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Well ID: 34-103-22495 | Loading map...
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Country: United States | |
State: Ohio | |
County: Medina | |
Municipality: Sharon Township | |
Operator Name: G & O RESOURCES LTD | |
Well Pad ID: | |
Farm/Lease Name: DILLEY G | |
License Status: Plugged and Abandoned | |
License Date: 2015-02-18 | |
Spud Date: 1981-01-31 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-02-05 | |
Well Total Depth: 3681.00 ft | |
Configuration: Vertical | |
Latitude: 41.130000 | |
Longitude: -81.750000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-12-30 | 5 PENINSULA GROUP INC GeoDate 12/30/80 |
Oil and Gas | 1980-12-30 | Issued Date 12/30/80 Expired Date Acres 0134600 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
Original Spud | 1981-01-31 | |
Completed | 1981-02-05 | |
Reached Total Depth | 1981-02-05 | |
Completion Report Received | 1981-08-14 | |
CO | 1991-11-13 | 201 GREEN GAS CO GeoDate 12/30/80 |
CO | 1992-09-01 | 4280 JRD ENERGY GeoDate 12/30/80 |
Change of Owner | 1997-08-04 | Operator changed from 4280, JRD ENERGY to 5894, G & O RESOURCES LTD |
APP | 2015-02-18 | Proposed Formations:CLINTON, Issued Date:2/18/2015, Expired Date:2/17/2017 12:00:00 PM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-06-29 | |
Record Last Modified | 2017-02-10 | |
Construction Permit Expires | 2017-02-17 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3525 | 3555 | 17 |
3525 | 3555 | 17 | |
3525 | 3555 | 17 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 63400 Gal | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | PENINSULA GROUP INC | 6836.00 | 134.00 | 365 |
1985 | PENINSULA GROUP INC | 5621.00 | 0.00 | 0 |
1986 | PENINSULA GROUP INC | 2375.00 | 74.00 | 365 |
1987 | PENINSULA GROUP INC | 1093.00 | 0.00 | 365 |
1988 | PENINSULA GROUP INC | 803.00 | 48.00 | 365 |
1989 | PENINSULA GROUP INC | 943.00 | 0.00 | 365 |
1990 | PENINSULA GROUP INC | 1210.00 | 56.00 | 365 |
1991 | PENINSULA GROUP INC | 1079.00 | 0.00 | 365 |
1992 | JRD ENERGY | 971.00 | 0.00 | 365 |
1993 | JRD ENERGY | 966.00 | 0.00 | 365 |
1994 | JRD ENERGY | 881.00 | 0.00 | 365 |
1995 | JRD ENERGY | 762.00 | 0.00 | 365 |
1996 | JRD ENERGY | 837.00 | 0.00 | 365 |
1997 | JRD ENERGY | 370.00 | 83.00 | 197 |
1998 | G & O RESOURCES LTD | 771.00 | 0.00 | 365 |
1999 | G & O RESOURCES LTD | 381.00 | 0.00 | 360 |
2000 | G & O RESOURCES LTD | 464.00 | 0.00 | 360 |
2001 | G & O RESOURCES LTD | 408.00 | 0.00 | 365 |
2002 | G & O RESOURCES LTD | 298.00 | 0.00 | 365 |
2003 | G & O RESOURCES LTD | 114.00 | 0.00 | 365 |
2004 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2005 | G & O RESOURCES LTD | 0.00 | 34.00 | 365 |
2006 | G & O RESOURCES LTD | 3.00 | 0.00 | 365 |
2007 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2008 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2009 | G & O RESOURCES LTD | 28.00 | 0.00 | 365 |
2010 | G & O RESOURCES LTD | 0.00 | 0.00 | 365 |
2011 | G & O RESOURCES LTD | 0.00 | 0.00 | 365 |
2012 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2013 | G & O RESOURCES LTD | 21.00 | 0.00 | 365 |
2014 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2015 | G & O RESOURCES LTD | 0.00 | 0.00 | 0 |
2016 | G & O RESOURCES LTD | 5.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | PENINSULA GROUP INC | Brine | 0 | 365 |
1985 | PENINSULA GROUP INC | Brine | 140 | 0 |
1986 | PENINSULA GROUP INC | Brine | 0 | 365 |
1987 | PENINSULA GROUP INC | Brine | 0 | 365 |
1988 | PENINSULA GROUP INC | Brine | 0 | 365 |
1989 | PENINSULA GROUP INC | Brine | 0 | 365 |
1990 | PENINSULA GROUP INC | Brine | 40 | 365 |
1991 | PENINSULA GROUP INC | Brine | 0 | 365 |
1992 | JRD ENERGY | Brine | 0 | 365 |
1993 | JRD ENERGY | Brine | 78 | 365 |
1994 | JRD ENERGY | Brine | 0 | 365 |
1995 | JRD ENERGY | Brine | 80 | 365 |
1996 | JRD ENERGY | Brine | 0 | 365 |
1997 | JRD ENERGY | Brine | 0 | 197 |
1998 | G & O RESOURCES LTD | Brine | 40 | 365 |
1999 | G & O RESOURCES LTD | Brine | 0 | 360 |
2000 | G & O RESOURCES LTD | Brine | 5 | 360 |
2001 | G & O RESOURCES LTD | Brine | 0 | 365 |
2002 | G & O RESOURCES LTD | Brine | 0 | 365 |
2003 | G & O RESOURCES LTD | Brine | 45 | 365 |
2004 | G & O RESOURCES LTD | Brine | 0 | 0 |
2005 | G & O RESOURCES LTD | Brine | 0 | 365 |
2006 | G & O RESOURCES LTD | Brine | 0 | 365 |
2007 | G & O RESOURCES LTD | Brine | 0 | 0 |
2008 | G & O RESOURCES LTD | Brine | 0 | 0 |
2009 | G & O RESOURCES LTD | Brine | 0 | 365 |
2010 | G & O RESOURCES LTD | Brine | 0 | 365 |
2011 | G & O RESOURCES LTD | Brine | 0 | 365 |
2012 | G & O RESOURCES LTD | Brine | 0 | 0 |
2013 | G & O RESOURCES LTD | Brine | 0 | 365 |
2014 | G & O RESOURCES LTD | Brine | 0 | 0 |
2015 | G & O RESOURCES LTD | Brine | 0 | 0 |
2016 | G & O RESOURCES LTD | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1553941472 | 2015-7-27 0:00: | FR | No Violations | |
-1786355292 | 2014-8-8 0:00:0 | PW | No Violations | |
-235332298 | 2015-3-17 0:00: | PW | No Violations | |
-656657806 | 2015-6-17 0:00: | PB | No Violations | |
000PL12183 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0235332298 | 2015-03-17 | Production Wells | No Violations | Inspected production well on 03/17/2015 to follow-up on a previously-issued compliance notice. The tank battery consists of 1-210 bbl steel tank, 1-100 bbl steel tank, and 1-horizontal separator located within an earthen dike; the diked area is located within an unlocked metal fence. Well identification is clearly displayed. The well is a rabbit well. No problems were noted at the time of the inspection. According to 2014 production data, the well did not produce. A plugging permit has been issued, and Nicks Well Plugging is scheduled to plug the well in early June, therefore a 4-month extension is granted to get the well plugged. |
0421492865 | 2015-08-03 | Final Restoration | No Violations | Visited location on 08/03/2015 to follow-up on the status of location reclamation. The location has been graded, but still needs re-seeded. Will continue to follow-up. |
0656657806 | 2015-06-17 | Plug / Plug Back | No Violations | Visited location on 06/17/2015 to witness plugging operations at the Dilley #2 well. Nicks Well Plugging was onsite and rigged up, and in the process of digging the pit. Finished digging and lining pit. Began pumping on well to see if a rabbit is present downhole - it is. Attempted to circulate out the rabbit, but were unable to do so. Pulled all tubing out of hole to retrieve rabbit. Retrieved rabbit. Ran all tubing back downhole to set bottom plug through tubing. Pumped fluid ahead, but did not try to achieve circulation, as 50 bbls had already been used attempting to flush out the rabbit. Set bottom (Clinton) plug through tubing from 3,605-3,205. Broke circulation during displacement. Finished pumping displacement. Began pulling tubing out of the well. Transmission on draw works went out with one joint to go. Shut down for rig repairs. |
1553941472 | 2015-07-27 | Final Restoration | No Violations | Visited location on 07/27/2015 to check on status of location reclamation. The tanks have been removed and the pit closed. The location has been mostly rough graded, but not yet re-seeded. Will follow-up. |
1786355292 | 2014-08-08 | Production Wells | Violations Noted | Inspected production well on 08/08/2014. The tank battery consists of 1-210 bbl steel tank, 1-100 bbl steel tank, and 1-horizontal separator within an earthen dike. The diked area is located within an unlocked metal fence. Well identification is clearly displayed at the tank battery. The well is a rabbit well. The area around the wellhead was overgrown at the time of the inspection. Research into the production history of the well showed that it has not met the minimum production requirements since 2005, therefore the well must be plugged. |
1833161733 | 2015-06-16 | Plug / Plug Back | No Violations | Visited location on 06/16/2015 with Kevin Komara to check on status of plugging operations. Nicks Well Plugging is moving equipment in and plan to plug tomorrow. |
2061436120 | 2015-06-29 | Plug / Plug Back | No Violations | Visited location on 06/29/2015 to continue plugging out well. Rigged up Nicks Well Plugging. As pit was very full, decision made to pump out pit to production tanks through flowline. Broke circulation prior to setting Big Lime/Oriskany plug. Pulled out 2,310 4 1/2 casing. Ran in hole with 21 joints tubing. Broke circulation prior to setting plug. Set Berea plug. Pulled up to set top plug. Broke circulation prior to setting plug. Set plug to surface. Pulled out last 6-joints of tubing. Top of cement fell down approximately 3-4. Topped off with mixed cement. No problems encountered during plugging operations. |
421492865 | 2015-8-3 0:00:0 | FR | No Violations | |
PL12183 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1786355292 | US-OH-117806 | 2014-10-07 | Well shall be plugged |
For data sources see[9]