inspected the well location at the request of John Trujillo. This well is apparently producing brine from the Newberg Formation. However, the sills holding the pumping unit have broken down causing the pumping unit to be incapable of pumping this well. This well is incapable of production and has no display of identification at the well or the tank battery. This permit number was recently assigned to this well by the permitting office in Columbus.
0904156053 2016-05-11 Production Wells No Violations Inspect well as a follow-up. The well is capable of production and identification was posted at the well. Violation resolved. Time of inspection: 2:35 PM. Weather: 68*F, Overcast
0982347722 2009-03-19 Production Wells No Violations FOLLOW UP TO NOV # -1467465739 FOLLOW UP TO NOV # 1239636552 Jeff Fry and I inspected the well location at the request of John Trujillo. This well is apparently producing brine from the Newberg Formation. However, the sills holding the pumping unit have broken down causing the pumping unit to be incapable of pumping this well. This well is incapable of production and has no display of identification at the well or the tank battery. This permit number was recently assigned to this well by the permitting office in Columbus.
1239636552 2009-03-19 Production Wells Violations Noted Jeff Fry and I inspected the well location at the request of John Trujillo. This well is apparently producing brine from the Newberg Formation. However, the sills holding the pumping unit have broken down causing the pumping unit to be incapable of pumping this well. This well is incapable of production and has no display of identification at the well or the tank battery. This permit number was recently assigned to this well by the permitting office in Columbus.
1360994556 2009-05-05 Production Wells No Violations There is proper identification displayed at this well and at the tank battery. This well is not currently in production and is still not capable of production. However, the company has written a letter, dated April 23, 2009, to the Division stating that this well will be put back into production by December of 2009. This request was granted by the Division.
1467465739 2009-03-19 Production Wells No Violations FOLLOW UP TO NOV # 1239636552 Jeff Fry and I inspected the well location at the request of John Trujillo. This well is apparently producing brine from the Newberg Formation. However, the sills holding the pumping unit have broken down causing the pumping unit to be incapable of pumping this well. This well is incapable of production and has no display of identification at the well or the tank battery. This permit number was recently assigned to this well by the permitting office in Columbus.
982347722 2009-3-19 0:00: PW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1239636552 US-OH-106380 2009-04-13 Failure to legibly identify well
1239636552 US-OH-106381 2009-04-13 Well shall be plugged

For data sources see[8]

References