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34-153-20640

Well Details

Well ID: 34-153-20640
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: MOORE WELL SERVICES INC
Well Pad ID:
Farm/Lease Name: WALSH
License Status: Plugged and Abandoned
License Date: 2015-10-05
Spud Date: 1979-03-05
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1979-03-12
Well Total Depth: 3959.00 ft
Configuration: Vertical
Latitude: 41.180000
Longitude: -81.490000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-09-09 140 KST OIL & GAS CO INC GeoDate 9/9/78
Original Spud 1979-03-05
Completed 1979-03-12
Reached Total Depth 1979-03-12
Completion Report Received 1979-04-05
CO 1995-12-05 182 BELDEN & BLAKE CO GeoDate 9/9/78
Change of Owner 1997-06-23 Operator changed from 182, BELDEN & BLAKE CO to 5601, MOORE WELL SERVICES INC
APP 2010-07-08 Proposed Formations:CLINTON, Issued Date:7/8/2010, Expired Date:7/8/2011 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2015-10-05 Proposed Formations:CLINTON, Issued Date:10/5/2015, Expired Date:10/4/2017 12:00:00 PM, Drilling unit acres:24, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-08-24
Construction Permit Expires 2016-10-04
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-06-13 3747 3777 12
3747 3777 12
3747 3777 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 66000 Gal 80000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC 6996.00 117.00 365
1985 KST OIL & GAS CO INC 5552.00 68.00 365
1986 KST OIL & GAS CO INC 5512.00 137.00 82
1987 KST OIL & GAS CO INC 3246.00 89.00 365
1988 KST OIL & GAS CO INC 3280.00 49.00 365
1989 KST OIL & GAS CO INC 3140.00 62.00 365
1990 KST OIL & GAS CO INC 2534.00 75.00 365
1991 KST OIL & GAS CO INC 2228.00 37.00 365
1992 KST OIL & GAS CO INC 1661.00 25.00 365
1993 KST OIL & GAS CO INC 55.00 0.00 365
1994 KST OIL & GAS CO INC 0.00 0.00 0
1995 KST OIL & GAS CO INC 0.00 0.00 0
1997 MOORE WELL SERVICES INC 0.00 0.00 0
1998 MOORE WELL SERVICES INC 0.00 0.00 0
2000 MOORE WELL SERVICES INC 0.00 0.00 0
2001 MOORE WELL SERVICES INC 0.00 0.00 365
2002 MOORE WELL SERVICES INC 0.00 0.00 0
2003 MOORE WELL SERVICES INC 0.00 0.00 0
2004 MOORE WELL SERVICES INC 0.00 0.00 0
2005 MOORE WELL SERVICES INC 0.00 0.00 0
2006 MOORE WELL SERVICES INC 0.00 0.00 0
2007 MOORE WELL SERVICES INC 0.00 0.00 0
2008 MOORE WELL SERVICES INC 0.00 0.00 0
2009 MOORE WELL SERVICES INC 0.00 0.00 0
2010 MOORE WELL SERVICES INC 0.00 0.00 0
2011 MOORE WELL SERVICES INC 0.00 0.00 0
2012 MOORE WELL SERVICES INC 0.00 0.00 0
2013 MOORE WELL SERVICES INC 0.00 0.00 0
2014 MOORE WELL SERVICES INC 0.00 0.00 0
2016 MOORE WELL SERVICES INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 KST OIL & GAS CO INC Brine 0 365
1985 KST OIL & GAS CO INC Brine 139 365
1986 KST OIL & GAS CO INC Brine 324 82
1987 KST OIL & GAS CO INC Brine 197 365
1988 KST OIL & GAS CO INC Brine 196 365
1989 KST OIL & GAS CO INC Brine 280 365
1990 KST OIL & GAS CO INC Brine 303 365
1991 KST OIL & GAS CO INC Brine 269 365
1992 KST OIL & GAS CO INC Brine 42 365
1993 KST OIL & GAS CO INC Brine 11 365
1994 KST OIL & GAS CO INC Brine 30 0
1995 KST OIL & GAS CO INC Brine 0 0
1997 MOORE WELL SERVICES INC Brine 0 0
1998 MOORE WELL SERVICES INC Brine 0 0
2000 MOORE WELL SERVICES INC Brine 0 0
2001 MOORE WELL SERVICES INC Brine 0 365
2002 MOORE WELL SERVICES INC Brine 0 0
2003 MOORE WELL SERVICES INC Brine
2004 MOORE WELL SERVICES INC Brine 0 0
2005 MOORE WELL SERVICES INC Brine 0 0
2006 MOORE WELL SERVICES INC Brine 0 0
2007 MOORE WELL SERVICES INC Brine 0 0
2008 MOORE WELL SERVICES INC Brine 0 0
2009 MOORE WELL SERVICES INC Brine 0 0
2010 MOORE WELL SERVICES INC Brine 0 0
2011 MOORE WELL SERVICES INC Brine 0 0
2012 MOORE WELL SERVICES INC Brine 0 0
2013 MOORE WELL SERVICES INC Brine 0 0
2014 MOORE WELL SERVICES INC Brine 0 0
2016 MOORE WELL SERVICES INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1049978631 2009-3-31 0:00: PW No Violations
-962724667 2015-10-30 0:00 UP No Violations
0962724667 2015-10-30 UrbanProduction Wells No Violations I inspected the deconstruction of the tank battery for the Walsh Jesuit High School # 3 in preparation for the plugging of the Walsh # 3 well. The tank battery is a common tank battery with the Walsh # 2 and Walsh # 4 wells. The tank battery consisted of six(6) 100 barrel tanks, three (3) 50 barrel brine tanks, three (3) vertical separators and three (3) gas measurement stations.. Moore Well Service was the contractor for the tank battery removal. No violations were identified.
1049978631 2009-03-31 Production Wells No Violations I received a call from Dominion East Ohio reporting a natural gas leak on the north side of the Walsh Jesuit High School property. The leak was determined to be associated with the Walsh wells operated by Moore Well Service. Moore responded with personnel and equipment to expose and clamp the leaking line. The last reported production from this well was in 1993. I spoke with Jeff Moore about any plans for this well. He said that he would review the history but in all likelyhood, would plug and abandon in the near future.
1222294308 2017-07-27 Final Restoration No Violations I inspected the Walsh Jesuit High School # 3 for completion of final restoration. The area was graded and free from erosional features. There were two (2) area which needed to be reseeded. I spoke with Jeff Moore ( Moore Well Services ) and requested the area be reseeded and strawed. He agreed to do the work during the plugging and restoration of Walsh #4 & #2 wells. Walsh # 2 & # 4 wells are schedule to be plugged beginning the week of 31st of July. The service rig was over the Walsh # 2 well during my inspection. The Walsh # 3 location did not meet the final restoration criteria during this inspection.
1861538864 2016-08-09 UrbanProduction Wells No Violations I conducted a pre-plugging inspection of the Walsh Jesuit High School # 3 on 8/9/2016. Moore Well Services was on location to prep the well for P&A activity. The fencing surrounding the well head was removed. The scrub brush was removed and piled up for disposal. I requested that the 8.625 surface casing be exposed to check for any annular pressure. Once exposed the valve on the casing head was found to be opened. The tubing was found not to have any pressure. The 4.5 production casing was not checked due poor condition of the valves. No gas indication was observed around the outside of the 8.625 surface casing. No violation identified during this inspection.

For data sources see[9]

References