X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-117-21369

Well Details

Well ID: 34-117-21369
Loading map...
Country: United States
State: Ohio
County: Morrow
Municipality: Cardington Township
Operator Name: FISHBURN PRODUCING INC
Well Pad ID:
Farm/Lease Name: LEE H & M
License Status: Producing
License Date: 1981-03-28
Spud Date: 1900-01-01
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth: 3166.00 ft
Configuration: Vertical
Latitude: 40.540000
Longitude: -82.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-03-28 176 ASHLAND EXPLORATION INC GeoDate 3/28/81
CO 1991-08-21 3941 FISHBURN PRODUCING INC GeoDate 3/28/81
Record Last Modified 2015-09-24 GL=1010.3

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2980 3002 0
2980 3002 0
2980 3002 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 1000 Gal 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC 0.00 2090.00 365
1985 ASHLAND EXPLORATION INC 0.00 1393.00 0
1986 ASHLAND EXPLORATION INC 0.00 1320.00 365
1992 FISHBURN PRODUCING INC 0.00 1086.00 355
1993 FISHBURN PRODUCING INC 0.00 839.00 350
1994 FISHBURN PRODUCING INC 0.00 603.00 254
1995 FISHBURN PRODUCING INC 0.00 670.00 325
1996 FISHBURN PRODUCING INC 0.00 352.00 240
1997 FISHBURN PRODUCING INC 0.00 676.00 175
1998 FISHBURN PRODUCING INC 0.00 709.00 301
1999 FISHBURN PRODUCING INC 0.00 0.00 0
2000 FISHBURN PRODUCING INC 0.00 960.00 156
2001 FISHBURN PRODUCING INC 0.00 839.00 195
2002 FISHBURN PRODUCING INC 0.00 1093.00 198
2003 FISHBURN PRODUCING INC 0.00 1003.00 194
2004 FISHBURN PRODUCING INC 0.00 445.00 242
2005 FISHBURN PRODUCING INC 0.00 516.00 302
2006 FISHBURN PRODUCING INC 0.00 540.00 265
2007 FISHBURN PRODUCING INC 0.00 533.00 185
2009 FISHBURN PRODUCING INC 0.00 361.00 284
2010 FISHBURN PRODUCING INC 0.00 718.00 239
2011 FISHBURN PRODUCING INC 0.00 365.00 93
2012 FISHBURN PRODUCING INC 0.00 357.00 214
2013 FISHBURN PRODUCING INC 0.00 521.00 287
2014 FISHBURN PRODUCING INC 0.00 347.00 205
2015 FISHBURN PRODUCING INC 0.00 173.00 163
2016 FISHBURN PRODUCING INC 0.00 353.00 259
2017 FISHBURN PRODUCING INC 0.00 350.00 233
2018 FISHBURN PRODUCING INC 0.00 155.00 70

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ASHLAND EXPLORATION INC Brine 0 365
1985 ASHLAND EXPLORATION INC Brine 757 0
1986 ASHLAND EXPLORATION INC Brine 1416 365
1992 FISHBURN PRODUCING INC Brine 975 355
1993 FISHBURN PRODUCING INC Brine 1015 350
1994 FISHBURN PRODUCING INC Brine 872 254
1995 FISHBURN PRODUCING INC Brine 558 325
1996 FISHBURN PRODUCING INC Brine 228 240
1997 FISHBURN PRODUCING INC Brine 223 175
1998 FISHBURN PRODUCING INC Brine 125 301
1999 FISHBURN PRODUCING INC Brine 0 0
2000 FISHBURN PRODUCING INC Brine 574 156
2001 FISHBURN PRODUCING INC Brine 1498 195
2002 FISHBURN PRODUCING INC Brine 2630 198
2003 FISHBURN PRODUCING INC Brine 2010 194
2004 FISHBURN PRODUCING INC Brine 3255 242
2005 FISHBURN PRODUCING INC Brine 3655 302
2006 FISHBURN PRODUCING INC Brine 2340 265
2007 FISHBURN PRODUCING INC Brine 1742 185
2009 FISHBURN PRODUCING INC Brine 2805 284
2010 FISHBURN PRODUCING INC Brine 2240 239
2011 FISHBURN PRODUCING INC Brine 1495 93
2012 FISHBURN PRODUCING INC Brine 2440 214
2013 FISHBURN PRODUCING INC Brine 2985 287
2014 FISHBURN PRODUCING INC Brine 1745 205
2015 FISHBURN PRODUCING INC Brine 1560 163
2016 FISHBURN PRODUCING INC Brine 2255 259
2017 FISHBURN PRODUCING INC Brine 1845 233
2018 FISHBURN PRODUCING INC Brine 1940 70

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1237437002 2015-7-9 0:00:0 SC No Violations
-150920001 2020-2-13 0:00: PW No Violations 0.50
-1725316508 2007-2-20 0:00: PW No Violations
-1795762086 2003-4-23 0:00: PW No Violations
-1971103290 2018-1-9 0:00:0 PW No Violations
-349722163 2019-5-2 0:00:0 PW No Violations
-689332533 2020-4-20 0:00: PW No Violations
-923242134 2017-11-15 0:00 PW No Violations
-995385806 2018-3-2 0:00:0 PW No Violations
0000PL9191 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0069277590 2006-01-05 Production Wells No Violations Chk well and storage, Ok.
0130545831 2018-01-03 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
0246116305 2015-02-02 Production Wells No Violations Location Information for the H K Lee #2 (#1369). WELL HEAD: Lat. 40.54812 Long. -82.90259 / CENTER-OF-STORAGE: Lat. 40.55182 Long. -82.90218 / ENTRANCE: Lat. 40.54867 Long. -82.90052.
0349722163 2019-05-02 Production Wells No Violations Inspected the Lee #2 (#1369) as part of a standard production well status check. Inspect well, storage and identification. Status: no change-in-status from previous inspection.
0396812105 2015-02-11 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over.
0663185661 2018-02-05 Production Wells No Violations Inspected the Lee #2 (#1369) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection.
0780269839 2017-08-31 Production Wells No Violations The operator has replaced the pumping jack and placed the well back into production.
0871114831 2018-03-08 Work Over Reconditioning No Violations Fishburn service rig is on the well for work over. Currently rigging up. Status: ok.
0897247142 2017-07-06 Production Wells No Violations Inspect well, storage and identification. The operator has removed the pump jack from the well for repair. A 2 inch nipple on the tubing backside was missing a bull plug and venting gas, met with the well tender who installed a ball valve. Status: ok, added location directions.
0923242134 2017-11-15 Production Wells No Violations Inspect well, storage and identification. Status: ok, the well was pumping at the time of inspection.
0970485182 2015-02-02 Production Wells No Violations Inspected the H K Lee #1 (#1369) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
0995385806 2018-03-02 Production Wells No Violations Inspected the Lee #2 (#1369) as part of a standard production well status check. Inspect well, storage and identification. Status: ok.
1084368501 2004-05-12 Production Wells No Violations Chl well and storage, Ok.
1237437002 2015-07-09 Surface Facility Construction No Violations The operator has constructed a new storage facility consisting of a single 210 barrel tank set in a gravel lined dike - moved closer to the well. New storage coordinates Lat: 40.54873 Long: -82.90321.
130545831 2018-1-3 0:00:0 WR No Violations
1359998615 2013-02-04 Production Wells No Violations Inspected the Lee #2 (#1369) as part of a standard productive well status check. The well is pumping by a black USS oilwell electric powered pump jack. The storage consists of two tanks and a vertical separator set on gravel. The well identification and emergency contact information is clearly marked at the storage and the well. The site is currently snow covered and no trespassing signs are posted. Status: Ok.
1370893352 2019-10-23 0:00 WR No Violations
1395079152 2014-03-14 Work Over Reconditioning No Violations Fishburn service rig has moved on the well for workover.
1570736336 2019-10-7 0:00: WR No Violations
1596180716 2020-8-25 0:00: PW No Violations
1725316508 2007-02-20 Production Wells No Violations Inspect well location. Well in production. Site ok.
1795762086 2003-04-23 Production Wells No Violations Chk well and storage. Shows sibns of recent service, new gravel put down around the well head.
1922158886 2017-07-26 Production Wells No Violations The operator has delivered two loads of stone to the well in preparation of setting the pump jack.
1971103290 2018-01-09 Production Wells No Violations The operator has placed the well back into production. Status: ok.
20018485 2019-12-5 0:00: PW No Violations 0.40
2006535593 2018-07-17 Work Over Reconditioning No Violations Fishburn Service rig is on the well for workover. Rods and tubing are pulled. The operator reported they are attempting to locate a possible hole in the production casing.
2026309423 2018-12-04 Production Wells No Violations Inspected the Lee #2 (#1369) as part of a standard production well status check. Fishburn has moved off the well without placing the well back into production.
246116305 2015-2-2 0:00:0 PW No Violations
396812105 2015-2-11 0:00: WR No Violations
663185661 2018-2-5 0:00:0 PW No Violations
69277590 2006-1-5 0:00:0 PW No Violations
780269839 2017-8-31 0:00: PW No Violations
871114831 2018-3-8 0:00:0 WR No Violations
897247142 2017-7-6 0:00:0 PW No Violations
970485182 2015-2-2 0:00:0 PW No Violations
PL9191 PL No Violations

For data sources see[9]

References