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34-119-23624

Well Details

Well ID: 34-119-23624
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: MATTINGLY FOOD INC.
Well Pad ID:
Farm/Lease Name: RITTBERGER CC & B & ORR COMPANY
License Status: Producing
License Date: 1975-09-15
Spud Date: 1975-09-22
Spud Drilling Contractor: GRATIOT DRLG
Final Drill Date: 1975-10-27
Well Total Depth: 3590.00 ft
Configuration: Vertical
Latitude: 39.940000
Longitude: -82.020000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1975-09-22 N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID
Completed 1975-10-27 N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID
Reached Total Depth 1975-10-27 N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID
Completion Report Received 1975-11-19 N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID
Change of Owner 1999-06-11 Operator changed from 736, RITTBERGER CARL SR INC to 6490, MATTINGLY FOOD INC.
Record Last Modified 2017-02-15 N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 15 210000 Gal 24000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CARL RITTBERGER SR INC 439.00 61.00 0
1985 CARL RITTBERGER SR INC 0.00 0.00 0
1986 CARL RITTBERGER SR INC 0.00 0.00 365
2014 MATTINGLY FOOD INC. 500.00 0.00 147
2016 MATTINGLY FOOD INC. 0.00 0.00 28

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CARL RITTBERGER SR INC Brine 0 0
1985 CARL RITTBERGER SR INC Brine 0 0
1986 CARL RITTBERGER SR INC Brine 0 365
2014 MATTINGLY FOOD INC. Brine 0 147
2016 MATTINGLY FOOD INC. Brine 0 28

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1325726420 2018-1-29 0:00: PW No Violations 1.50
-1652395455 2018-1-2 0:00:0 PW No Violations 0.70
-274547287 2017-12-15 0:00 PW No Violations 0.40
-328404365 2017-2-9 0:00:0 PW No Violations 1.00
-41634547 2019-2-5 0:00:0 PW No Violations 0.70
0015230415 2019-02-13 Production Wells No Violations The inspection is due to multiple Compliance Notices (Identification, Plug well, Well leaking gas, Bull plugs.) The well is equipped with a pumping unit, electric motor, tubing head and the valves are all closed. The well is needing bull plugs and is still leaking gas. There is no associated tank site. The company has failed to respond on the leaking gas issue and show the capabilities of producing gas. Identification was at well and is missing again. I talked to the Cara Dodson in the Corporate office and she had Shane Girton get in touch with me. Shane called and stated that he had two people working on the gas problem. I stated to Shane you have to get into compliance with the well. Show numbers, post identification, fix gas leak and install bull plugs.
0041634547 2019-02-05 Production Wells Violations Noted The purpose of my inspection is due to Compliance Notice follow-up to inspection number 320871078 (well shall be plugged and failure to identify). The well is venting gas into the atmosphere. It is equipped with a partially buried well head, 5 1/2 inch diameter casing, tubing head with 2 3/8 inch diameter tubing and a pumping unit equipped complete with electric motor and belts. Identification is still not posted at the well and still shut-in. Last reported production in RBDMS was 2014. The company has 1 day to fix the leaking well and place into production. The company has 10 days to get the identification posted permanently.
0274547287 2017-12-15 Production Wells No Violations The purpose of my inspection is due to Chiefs Order Follow-up to number 2016-
0320871078 2017-07-27 Production Wells Violations Noted On the day of my inspection the well is idle and shut in. There are no lines hooked up to the well or tanks. The well is equipped with a pumping unit, 7diameter casing, 5.5diameter casing, tubing head and 2.375diameter tubing. The production manifold is closed in at the rod and tubing annulus. There is an electric motor with belts intact. There is no identification at the well. Shane Girton with Mattingly stopped by and I explained that they will be receiving Compliance Notice on the well. The well owner /operator shall submit a written plugging schedule to Patrick Shreve at 5880 Memory Rd. Zanesville, Ohio 43701 within 30 days per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
0328404365 2017-02-09 Production Wells No Violations

-

0786167471 2019-02-20 Production Wells No Violations The inspection is a Compliance Notice Follow-up to number 320871078 and -41634547 respectively. The inspection revealed that the well is equipped with an Alten pumping unit, electric motor, tubing head and 2 3/8-
1325726420 2018-01-29 Production Wells No Violations The purpose of my inspection is due to Chiefs Order Follow-up 2016-222 and Compliance Notice Follow-up to number 320871078. I stopped at the well and talked to Shane Girton. He stated that they are in the process of taking care of Insurance issue to clear up the Chiefs Order. I stated that after the insurance issue is fixed then I need to verify the gas with the well. If there is no capabilities then have a plug permit issued and will work out an arrangement for time of plugging. I talked to Bill Grubaugh on this matter. He will let me know when they have Insurance.
1490708034 2017-03-27 Production Wells No Violations On the day of my inspection the well is currently shut in. I talked to a Shane Girton the Facility Director. He stated that the well will not keep up with the current gas pressure to supply gas. I gave him some contacts to call for plugging the well. The well currently does not have identification (id) at the well head. There are no tanks. There is an Alten pumping unit that is series 40. Shane will install an id at the well.
1496814247 2017-11-17 Production Wells No Violations

-up to number 2016-

15230415 2019-2-13 0:00: PW No Violations 0.50
1524489396 2018-04-23 Production Wells No Violations The ground conditions are clear and dry at 55 degrees Fahrenheit. The purpose of the inspection is due to Compliance Notice follow-
1652395455 2018-01-02 Production Wells No Violations The purpose of my inspection is due to a Chiefs Order follow-up to 2016-222. The well is currently idle and the production valves are closed. There is a pumping unit and an electric motor on the unit. The identification is posted at the well.
320871078 2017-7-27 0:00: PW No Violations 1.00
786167471 2019-2-20 0:00: PW No Violations 0.70

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0041634547 US-OH-124429 2019-05-14 9-9-05(A)1 Well insufficiently equipped to prevent escape of oil and gas
0320871078 US-OH-123339 2017-08-25 Failure to legibly identify well
0320871078 US-OH-123340 2017-08-25 Well shall be plugged

For data sources see[8]

References