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Well ID: 34-119-23624 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: MATTINGLY FOOD INC. | |
Well Pad ID: | |
Farm/Lease Name: RITTBERGER CC & B & ORR COMPANY | |
License Status: Producing | |
License Date: 1975-09-15 | |
Spud Date: 1975-09-22 | |
Spud Drilling Contractor: GRATIOT DRLG | |
Final Drill Date: 1975-10-27 | |
Well Total Depth: 3590.00 ft | |
Configuration: Vertical | |
Latitude: 39.940000 | |
Longitude: -82.020000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1975-09-22 | N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID |
Completed | 1975-10-27 | N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID |
Reached Total Depth | 1975-10-27 | N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID |
Completion Report Received | 1975-11-19 | N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID |
Change of Owner | 1999-06-11 | Operator changed from 736, RITTBERGER CARL SR INC to 6490, MATTINGLY FOOD INC. |
Record Last Modified | 2017-02-15 | N.L. F/W 5000BW, 240 SKS. SAND & 200 GAL. ACID |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 15 | 210000 Gal | 24000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CARL RITTBERGER SR INC | 439.00 | 61.00 | 0 |
1985 | CARL RITTBERGER SR INC | 0.00 | 0.00 | 0 |
1986 | CARL RITTBERGER SR INC | 0.00 | 0.00 | 365 |
2014 | MATTINGLY FOOD INC. | 500.00 | 0.00 | 147 |
2016 | MATTINGLY FOOD INC. | 0.00 | 0.00 | 28 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CARL RITTBERGER SR INC | Brine | 0 | 0 |
1985 | CARL RITTBERGER SR INC | Brine | 0 | 0 |
1986 | CARL RITTBERGER SR INC | Brine | 0 | 365 |
2014 | MATTINGLY FOOD INC. | Brine | 0 | 147 |
2016 | MATTINGLY FOOD INC. | Brine | 0 | 28 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1325726420 | 2018-1-29 0:00: | PW | No Violations | 1.50 |
-1652395455 | 2018-1-2 0:00:0 | PW | No Violations | 0.70 |
-274547287 | 2017-12-15 0:00 | PW | No Violations | 0.40 |
-328404365 | 2017-2-9 0:00:0 | PW | No Violations | 1.00 |
-41634547 | 2019-2-5 0:00:0 | PW | No Violations | 0.70 |
0015230415 | 2019-02-13 | Production Wells | No Violations | The inspection is due to multiple Compliance Notices (Identification, Plug well, Well leaking gas, Bull plugs.) The well is equipped with a pumping unit, electric motor, tubing head and the valves are all closed. The well is needing bull plugs and is still leaking gas. There is no associated tank site. The company has failed to respond on the leaking gas issue and show the capabilities of producing gas. Identification was at well and is missing again. I talked to the Cara Dodson in the Corporate office and she had Shane Girton get in touch with me. Shane called and stated that he had two people working on the gas problem. I stated to Shane you have to get into compliance with the well. Show numbers, post identification, fix gas leak and install bull plugs. |
0041634547 | 2019-02-05 | Production Wells | Violations Noted | The purpose of my inspection is due to Compliance Notice follow-up to inspection number 320871078 (well shall be plugged and failure to identify). The well is venting gas into the atmosphere. It is equipped with a partially buried well head, 5 1/2 inch diameter casing, tubing head with 2 3/8 inch diameter tubing and a pumping unit equipped complete with electric motor and belts. Identification is still not posted at the well and still shut-in. Last reported production in RBDMS was 2014. The company has 1 day to fix the leaking well and place into production. The company has 10 days to get the identification posted permanently. |
0274547287 | 2017-12-15 | Production Wells | No Violations | The purpose of my inspection is due to Chiefs Order Follow-up to number 2016- |
0320871078 | 2017-07-27 | Production Wells | Violations Noted | On the day of my inspection the well is idle and shut in. There are no lines hooked up to the well or tanks. The well is equipped with a pumping unit, 7diameter casing, 5.5diameter casing, tubing head and 2.375diameter tubing. The production manifold is closed in at the rod and tubing annulus. There is an electric motor with belts intact. There is no identification at the well. Shane Girton with Mattingly stopped by and I explained that they will be receiving Compliance Notice on the well. The well owner /operator shall submit a written plugging schedule to Patrick Shreve at 5880 Memory Rd. Zanesville, Ohio 43701 within 30 days per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
0328404365 | 2017-02-09 | Production Wells | No Violations
- | |
0786167471 | 2019-02-20 | Production Wells | No Violations | The inspection is a Compliance Notice Follow-up to number 320871078 and -41634547 respectively. The inspection revealed that the well is equipped with an Alten pumping unit, electric motor, tubing head and 2 3/8- |
1325726420 | 2018-01-29 | Production Wells | No Violations | The purpose of my inspection is due to Chiefs Order Follow-up 2016-222 and Compliance Notice Follow-up to number 320871078. I stopped at the well and talked to Shane Girton. He stated that they are in the process of taking care of Insurance issue to clear up the Chiefs Order. I stated that after the insurance issue is fixed then I need to verify the gas with the well. If there is no capabilities then have a plug permit issued and will work out an arrangement for time of plugging. I talked to Bill Grubaugh on this matter. He will let me know when they have Insurance. |
1490708034 | 2017-03-27 | Production Wells | No Violations | On the day of my inspection the well is currently shut in. I talked to a Shane Girton the Facility Director. He stated that the well will not keep up with the current gas pressure to supply gas. I gave him some contacts to call for plugging the well. The well currently does not have identification (id) at the well head. There are no tanks. There is an Alten pumping unit that is series 40. Shane will install an id at the well. |
1496814247 | 2017-11-17 | Production Wells | No Violations
-up to number 2016- | |
15230415 | 2019-2-13 0:00: | PW | No Violations | 0.50 |
1524489396 | 2018-04-23 | Production Wells | No Violations | The ground conditions are clear and dry at 55 degrees Fahrenheit. The purpose of the inspection is due to Compliance Notice follow- |
1652395455 | 2018-01-02 | Production Wells | No Violations | The purpose of my inspection is due to a Chiefs Order follow-up to 2016-222. The well is currently idle and the production valves are closed. There is a pumping unit and an electric motor on the unit. The identification is posted at the well. |
320871078 | 2017-7-27 0:00: | PW | No Violations | 1.00 |
786167471 | 2019-2-20 0:00: | PW | No Violations | 0.70 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0041634547 | US-OH-124429 | 2019-05-14 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
0320871078 | US-OH-123339 | 2017-08-25 | Failure to legibly identify well | |
0320871078 | US-OH-123340 | 2017-08-25 | Well shall be plugged |
For data sources see[8]