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34-115-24449

Well Details

Well ID: 34-115-24449
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Country: United States
State: Ohio
County: Athens
Municipality: Bern Township
Operator Name: MURPHY OIL COMPANY INC
Well Pad ID:
Farm/Lease Name: CARNES
License Status: Producing
License Date: 1999-11-19
Spud Date: 1998-03-05
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1998-03-09
Well Total Depth: 1075.00 ft
Configuration: Vertical
Latitude: 39.450000
Longitude: -81.870000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 1998-02-09 4350 CENTURY WELL SERVICE Proposed Formation COW RUN/MAXTON/KEENER/BEREA Issued Date 2/9/98 Expired Date 2/9/99 6:00:00 AM
Original Spud 1998-03-05 RBDMS Rec
Correction to Well 1998-03-06 CORRECTION IN WELL NUMBER FROM #490 TO #491.
Completed 1998-03-09 RBDMS Rec
Reached Total Depth 1998-03-09 RBDMS Rec
Completion Report Received 1998-05-08 RBDMS Rec
Change of Owner 1998-10-14 Operator changed from 4350, CENTURY WELL SERVICE to 2348, TRIAD RESOURCES INC
APP 1999-11-19 Proposed Formations:MAXTON (BIG INJUN), Issued Date:11/19/99, Expired Date:11/18/2000 6:00:00 AM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2000-11-18 RBDMS Rec
Change of Owner 2009-05-28 Operator changed from 2348, TRIAD RESOURCES INC to 4350, CENTURY WELL SERVICE
Change of Owner 2015-04-28 Operator changed from 4350, CENTURY WELL SERVICE to 516, MURPHY OIL COMPANY INC - WELL NOT TRANSFERRED ON TRANSFER PROCESSED ON 4/26/2006 FROM CENTURY WELL SERVICE TO MURPHY OIL COMPANY INC. TRANSFER STATED THAT THE WELL WAS MARKED OFF BECAUSE IT BELONGED TO TRIAD RESOURCES, INC. HOWEVER, TRIAD RESOURCES, INC. TRANSFERRED THIS WELL TO CENTURY WELL SERVICES INC. ON 4/26/2000. SO THE WELL SHOULD HAVE BEEN TRANSFERRED TO MURPHY OIL COMPANY INC. PLEASE SEE FILE FOR BOTH TRANSFERS 4/28/2015 CM.
Record Last Modified 2017-02-15 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1998-07-30 846 854 17
846 854 17
846 854 17

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 20 550 Gal 0 500 GALLONS FE ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 TRIAD RESOURCES INC 0.00 0.00 365
2003 TRIAD RESOURCES INC 0.00 0.00 365
2004 TRIAD RESOURCES INC 0.00 0.00 365
2005 TRIAD RESOURCES INC 0.00 0.00 365
2016 MURPHY OIL COMPANY INC 0.00 0.00 0
2017 MURPHY OIL COMPANY INC 0.00 0.00 0
2018 MURPHY OIL COMPANY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 TRIAD RESOURCES INC Brine 0 365
2003 TRIAD RESOURCES INC Brine 0 365
2004 TRIAD RESOURCES INC Brine 0 365
2005 TRIAD RESOURCES INC Brine 0 365
2016 MURPHY OIL COMPANY INC Brine 0 0
2017 MURPHY OIL COMPANY INC Brine 0 0
2018 MURPHY OIL COMPANY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1224517527 2009-5-13 0:00: DD No Violations
-1854616000 2015-5-1 0:00:0 PW No Violations 1.00
-621483086 2009-7-27 0:00: PW No Violations
0621483086 2009-07-27 Production Wells No Violations Follow-up on NOV, In-Compliance.
1224517527 2009-05-13 Drill / Deepen / Reopen Violations Noted An inspection of the well revealed no ID at the well or tank battery.
1325805674 2012-01-05 Production Wells No Violations Request by landowner, Shirley Carnes, to determine if wells are producing - she has not been paid in years, if ever. Says Logan Gas is the owner. This day found well with jack, valves open on well, IDs on tank, poor dike. Shirleys brother on location, says this well has not produced in years. No production has been turned in, records show Triad last produced well and well needs transferred into Logan Gass name - Century no longer in business. Shirley is trying to break lease - will not request NOV until time that well needs plugged. Talked with Logan Gas and they said wells had been producing, have a blockage in the gas line that has not been fixed. This day found no meter showing any gas sales.
1854616000 2015-05-01 Production Wells No Violations I was at this well it do a follow-up inspection on it. The well is currently idle and not capable of production. There are no production lines hooked up to the well. The valves at the well are shut at this time. The well is still in violation.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1224517527 US-OH-105840 2009-05-20 Failure to legibly identify well

For data sources see[9]

References