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Well ID: 34-089-26140 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Burlington Township | |
Operator Name: JAMES WRAY INC | |
Well Pad ID: | |
Farm/Lease Name: CUNNINGHAM | |
License Status: Producing | |
License Date: 2013-11-13 | |
Spud Date: 2014-05-12 | |
Spud Drilling Contractor: H & D DRILLING | |
Final Drill Date: 2014-06-14 | |
Well Total Depth: 2289.00 ft | |
Configuration: Vertical | |
Latitude: 40.260000 | |
Longitude: -82.500000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2013-11-13 | Proposed Formations:CLINTON, Issued Date:11/13/2013, Expired Date:11/13/2015 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2014-06-14 | |
Completion Report Received | 2015-07-15 | |
Construction Permit Expires | 2015-11-13 | |
Record Last Modified | 2019-06-11 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2015-07-16 | 2220 | 2240 | 21 |
2220 | 2240 | 21 | |
2220 | 2240 | 21 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2015-05-07 | H2O | 0 | 40888 Gal | 60000 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | JAMES WRAY INC | 728.00 | 0.00 | 156 |
2015 | JAMES WRAY INC | 0.00 | 0.00 | 0 |
2016 | JAMES WRAY INC | 3585.00 | 0.00 | 90 |
2017 | JAMES WRAY INC | 595.00 | 0.00 | 156 |
2018 | JAMES WRAY INC | 2169.00 | 0.00 | 90 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | JAMES WRAY INC | Brine | 0 | 156 |
2015 | JAMES WRAY INC | Brine | 0 | 0 |
2016 | JAMES WRAY INC | Brine | 145 | 90 |
2017 | JAMES WRAY INC | Brine | 0 | 156 |
2018 | JAMES WRAY INC | Brine | 0 | 90 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1040883872 | 2016-2-18 0:00: | PW | No Violations | |
-1539647110 | 2014-6-5 0:00:0 | CS | No Violations | |
-154610546 | 2014-6-4 0:00:0 | DD | No Violations | |
-1652580056 | 2015-5-18 0:00: | PL | No Violations | |
-1653906542 | 2014-6-10 0:00: | DD | No Violations | |
-1661991880 | 2014-6-6 0:00:0 | CS | No Violations | |
-234019531 | 2014-9-29 0:00: | PL | No Violations | |
-604795590 | 2014-5-13 0:00: | DD | No Violations | |
-911658091 | 2014-5-29 0:00: | DD | No Violations | |
0091691116 | 2014-05-07 | Drill / Deepen / Reopen | No Violations | I inspected this location today accompanied by Jeff Fry. H & D Drilling was working on the location and preparing to rig up. No violations. |
0154610546 | 2014-06-04 | Drill / Deepen / Reopen | No Violations | I inspected drilling operations today. H & D Drilling drilling during inspection. No violations. |
0234019531 | 2014-09-29 | Preliminary Restoration | No Violations | This inspection was conducted as a status check. A service rig was over the well. A properly lined pit was next to the well as well as a 100 barrel tank. The well has not been fraced as of this date. No activity during inspection. No violations. |
0356428281 | 2014-05-27 | Drill / Deepen / Reopen | No Violations | Inspect drilling operations. H & D Drilling drilling on fluid during inspection. Depth approximately 200 feet. No violations. |
0604795590 | 2014-05-13 | Drill / Deepen / Reopen | No Violations | I inspected drilling operations today. H & D Drilling was installing 11 drive pipe during inspection. The pit was lined and permit displayed. No violations. |
0911658091 | 2014-05-29 | Drill / Deepen / Reopen | No Violations | Inspect drilling operations. Inspection revealed that the hole has caved in again. H & D Drilling will install drive pipe into the bedrock. No violations. |
1002658828 | 2014-05-21 | Drill / Deepen / Reopen | No Violations | Inspect drilling operations. H & D Drilling installling more drive pipe. The hole caved in at 180 feet again. |
1040883872 | 2016-02-18 | Production Wells | No Violations | Inspect well and storage. Status: ok. |
1418374262 | 2014-06-30 | Preliminary Restoration | No Violations | This inspection was conducted as a status check. The rig has been removed. The pits were being closed during the inspection. No violations. |
1474045959 | 2014-06-16 | Drill / Deepen / Reopen | No Violations | I inspected drilling operations today. The well has been drilled. The production casing was cemented on 6/14/2014. The cement ticket was received during this inspection. H & D Drilling rigging down during inspection. |
1539647110 | 2014-06-05 | Casing String Witnessed | No Violations | I witnessed the cementing of the 8 surface casing for James Wray Inc. H & D Drilling has been contracted to drill the well. Formation Cementing was on location for the cement job. Formation Cementing broke circulation and good cement returns were observed. A cement basket was not used. |
1586782615 | 2020-4-13 0:00: | PW | No Violations | 0.50 |
1652580056 | 2015-05-18 | Preliminary Restoration | No Violations | Inspect well. The well has a pumping unit and motor. Rig used during completion still on well. Pit used during frac job was open. The company will be notified of inspection and will be advised to finish restoration. Division intern Brittany Hupp accompanied me on this inspection. Time of inspection: 3:30 PM. Weather: 75*F, Cloudy |
1653906542 | 2014-06-10 | Drill / Deepen / Reopen | No Violations | I inspected drilling operations. H & D Drilling dusting at the top of the Lime during inspection. No violations. |
1661991880 | 2014-06-06 | Casing String Witnessed | No Violations | I witnessed H & D Drilling pressure up on the 8 surface casing. The casing was tested @ 300 lbs. for 30 minutes. The pressure did not drop after 30 minutes. No violations. |
1685656607 | 2015-08-07 | Preliminary Restoration | No Violations | Inspect well as part of a preliminary restoration status check. The well was equipped with pumping unit and motor. The well was pumping during inspection. A service rig was on the well. The tank battery consists of (1) 100 barrel tank, (2) separators, (2) meters, and a compressor station. The pit has been closed. All drilling equipment has been removed. The location has been restored. Inspection meets ORC 1509.072 requirements. Time of inspection: 9:50 AM. Weather: 68*F, Sunny |
2085499438 | 2014-05-20 | Drill / Deepen / Reopen | No Violations | Inspect drilling operations. H & D Drilling tripping in drill collars during inspection. H & D Drilling set approximately 110 feet of drive pipe. The hole caved in at 180 feet. Additional drive pipe has been installed to prevent well from caving in. |
356428281 | 2014-5-27 0:00: | DD | No Violations | |
91691116 | 2014-5-7 0:00:0 | DD | No Violations |
For data sources see[9]