X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-145-60170

Well Details

Well ID: 34-145-60170
Loading map...
Country: United States
State: Ohio
County: Scioto
Municipality: Madison Township
Operator Name: ODOT DISTRICT 9
Well Pad ID:
Farm/Lease Name: ODOT
License Status: Final Restoration
License Date:
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 38.860000
Longitude: -82.900000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Well Added to System 2011-04-07 WELL WAS ADDED TO SYSTEM ON 4/7/2011 9:37:31 AM
Change of Owner 2015-08-04 Operator changed from 9998, HISTORIC OWNER to 9518, ODOT DISTRICT 9
Plugged/Abandoned 2015-08-20 WELL INSPECTED BY JON SCOTT, 3/16/2011 AFTER NOTIFICATION BY ODOT OF WELL BEING FOUND AT A HOUSE THAT WAS PURCHASED FOR PORTSMOUTH BYPASS. THE WELL IS ENCLOSED IN A WOODEN STRUCTURE 20" WIDE BY 60" LONG BY 51" TALL. WELL CONSTRUCTION, 5" CASING THAT IS 7" ABOVE GROUND LEVEL, A HOME MADE 5"BY 2" SWEDGE WITH A 2" TEE LOCATED 22" ABOVE GROUND. THERE IS A 2" BY 1" BUSHING, 1" VALVE (SHUT), AT TOP OF 2" TEE THERE IS A 2" BY 3/8" BUSHING, 3/8" NIPPLE WITH 3/8" BY 1/2"BUSHING, 1/2" VALVE; 1/2" BY 3/8" BUSHING, 3/8" NIPPLE, 3/8" 90 ELL, 3/8" BY 1/4" REDUCING COUPLING AND GAUGE. WELL IS LOCATED 11' FROM SIDE OF HOUSE, 17' FROM SIDE OF GARAGE, AND 63' FROM BLUE RUN ROAD. THE WELL IS PLUMBED FOR DOMESTIC USE AND NO PRODUCTION LINES WERE SEEN DURING INSPECTION.
Record Last Modified 2019-06-14 WELL INSPECTED BY JON SCOTT, 3/16/2011 AFTER NOTIFICATION BY ODOT OF WELL BEING FOUND AT A HOUSE THAT WAS PURCHASED FOR PORTSMOUTH BYPASS. THE WELL IS ENCLOSED IN A WOODEN STRUCTURE 20" WIDE BY 60" LONG BY 51" TALL. WELL CONSTRUCTION, 5" CASING THAT IS 7" ABOVE GROUND LEVEL, A HOME MADE 5"BY 2" SWEDGE WITH A 2" TEE LOCATED 22" ABOVE GROUND. THERE IS A 2" BY 1" BUSHING, 1" VALVE (SHUT), AT TOP OF 2" TEE THERE IS A 2" BY 3/8" BUSHING, 3/8" NIPPLE WITH 3/8" BY 1/2"BUSHING, 1/2" VALVE; 1/2" BY 3/8" BUSHING, 3/8" NIPPLE, 3/8" 90 ELL, 3/8" BY 1/4" REDUCING COUPLING AND GAUGE. WELL IS LOCATED 11' FROM SIDE OF HOUSE, 17' FROM SIDE OF GARAGE, AND 63' FROM BLUE RUN ROAD. THE WELL IS PLUMBED FOR DOMESTIC USE AND NO PRODUCTION LINES WERE SEEN DURING INSPECTION.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1061341749 2015-3-24 0:00: PW No Violations 0.30
-423375178 2015-8-13 0:00: PB No Violations 3.70
0059033408 2015-08-20 Plug / Plug Back No Violations Returned with Formation Cementing to top off hole. Cement top was tagged with a plub bob and verified at 25 feet previously. Fluid level checked and 6 gallons of Class A cement were batch mixed and grouted from the surface.
0293000331 2016-03-10 Final Restoration No Violations On my inspection I found that the location had been restored according to 1509.072. I passed the final restoration at this time.
0423375178 2015-08-13 Plug / Plug Back No Violations Witnessed plugging operations. Wireline ran to 398 to verify TD. Freepoint along backside of 2 7/8 casing verified with a VDL log to be 150 feet. There also appears to be 50 feet of cement showing on the bond from the surface down that was poured around the 2 7/8 casing in conjuction with the large concrete pad around the well site. After having the company dig out around the casing and down roughly 4 feet, I was unable to locate any surface casing. The 2 7/8 casing was shot at 57 with a casing cutter, 1 tubing was ran to TD and 35 sacks of Class A cement were circulated to surface to fill the casing and the void from 150-50 feet. Fluid circulation came from inside the 2 7/8 casing and not up the backside. Fluid depth was roughly 50 feet after the 1 tubing was pulled and the well will be tipped off at a later date.
0705799157 2014-08-14 Production Wells No Violations Well has been painted yellow. Accompanied by Inspector Kip Thompson. No gas leaks were observed.
0727396245 2015-04-01 Production Wells No Violations I met with Josh Garland on well on a well that will bidded out for plugging by ODOT and revealed the following : There was 4.5casing incased with cement or a drip with 2welded to the top. There was 2tubing and a 2tee with a 3/4tap@ the top in a 2plug. There is a concrete pad around the well.
0948609019 2015-08-18 Plug / Plug Back No Violations Verified cement top at 25 feet inside 2 7/8 casing with a small wireline.
1061341749 2015-03-24 Production Wells No Violations Met with company representative and DOT representative to discuss plugging options for the well as part of a package to put in Portsmouth Bi-pass. 2 tubing visible at surface and a large concrete pad has been poured around the well head, there is also a cement cast wrapped around the bottom 6-8 of the tubing that is roughly 4 in diameter.
1089327950 2014-08-14 Production Wells No Violations Inspector Jon Scott showed myself this well. It consists of a casing with a swage, and two valves. The well is not leaking.
1334839013 2012-04-04 Production Wells No Violations 697 Blue Run Road, ODOT Portsmouth bypass project. House and garage have been removed. Site is graded with vegetative growth established. Wellhead has been disconnected (with a plug installed) from house line and painted yellow.
1462898627 2015-08-12 Plug / Plug Back No Violations Review of well construction with Kilbargers and pulled roughly 250 feet of a 1/2 plastic line from well that was being used as tubing. The concrete cast around the tubing was broken off and the well was blewn down.
1944343281 2015-04-01 Production Wells No Violations Met with Pat Shreve to discuss plugging of well.
1951433540 2015-08-18 Plug / Plug Back No Violations I met with Dave White with Kilbarger, Josh Garland Oil and Gas Division on the plugging on the well. There was some discussion on perferation process on ODOT Wells.
2115213251 2015-08-27 Plug / Plug Back No Violations Kilbarger has dug down 30 and cut off the 2 7/8 tubing. The tubing has a Identification plate placed on top the cut off tubing.
293000331 2016-3-10 0:00: FR No Violations 1.50
59033408 2015-8-20 0:00: PB No Violations 0.70
705799157 2014-8-14 0:00: PW No Violations 1.50
727396245 2015-4-1 0:00:0 PW No Violations 1.00
948609019 2015-8-18 0:00: PB No Violations 2.50

For data sources see[3]

References