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34-115-24656

Well Details

Well ID: 34-115-24656
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield Township
Operator Name: R C POLING CO INC
Well Pad ID:
Farm/Lease Name: WEAVER
License Status: Final Restoration
License Date: 2010-06-18
Spud Date: 2010-06-28
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2010-07-02
Well Total Depth: 1367.00 ft
Configuration: Vertical
Latitude: 39.680000
Longitude: -82.010000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2010-06-18 Proposed Formations:BEREA/KNOX (MAY NOT PRODUCE CLINTON), Issued Date:6/18/2010, Expired Date:6/18/2011 6:00:00 AM, Drilling unit acres:70, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2010-07-02 LOST HOLE WHILE CEMENTING SURFACE PIPE. WILL P&A AND SKID TO DRILL NEW WELL.
Reached Total Depth 2010-07-02 LOST HOLE WHILE CEMENTING SURFACE PIPE. WILL P&A AND SKID TO DRILL NEW WELL.
Completion Report Received 2010-07-13 LOST HOLE WHILE CEMENTING SURFACE PIPE. WILL P&A AND SKID TO DRILL NEW WELL.
Correction to Well 2010-07-16 UNIT SIZE DECREASED TO 40 ACRES.
Construction Permit Expires 2011-06-18 LOST HOLE WHILE CEMENTING SURFACE PIPE. WILL P&A AND SKID TO DRILL NEW WELL.
Record Last Modified 2013-03-14 LOST HOLE WHILE CEMENTING SURFACE PIPE. WILL P&A AND SKID TO DRILL NEW WELL.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-111717830 2010-6-30 0:00: DD No Violations 4.00
-1268830470 2010-7-6 0:00:0 DD No Violations
-1641412110 2010-6-25 0:00: DD No Violations 1.00
0111717830 2010-06-30 Drill / Deepen / Reopen No Violations Surface job, ran 1367ft of used 8 5/8 casing, while pumping cement casing parted and cement balanced in well bore and outside casing.
0320757145 2010-07-01 Plug / Plug Back No Violations Plugged well and well bore from 809ft to surface, set plugs from 809ft to 509ft and 300ft to surface.
0884576307 2010-07-01 Drill / Deepen / Reopen No Violations Company ran a Bond log on well, log went down to 809ft, well bore and inside of casing cemented off at that point. Casing had parted at approx. 802ft. Tried pulling 8 5/8 casing, removed 90ft of casing from well. Company has chosen to skid rig and plug well, ran in drill pipe to 790ft, to start plugging of well.
0974004949 2011-06-30 Final Restoration No Violations Inspection this day found well, old plugged well nearby. Location still needs more work to say it is reclaimed, ground has been smoothed, pits filled in, only need grass sown. I am passing FRD as will be taken care of when PRD for 4657 is complete.
1268830470 2010-07-06 Drill / Deepen / Reopen No Violations Witnessed BOP test for Dan Goins. The BOP passed the required test.
1641412110 2010-06-25 Drill / Deepen / Reopen No Violations Drlg rig moving in to start drlg.
320757145 2010-7-1 0:00:0 PB No Violations 4.00
884576307 2010-7-1 0:00:0 DD No Violations 8.00
974004949 2011-6-30 0:00: FR No Violations 0.50

For data sources see[3]

References