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34-103-24515

Well Details

Well ID: 34-103-24515
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Country: United States
State: Ohio
County: Medina
Municipality: Chatham Township
Operator Name: HARLEY DRILLING & PRODUCING LT
Well Pad ID:
Farm/Lease Name: KING
License Status: Active Injection
License Date: 1994-01-10
Spud Date: 1989-06-19
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]]
Final Drill Date: 1994-06-28
Well Total Depth: 2806.00 ft
Configuration: Vertical
Latitude: 41.090000
Longitude: -82.030000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1989-05-30 3363 KING OIL GeoDate 5/30/89
Conversion to Injector 1989-05-30
Salt Water Injection Well 1989-05-30 Issued Date 5/30/89 Expired Date 5/30/90 Acres 0100000 Tool Type RTAF Proposed Formation NEWBURG/CLIN Proposed Depth 02806 Proposed Drill Depth 02806
Storage Well 1989-05-30 Issued Date 5/30/89 Expired Date 5/30/90 Acres 0100000 Tool Type RTAF Proposed Formation NEWBURG/CLIN Proposed Depth 02806 Proposed Drill Depth 02806
Original Spud 1989-06-20 RI/CONVERT 1-15-94
Completion Report Received 1989-07-12 RI/CONVERT 1-15-94
First Injection 1989-08-03 RI/CONVERT 1-15-94
CO 1992-04-23 3363 KING OIL GeoDate 4/23/92
Salt Water Injection Well 1992-04-23 Issued Date 6/2/92 Expired Date Acres 0100000 Tool Type CT Proposed Formation ORISKANY/NEWBURG Proposed Depth Proposed Drill Depth
Storage Well 1992-04-23 Issued Date 6/2/92 Expired Date Acres 0100000 Tool Type CT Proposed Formation ORISKANY/NEWBURG Proposed Depth Proposed Drill Depth
Plugged Back 1992-04-25 RI/CONVERT 1-15-94
CO 1994-01-10 3363 KING OIL GeoDate 1/10/94
Salt Water Injection Well 1994-01-10 Issued Date 1/10/94 Expired Date 1/10/95 Acres 0100000 Tool Type NT Proposed Formation ORIS/SICL/NBRG Proposed Depth 00000 Proposed Drill Depth 00000
Storage Well 1994-01-10 Issued Date 1/10/94 Expired Date 1/10/95 Acres 0100000 Tool Type NT Proposed Formation ORIS/SICL/NBRG Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1994-06-28 RI/CONVERT 1-15-94
Reached Total Depth 1994-06-28 RI/CONVERT 1-15-94
Construction Permit Expires 1995-01-10 RI/CONVERT 1-15-94
Annulus Pressure Monitoring Approved 1998-11-27 RI/CONVERT 1-15-94
Last Compliance Report 2002-01-24 RI/CONVERT 1-15-94
Change of Owner 2002-12-10 Operator changed from 3363, KING OIL to 6748, REPUBLIC OIL INC.
Change of Owner 2009-10-01 Operator changed from 6748, HEARTLAND OIL & GAS to 8547, KING OIL COMPANY INC
Change of Owner 2019-05-08 Operator changed from 8547, KING OIL COMPANY INC to 337, HARLEY DRILLING & PRODUCING LTD
Record Last Modified 2019-05-08 RI/CONVERT 1-15-94

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-01-24 1760 0
2002-01-24 2586 2610 1
1760 0
2586 2610 1
1760 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 15 2000 Gal 0 ACIDIZED W/2000 GAL 15% HCL

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1051818798 2013-5-9 0:00:0 SW No Violations
-1055332763 2014-12-8 0:00: SW No Violations
-1190102949 2019-8-5 0:00:0 SW No Violations 1.40
-1191139431 2010-9-2 0:00:0 SW No Violations 1.00
-1296927590 2018-11-2 0:00: SW No Violations
-1486765048 2014-3-31 0:00: SW No Violations
-1512751067 2018-8-17 0:00: SW No Violations
-1592419846 2003-7-1 0:00:0 SW No Violations 1.50
-1661326208 2008-3-28 0:00: SW No Violations 1.00
-1700924333 2017-3-24 0:00: SW No Violations
-1736713394 2016-3-10 0:00: SW No Violations
-1766601139 2017-11-9 0:00: SW No Violations 1.00
-1777720954 2007-7-23 0:00: SW No Violations 1.00
-1798004468 2017-9-25 0:00: SW No Violations
-2028915081 2003-1-7 0:00:0 SW No Violations 1.50
-275442058 2009-8-7 0:00:0 SW No Violations 1.00
-355096126 2009-9-11 0:00: SW No Violations 1.00
-379913583 2014-9-29 0:00: SW No Violations
-384111000 2014-9-29 0:00: SW No Violations
-418241578 2013-9-25 0:00: SW No Violations
-421570946 2016-8-8 0:00:0 SW No Violations
-511256226 2020-2-10 0:00: SW No Violations 1.30
-645490925 2016-12-9 0:00: SW No Violations
-681435873 2020-1-8 0:00:0 SW No Violations 1.00
-699110419 2019-4-30 0:00: SW No Violations
-712511271 2010-4-12 0:00: SW No Violations 1.00
-813244393 2015-5-23 0:00: SW No Violations
-997605089 2016-6-30 0:00: SW No Violations
0000UIC724 1989-07-03 Salt Water Injection Well No Violations 1509.22 (A)(2) Storage of Brine
0000UIC725 1989-07-03 Salt Water Injection Well No Violations 1501:9-3-04 (A) Prevention of Contam
0000UIC726 1989-07-03 Salt Water Injection Well No Violations 1509.072 Restore Land Surface
0000UIC761 1989-09-11 Salt Water Injection Well No Violations 1509.22 (A)(2) storage & disposal
0000UIC762 1989-09-11 Salt Water Injection Well No Violations 1501:9-3-04 Prevent cont. & Poll
000PL11290 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
000UIC1050 1991-02-26 Salt Water Injection Well No Violations 1509.03 RULES & REG.
000UIC1051 1991-02-26 Salt Water Injection Well No Violations 1509.22 (A,2) STORAGE & DISPOSAL
000UIC1052 1991-02-26 Salt Water Injection Well No Violations 1501:9-3-04 POLLUTION
000UIC1095 1991-03-26 Salt Water Injection Well No Violations 1501:9-3-07 (E) 4TH.QTR.REPORT
000UIC1096 1991-03-26 Salt Water Injection Well No Violations 1501:9-3-07 (F) 4TH.QTR.REPORT
000UIC1152 1991-09-24 Salt Water Injection Well No Violations 1501: 9-3-07 (E)&(F) QUARTERLY REPORTS
000UIC1207 1992-01-02 Salt Water Injection Well No Violations 1501: 9-3-07 (E) QUARTERLY REPORTS
000UIC1536 1994-08-12 Salt Water Injection Well No Violations 1509.22 STORAGE AND DISPOSAL
000UIC1537 1994-08-12 Salt Water Injection Well No Violations 1501: 9-5-06 PREVENT CONTAMINATE
000UIC1538 1994-08-12 Salt Water Injection Well No Violations 1509.072 RESTORATION
000UIC1596 1995-02-03 Salt Water Injection Well No Violations 1509.03 PERMIT
000UIC1597 1995-02-03 Salt Water Injection Well No Violations 1501: 9-1-07 PREVENT CONYAMINATE
000UIC1598 1995-02-03 Salt Water Injection Well No Violations 1501: 9-8-06 (B) IDENTIFICATION
000UIC1712 1998-03-30 Salt Water Injection Well No Violations 1501:9-3-07 (C) NEED TO RUN MINITEST
000UIC1721 1998-05-20 Salt Water Injection Well No Violations 1501:9-3-07 (E) (F) QUARTERLY REPORTS
000UIC1775 1999-06-22 Salt Water Injection Well Violations Noted 1501: 9-03-07 (E) (F) ANNUAL REPORTS
0011320513 2016-03-02 Salt Water Injection Well No Violations Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd & 4th quarter of 2015 despite a letter that was sent with a deadline of February 29, 2016. Please submit the appropriate reports by March 16th, 2016. REPORTS RECD
001220i135 2002-01-25 Salt Water Injection Well No Violations Violations have been corrected and well has 125psi on gauge.
0012778811 2001-12-06 Salt Water Injection Well No Violations Republic Oil is working on facility to bring in production. Well has been idle. Serivice rig scheduled for 12-10-2001 to reset packer in well. Notified company to clean up oil and water in dike. Remove debris around staging area. Identify well and tank battery.
0012979460 2002-07-10 Salt Water Injection Well No Violations An unreported oil spill and an open unlined brine pit were discovered during a quarterly inspection of the injection operation. Inspectors Moravy and Worstall conducted the inspection. Also on site during the inspection was Jim Persinger (330-242-3539), King Oil pumper. The oil spill originated outside of the southeast corner of the tank battery dike. The vegetation kill zone affected an area approximately 100 feet long and 20 feet wide. At this point, the spill entered a small unnamed creek. Kings response to the release was to lime and straw the vegetation and place sorbent pads in the drainage way. The pads were all oil saturated. King did not report the release to either OEPA or ODNR. The open pit was constructed for a pressure test conducted on January 25, 2002. After the testing, the pit was supposed to be pumped out and closed. Instead, the liner was removed and the pit was left open. Quantab analysis of the water in the pit indicated chloride concentrations in excess of 6,514 ppm. A new growth vegetation pattern indicates that the pit has overflowed and impacted downgradient vegetation. The facility was ordered closed and spill remediation was to begin immediately. Pete Mongue (330-242-3540) with King Oil was notified by phone.
0014379551 2002-07-19 Production Wells No Violations Heartland Oil and Gas retained Petro Environmental to remove and dispose of the contaminated soil downgradient from the oil spill and the contaminated soil near the open pit. The pit has been pumped out and closed and the oil impacted soil has been removed. Both areas will be limed, seeded and mulched. The line leak was repaired and the loading pad vault has been pumped. The major issues have been addressed. The NOV will be satisfied after the vegetation has established itself. The receptor creek will need to be monitored for any sheen after the next several rainfalls. The stressed vegetation near the open pit will also need to be monitored. The on-site personnel included James Ray (480-816-6140), Pete Mongue (330-242-3540), and Jim Persinger (330-242-3539) with Heartland (aka Republic Oil) and Randy Jarvis (330-948-1494) with Petro.
002155i131 2002-07-15 Salt Water Injection Well No Violations Follow up inspection to oil and brine spills discovered at this UIC well and Berea field. The wells are under the King Oil bond but are operated by Heartland Oil and Gas. Work on remediating the spills has not begun. Conversations with Heartland CFO (Katrina Baines 503-228-7905) indicated that they are trying to correct the record. Clean-up is scheduled to start 7/18.
002155i232 2002-08-12 Salt Water Injection Well No Violations Status check inspection - the Operator has remediated the spill and closed the pit. The impacted area has been seeded and mulched. Have not received soil disposal documentation. Waiting for rainfall in order to verify no impact in the stream channel and to promote vegetation growth before passing.
002155i288 2002-09-04 Salt Water Injection Well No Violations The oil spill has been remediated and the vegetation has established. The violation has been corrected.
002155i341 2002-09-30 Salt Water Injection Well No Violations Status check inspection of the injection well. No violations at this time.
0133847209 2018-02-16 Salt Water Injection Well Violations Noted Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarter of 2017 . Please submit the appropriate reports by March 17, 2018. Reports received March 28, 2018.
0275442058 2009-08-07 Salt Water Injection Well No Violations Tested tubing pressure at 620 psi. Advised company to shut down well asap and reduce pressure to 365 psi. Call inspector prior to injection for a test. Annular side needs pumped to 200 psi and tested. Well is being sold to Dave King. King Oil is to take possession on August 15, 2009.
0289447641 2019-01-04 Salt Water Injection Well No Violations I found no evidence of recent activity. The injection well is not in operation. The diked tank battery is full of water and overgrown vegetation. The injection well and facility equipment have a rusty and corroded appearance. The access road gate was closed.
0318033298 2007-12-04 Salt Water Injection Well Violations Noted No response to NOV. All violations remain and packer test was not scheduled. Requesting Chiefs Order to forfeit bond. Snow flurries, 30 degrees.
0355096126 2009-09-11 Salt Water Injection Well No Violations Injection pressure at 350 psi. No violations at this time. Sun, 70 degrees.
0379913583 2014-09-29 Salt Water Injection Well No Violations Visited location on 09/29/2014 with Steve Ochs to perform quarterly inspection.
0384111000 2014-09-29 Salt Water Injection Well No Violations An inspection found the well idle. The pressure on the tubing was equal to that of the tubing/casing annulus. The well owner was instructed to perform a mechanical integrity test (MIT) on the well. Furthermore, the injection operation cannot resume, until the MIT is successfully completed.
0418241578 2013-09-25 Salt Water Injection Well No Violations My inspection of the well and injection facility found no violations.
0421570946 2016-08-08 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
0515126667 2017-06-29 Salt Water Injection Well No Violations Performed quarterly inspection of the injection well and surface facilities on 06/29/2017 with Steve Ochs. Pressure was noted on the tubing, however it was too small to be registered by the gauge (<20 psi). No problems were noted at the time of the inspection.
0645490925 2016-12-09 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations at the time.
0647087283 2018-05-08 Salt Water Injection Well No Violations

-

King Oil Company still needs to: Clean up all of the oil impacted peat sorb, soil, weeds and grass. Properly dispose of the oil impacted peat sorb, soil, weeds, and grass. Repair the damaged 100 bbl. storage tank. Post a new identification sign.

0712511271 2010-04-12 Salt Water Injection Well No Violations Injection pressure has been lowered to 295 psi at well. Underground concrete vault was pumped and identification posted on pump house. Sun, 60 degrees.
0813244393 2015-05-23 Salt Water Injection Well No Violations Visited location on 05/23/2015 to witness mechanical integrity test (MIT). Moore Well Service, David King (King Oil), and Steve Ochs were onsite. Pressured well up to 600# for initial test - well failed almost immediately. Let well sit for a few minutes. Pressured well up to 560# at 11:04A. At 11:20AM, the well had 559#. Test passed.
0952638995 2018-01-02 Salt Water Injection Well No Violations
0997605089 2016-06-30 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1029362184 2019-6-11 0:00: SW No Violations 1.70
1043343282 2019-02-11 Salt Water Injection Well Violations Noted The Division has not received the 1st, 2nd, 3rd, & 4th quarter brine disposal fees for 2018. Please forward disposal fees and sheets to the Division by 3/12/2019.
1051818798 2013-05-09 Salt Water Injection Well No Violations There was a new ID posted at the wellhead. The surface facility needs identification.
1054221679 2003-05-29 Salt Water Injection Well Violations Noted Need to maintain pressure on annulus or perform monthly minitest to demonstrate mechanicl integrity. Rebuild concrete block walls on loading pad and seal all cracks. Prepare gravel road to unloading pad.
1055332763 2014-12-08 Salt Water Injection Well No Violations The well owner has made no attempt to test the well. The well appears to be idle. There was no sign of recent activity on site.
1064842221 2003-09-29 Salt Water Injection Well Violations Noted Well in operation except for annular test needs completed. Pumper is working on annular hook up at this time.
1066225645 2003-10-15 Salt Water Injection Well No Violations Well has been set up to test annular space between 2 injection tubing and 4.5 casing. Tubing pressure is 100psi and annular pressure is 10psi. Mini test approved. Nov in compliance.
1079978662 2004-03-22 Salt Water Injection Well No Violations No activity at well site. Pressure gauges read 0 psi on well and annulus. No violations at this time. Snow, 30 degrees.
1086791052 2004-06-09 Salt Water Injection Well No Violations Inspected injection well and facility. No violations at site. Well mantained and clean. Sun,85 degrees.
1098278759 2004-10-20 Salt Water Injection Well No Violations Tubing valve is open at well. 0 psi on pressure gauges. No violations at well or Tank battery. 5-100 barrel tanks, 1-75 barrel tank and 2 separators in battery. Fog, 50 degrees.
1110303294 2005-03-08 Salt Water Injection Well Violations Noted Well is idle with 0 PSI on tubing and annulus. Overflow vault at pad is full and needs pumped. Need to pump 200 psi on tubing annulus to test integrity.
1119454476 2005-06-22 Salt Water Injection Well Violations Noted No response from company on NOV. Brine is leaking from 2 line inside tank battery contained in dike. Production wells are in operation. Sun 75 degrees
1125414575 2005-08-30 Salt Water Injection Well Violations Noted 2 line in tank battery has been repaired. Contamination removed in dike. Peter Mongue called to advise NOV in compliance. Rain, 75 degrees.
11320513 2016-3-2 0:00:0 SW No Violations
1136322142 2006-01-03 Salt Water Injection Well No Violations Met with new pumper on site and discussed well integrity. Advised company to keep underground tank pumped and stops installed in 100 barrel storage tanks.Jay, of Heartland, is putting Berea wells in production. Scheduled mini-test on annulus. No outstanding violations. Rain, 40 degrees.
1140024725 2006-02-15 Salt Water Injection Well Violations Noted Well idle at this time. Company is reconstructing injection pump and piping. Bull plugs have been put in storage tanks in dike. Underground storage tank at unloading site needs pumped. Annulus on well is reading 15psi. 0psi on tubing. Cloudy, 40 degrees
1140031126 2006-02-15 Salt Water Injection Well Violations Noted Underground storage tank needs pumped. Schedule annular tubing test. Bull plugs are in tanks. Re-constructing tubing pump.
1141071260 2006-02-27 Salt Water Injection Well Violations Noted Violations have been corrected. Concrete vault has been pumped. Tested packer at 200 psi. 0 psi drop in pressure for 15 minutes. Snow 30 degrees.
1147118737 2006-05-08 Salt Water Injection Well No Violations Called by Heartland Oil and Gas to inspect annulus and tubing pressure. Well is in compliance at this time. Pressured up on packer at 225psi and had 0psi drop in pressure. Tubing pressure is holding at 340psi. 70 degrees, sun.
1156490286 2014-06-27 Salt Water Injection Well No Violations The well was found idle. The well tender was told to pressure up the tubing/casing annulus.
1158239773 2006-09-14 Salt Water Injection Well Violations Noted Met on site with Jay, from Heartland Oil and Gas. Advised him to repair concrete block on spill pad. Grout is falling out between blocl and concrete vault is full and needs pumped. Jay is removing tanks in battery and replacing them with good 100 barrel tanks. Rain, 60 degrees.
1161800939 2006-10-25 Salt Water Injection Well No Violations New block wall has been built on spill pad. Conducted a mini- test on annulus at 200 psi and pressure did not drop in 15 minutes. Spill vault has been pumped out and is empty. NOV in compliance. Cloudy, 40 degrees.
1170858158 2007-02-07 Salt Water Injection Well No Violations Injection well inspection. Well is idle due to cold weather. No violations at this time. 0 degrees, snow.
1187791066 2007-08-22 Salt Water Injection Well No Violations No response from Heartland Oil and Gas since NOV was issued. Lease is shut down and gate is closed. Called Peter Mongues cell phone and office numbers and he advised me violations would be corrected in 10 days. Violations have not been corrected. Cloudy, 80 degrees.
1191139431 2010-09-02 Salt Water Injection Well No Violations Inspected well. Injection pressure is at 510 psi. Pump is not running. Tanks in battery have not been replaced. Brine remains leaking. Request Chiefs Order to suspend operations.
1200580888 2008-01-17 Salt Water Injection Well No Violations Pollution and contamination violations have been corrected. Well is in operation. Brine tank has been pumped. Area west of tank battery , contamination stopped. Barrel count is 3740. Called Dave King to schedule mini test on packer annulus. Cloudy, 25 degrees.
1202239016 2008-02-05 Salt Water Injection Well No Violations David King is operating the Heartland Oil and Gas wells. Called by David King to test annulus and packer on injection well. Pumped annular side of tubing to 220 psi and pressure fell 50 psi. pumped pressure to 200 psi and it dropped to 195 psi. Pumped back to 200 psi and pressure held for 15 minutes with out decline. NOV in compliance. Rain, 50 degrees.
1220i135 2002-1-25 0:00: SW No Violations 1.00
1232631273 2009-01-22 Salt Water Injection Well Violations Noted Well pressures are at 0 psi. Advised David King to schedule annulus pressure test when weather warms. Berea lease inactive due to cold weather. Identification needs updated.
1239627509 2009-04-13 Salt Water Injection Well No Violations Annulus pressure is holding at 110 psi. Advised Heartland Oil and Gas to pump concrete brine tank at unloading station. Update identification. Cloudy, 40 degrees.
1244637743 2009-06-10 Salt Water Injection Well Violations Noted No identification posted at well or pump house. Well needs annulus pressured to 200 psi and reported. Underground brine tank needs pumped. Drainage from pump house needs cleaned up on ground. Oil inside dike needs cleaned up.
1245762111 2009-06-23 Salt Water Injection Well Violations Noted Inspection of annulus pressure found injection pressure over the maximum. 395 psi is maximum and injection pressure is at 640 psi. Shut down well until pressure is at 395 psi. Pressured up annulus to 200 psi and had 0 psi decline in 15 minutes.
1247676244 2009-07-15 Salt Water Injection Well No Violations Arrived on location and Roger Canfield was blowing pressure down in a tank from top of injection well. Pressure was still holding at 500 psi. I advised him to drain water off until pressure is at 365 psi. Post identification at well. Repair brine leak in pump house and clean up 2 X 10 contaminated area outside of pump house.
1250697142 2009-08-19 Salt Water Injection Well No Violations Injection pressure has been lowered to 280 psi. Annular side is holding at 180 psi. Advised company to resume injection. NOV in compliance. Sun, 80 degrees.
1261492710 2009-12-22 Salt Water Injection Well No Violations Dave King purchased Heartland Oil. Acidized injection formation and tested packer. Pumped annulus side to 175 psi with 0 psi decline. Injection pressure is at 250 psi. Test approved. Advised Dave King to change identification on well and tanks and update company name. Snow, 30 degrees.
1277818089 2010-06-29 Salt Water Injection Well Violations Noted Mechanical integrity test. Pressure on annular side holding at 195 psi. and injection pressure is at 385 psi. Identification on pump house, but needs and emergency phone number on ID. Identify well at well site. Three 100 barrel tanks are leaking brine through heater tubes and 1 valve inside dike. Repair or replace tanks in dike by 7-29-2010. Cloudy, wet, 70 degrees.
12778811 2001-12-6 0:00: SW No Violations 1.50
1280344448 2010-07-28 Salt Water Injection Well No Violations Follow up to NOV. Brine tanks have not been removed and injection pressure is over limit. Called Dave King and advised him to shut down injection pump ASAP. It was over 600 psi. He advised the brine tanks will be removed this week and replaced with plastic tanks. Identification has been posted. Hot, 90 degrees.
1281017031 2010-08-05 Salt Water Injection Well No Violations Requested by David King to test injection pressure. Pressure was at 290 psi. After 15 minutes pressure climbed to 320 psi. Pressure valve began to leak brine. Advised David King to shut in well until gauge valve is replaced. Advised Dave King to filter water or have well serviced. Non- compliance. Sun, 80 degrees.
1284402010 2010-09-13 Salt Water Injection Well No Violations Storage tanks remain hooked up in tank battery. Two fiberglass tanks are in battery but not hooked up. Pressure on well is over 600 psi. I advised David King to shut well in until pressure is below 395 psi. Call division before injecting. Compliance order in non-compliance. Sun, 75 degrees.
1285851089 2010-09-30 Salt Water Injection Well No Violations Injection pressure at 360 psi. Approved company to begin injection. Advised Dave King to attach new pressure gauge to well. Storage tanks are set in battery but not hooked up. Waiting on contractor to pull 100 barrel tanks. Identification is posted at well. Cloudy, 55 degrees.
1296826359 2011-02-04 Salt Water Injection Well No Violations Injection pressure is at 240 psi. Annular side is at 50 psi. 100 barrel tank that was leaking has been removed and replaced with 80 barrel fiberglass tank in battery. NOV in compliance.12 snow on ground. Cold, sun, 15 degrees.
1296927590 2018-11-02 Salt Water Injection Well No Violations I found no evidence of recent activity. The injection well was not in operation. The injection well has a corroded appearance. There are several inches of rain water in the diked tank battery. I observed no spills or leaks.
12979460 2002-7-10 0:00: SW No Violations
1310547519 2020-8-13 0:00: SW No Violations 1.20
133847209 2018-2-16 0:00: SW No Violations
1404320774 2014-07-01 Salt Water Injection Well No Violations One hour prior to inspection, the well tender pumped up the pressure on the annulus to two hundred pounds per square inch. An inspection found 75 psi. of pressure on the tubing and 197 psi. on the tubing/casing annulus. The pressure readings did not change, during a 20 minute period.
14379551 2002-7-19 0:00: PW No Violations
1486765048 2014-03-31 Salt Water Injection Well No Violations No violations were found at the time of inspection.
1488394924 2017-02-28 Salt Water Injection Well No Violations Our records indicate that the Division has not received the Salt Water Injection Well disposal fees for the 1st, 2nd, 3rd, & 4th quarters of 2016. Please submit the appropriate reports by March 14, 2017. Fee reports received 3/13/2017
1501351720 2020-3-5 0:00:0 SW No Violations
1512751067 2018-08-17 Salt Water Injection Well No Violations

-3-06(K) is not posted on site. The entire site is overgrown with vegetation. There are several inches of water inside of the diked tank battery. There is a lock on the pump house. I spoke with David King from King Oil Company. I instructed Mr. King to post a proper identification sign at the facility and well by September 28, 2018. Mr. King stated the signs would get posted by September.

1522166093 2018-03-27 Salt Water Injection Well Violations Noted


I told Mr. King to: Clean-up all impacted soil and properly dispose of the material. Repair the leaking 100 bbl. storage tank.

Mr. King was notified a compliance notice has been issued. Photos were taken and are available upon request. A follow-up inspection will be conducted by April 9, 2018.

1553778320 2019-3-28 0:00: SW No Violations
1592419846 2003-07-01 Salt Water Injection Well Violations Noted Loading pad concrete blocks have been grouted to prevent leakage. Operators pumper has left employment. I advised them to install pressure gauge on 4.5 annulus for monitoring.
1594641028 2020-6-3 0:00:0 SW No Violations 1.50
1596671949 2013-03-19 Salt Water Injection Well Violations Noted My inspection of the well and surface facility found the following: The identification was no longer legible. The two inch valve on the annulus was stuck open.

Post a complete ID and ensure all valves on the well are in working order.

1661326208 2008-03-28 Salt Water Injection Well No Violations Inspected site and pressures. No violations at this time. Annular side is at 100 psi and tubing is at 0 psi. Pump is idle. Snow flurries, 32 degrees.
1661506133 2008-09-02 Salt Water Injection Well No Violations Well is in operation. Company truck unloading brine. Underground storage tank has been pumped. No violations at this time. David King advised, well needs acidized due to slow intake of brine.
1700924333 2017-03-24 Salt Water Injection Well No Violations An inspection of the injection well and surface facility found no violations.
1729323986 2015-03-31 Salt Water Injection Well No Violations A mechanical integrity test (MIT) is required. No attempt has been made to perform a MIT on the well. The well remains idle.
1736713394 2016-03-10 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
1746311964 2019-4-30 0:00: SW No Violations
1759848615 2011-06-29 Salt Water Injection Well No Violations Quarterly status check inspection found no violations at this time. The injection system was not running during this inspection.
1766601139 2017-11-09 Salt Water Injection Well No Violations
1777720954 2007-07-23 Salt Water Injection Well Violations Noted Inspecting injection well and found a 25 x 100 dead vegetation area west of brine injection tank battery. Brush and trees are dying, leading to a production berea well. Called Peter Mongue to meet with him on site.
1798004468 2017-09-25 Salt Water Injection Well No Violations Performed quarterly inspection on 09/25/2017 at the request of Steve Ochs and Andrew Adgate (DOGRM). The valves on the casing and tubing could not be opened/closed to allow pressure readings to be taken at the time of the inspection. Proper well identification is posted, and no problems were noted at the time of the inspection.
180749171 2019-10-2 0:00: SW No Violations 1.70
1838618888 2020-5-6 0:00:0 SW No Violations
1842046913 2010-03-25 Salt Water Injection Well Violations Noted Pressure tested injection pressure and it is at 730 psi. Maximum allowable pressure is 395 psi. Shut down injection until pressure is below 395 psi. Post identification at tank battery and well site. Pump concrete storage tank at loading pad. Met with Richard Hardway and shut down injection pump. Advised him of violations. Rain, 50 degrees.
2028915081 2003-01-07 Salt Water Injection Well No Violations Well is temporary shut down due to transformer problems in pump house. Pressure gauge at well reads 125 psi. Well and tank battery in compliance. Cloudy, 10 degrees.
2043760260 2013-03-19 Salt Water Injection Well No Violations FOLLOW UP TO NOV # 1596671949 My inspection of the well and surface facility found the following: The identification was no longer legible. The two inch valve on the annulus was stuck open.

Post a complete ID and ensure all valves on the well are in working order.

2054914839 2015-09-16 Salt Water Injection Well No Violations The injection well and surface facility were inspected. There were no violations found at the time.
2057732166 2018-07-06 Salt Water Injection Well No Violations I was on location to assess compliance notice #1522166093. I found the two (2) storage tanks sitting next to the diked tank battery removed. The oil impacted material has been removed. The injection well is not in operation. A sign is posted near the well. The access road gate was closed. There is overgrown vegetation throughout the site. There are several inches of standing water inside of the dike.
2067501343 2015-05-22 Salt Water Injection Well No Violations A mechanical integrity test (MIT) was performed on the well. A pressure of 561 psi. was placed on the tubing-casing annulus. The pressure of 45 psi. on the tubing remained constant. The MIT passed with a loss of 2 psi., during the fifteen minute test period.
2155i131 2002-7-15 0:00: SW No Violations
2155i232 2002-8-12 0:00: SW No Violations
2155i288 2002-9-4 0:00:0 SW No Violations
2155i341 2002-9-30 0:00: SW No Violations
289447641 2019-1-4 0:00:0 SW No Violations 1.30
318033298 2007-12-4 0:00: SW No Violations 1.00
515126667 2017-6-29 0:00: SW No Violations
647087283 2018-5-8 0:00:0 SW No Violations 1.50
842363469 2020-4-15 0:00: SW No Violations 1.00
952638995 2018-1-2 0:00:0 SW No Violations 0.80
iTOMK00009 2000-11-09 Salt Water Injection Well Violations Noted
iTOMK000091 2000-11-9 0:00: SW No Violations
iWEST00000 2003-04-30 Salt Water Injection Well No Violations NEED TO MAINTAIN PRESSURE ON ANNULUS OR PERFORM MONTHLY MINITEST; REBUILD CONCRETE WALLS ON UNLOADING PAD AND SEAL ALL CRACKS; PREPARE GRAVEL ROAD FOR UNLOADING PAD
iWEST000001 2003-4-30 0:00: SW No Violations
PL11290 PL No Violations
UIC1050 1991-2-26 0:00: SW No Violations
UIC1051 1991-2-26 0:00: SW No Violations
UIC1052 1991-2-26 0:00: SW No Violations
UIC1095 1991-3-26 0:00: SW No Violations
UIC1096 1991-3-26 0:00: SW No Violations
UIC1152 1991-9-24 0:00: SW No Violations
UIC1207 1992-1-2 0:00:0 SW No Violations
UIC1536 1994-8-12 0:00: SW No Violations
UIC1537 1994-8-12 0:00: SW No Violations
UIC1538 1994-8-12 0:00: SW No Violations
UIC1596 1995-2-3 0:00:0 SW No Violations
UIC1597 1995-2-3 0:00:0 SW No Violations
UIC1598 1995-2-3 0:00:0 SW No Violations
UIC1712 1998-3-30 0:00: SW No Violations
UIC1721 1998-5-20 0:00: SW No Violations
UIC1775 1999-6-22 0:00: SW No Violations
UIC724 1989-7-3 0:00:0 SW No Violations
UIC725 1989-7-3 0:00:0 SW No Violations
UIC726 1989-7-3 0:00:0 SW No Violations
UIC761 1989-9-11 0:00: SW No Violations
UIC762 1989-9-11 0:00: SW No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
000UIC1775 US-OH-131688 Failure to monitor pressures/volumes
000UIC1775 US-OH-131689 Failure to monitor annulus pressure
0133847209 US-OH-109742 2018-04-03 NONE Failure to report disposal fees
0318033298 US-OH-123163 2007-12-04 Pollution/Contamination
1043343282 US-OH-100657 2019-04-08 Failure to report disposal fees
1054221679 US-OH-100937 2003-05-29 Mechanical failure/contamination
1054221679 US-OH-100938 2003-05-29 Pits not liquid tight/Improper construction or use
1064842221 US-OH-101303 2003-09-29 Mechanical failure/contamination
1110303294 US-OH-102740 2005-03-08 Contamination at surface facility (permit after 6-1-82)
1119454476 US-OH-103038 2005-06-22 Contamination at surface facility (permit after 6-1-82)
1125414575 US-OH-103169 2005-03-08 Contamination at surface facility (permit after 6-1-82)
1140024725 US-OH-103537 2006-02-15 Violation of injection tubing/fitting requirements
1140024725 US-OH-103538 2006-02-15 Tanks not liquid tight/Improper burial
1140031126 US-OH-103539 2006-02-15 Violation of injection tubing/fitting requirements
1141071260 US-OH-103575 2006-02-15 Violation of injection tubing/fitting requirements
1158239773 US-OH-104185 2006-09-14 Pits not liquid tight/Improper construction or use
1232631273 US-OH-106248 2009-01-22 Failure to monitor annulus pressure
1244637743 US-OH-106526 2009-06-10 Pollution/Contamination
1244637743 US-OH-106527 2009-06-10 Mechanical failure/contamination
1245762111 US-OH-106556 2009-06-23 Pollution/Contamination
1245762111 US-OH-106557 2009-06-23 Mechanical failure/contamination
1277818089 US-OH-107721 2010-06-29 Contamination at surface facility (permit after 6-1-82)
1277818089 US-OH-107722 2010-06-29 Tanks not liquid tight/Improper burial
1522166093 US-OH-114486 2018-10-12 9-3-04(A) Pollution/Contamination
1592419846 US-OH-115463 2003-05-29 Mechanical failure/contamination
1592419846 US-OH-115464 2003-05-29 Pits not liquid tight/Improper construction or use
1596671949 US-OH-115626 2013-04-03 Violation of injection tubing/fitting requirements
1777720954 US-OH-117716 2007-07-23 Pollution/Contamination
1842046913 US-OH-118404 2010-03-25 Mechanical failure/contamination
iTOMK00009 US-OH-131633 Failure to monitor pressures/volumes

For data sources see[5]

References