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34-153-23002

Well Details

Well ID: 34-153-23002
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: OHIO VALLEY ENERGY SYSTEMS COR
Well Pad ID:
Farm/Lease Name: SMITH C P
License Status: Producing
License Date: 2007-04-12
Spud Date: 2007-06-18
Spud Drilling Contractor: WILDCAT DRILLING
Final Drill Date: 2007-06-23
Well Total Depth: 4122.00 ft
Configuration: Directional
Latitude: 41.260000
Longitude: -81.440000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2007-04-12 Proposed Formations:OHIO SHALE THRU CLINTON, Issued Date:4/12/2007, Expired Date:4/11/2008 6:00:00 AM, Drilling unit acres:22.14, Proposed Well Type:OG, Proposed Well Class:POOL
Completed 2007-06-23
Reached Total Depth 2007-06-23
Completion Report Received 2007-08-24
Correction to Well 2007-09-14 CORRECTION TO TARGET INFORMATION: NEW FOOTAGE= 955'SL & 585'WL OF LOT 85; X= 2,289175 AND Y= 583,940. (SOURCE OF LOCATION: AS DRILLED SURVEY).
Construction Permit Expires 2008-04-11
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2007-11-29 3894 3937 72
3894 3937 72
3894 3937 72

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2667 Bbl 80000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2007 OHIO VALLEY ENERGY SYSTEMS COR 562.00 396.00 90
2008 OHIO VALLEY ENERGY SYSTEMS COR 11671.00 665.00 334
2009 OHIO VALLEY ENERGY SYSTEMS COR 6556.00 325.00 365
2010 OHIO VALLEY ENERGY SYSTEMS COR 4686.00 235.00 365
2011 OHIO VALLEY ENERGY SYSTEMS COR 3943.00 215.00 365
2012 OHIO VALLEY ENERGY SYSTEMS COR 3408.00 212.00 366
2013 OHIO VALLEY ENERGY SYSTEMS COR 2020.00 112.00 365
2014 OHIO VALLEY ENERGY SYSTEMS COR 1838.00 137.00 365
2015 OHIO VALLEY ENERGY SYSTEMS COR 1788.00 69.00 365
2016 OHIO VALLEY ENERGY SYSTEMS COR 208.00 0.00 60
2017 OHIO VALLEY ENERGY SYSTEMS COR 692.00 99.00 245
2018 OHIO VALLEY ENERGY SYSTEMS COR 1532.00 115.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2007 OHIO VALLEY ENERGY SYSTEMS COR Brine 3299 90
2008 OHIO VALLEY ENERGY SYSTEMS COR Brine 1031 334
2009 OHIO VALLEY ENERGY SYSTEMS COR Brine 491 365
2010 OHIO VALLEY ENERGY SYSTEMS COR Brine 499 365
2011 OHIO VALLEY ENERGY SYSTEMS COR Brine 511 365
2012 OHIO VALLEY ENERGY SYSTEMS COR Brine 427 366
2013 OHIO VALLEY ENERGY SYSTEMS COR Brine 344 365
2014 OHIO VALLEY ENERGY SYSTEMS COR Brine 570 365
2015 OHIO VALLEY ENERGY SYSTEMS COR Brine 531 365
2016 OHIO VALLEY ENERGY SYSTEMS COR Brine 65 60
2017 OHIO VALLEY ENERGY SYSTEMS COR Brine 235 245
2018 OHIO VALLEY ENERGY SYSTEMS COR Brine 269 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1248349435 2019-4-1 0:00:0 UP No Violations
-1631521310 2019-4-8 0:00:0 UP No Violations
-2013608556 2019-2-28 0:00: UP No Violations
-257825667 2008-1-9 0:00:0 PL No Violations
0257825667 2008-01-09 Preliminary Restoration No Violations Preliminary restoration is approved.
1248349435 2019-04-01 UrbanProduction Wells No Violations My inspection indicated that the interceptor dike and syphon dam were free of any oil and the surface of the water was frozen. Plan forward was to closed the syphon dam and interceptor ditch to allow access to the tank battery to load the tank pad gravel and dirt into lined dump truck for removal and disposal at Kimble Landfill in Dover. Then place the tank battery equipment back into the tank battery area and re-construct the tank battery.
1554739903 2019-03-27 UrbanProduction Wells No Violations I received a phone call from Don Nething ( OVE, 330.283.5758 ) to alert me that a two (2) inch valve had failed and allowed the contents of the 140 barrel stock tank to be emptied into the diked area of the tank battery. Mr. Nething indicated that the Incident Notification number was called to alert Emergency Response.The closing gauge on the tank indicated that approximately 79 barrels of fluid was spilled. The majority of the spill was contained within the diked feature, but a minor amount of fluid was found outside of containment. This fluid had traced the path of the oil load line through the dike and covered an area of 10 X 60 towards the west. Ohio Valley Energy mobilized excavation equipment to dig an interceptor ditch perpendicular to the flow and construct a reverse syphon dam for containment in anticipation of heavy rains expected that night. A low range QuanTab indicated 550 ppm Chlorides 70 west of the tank battery. The site was stabilized and operations were shut down overnight.
1570318570 2007-07-09 Drill / Deepen / Reopen No Violations The drilling pits have been solidified and closed. No violations at this time.
1631521310 2019-04-08 UrbanProduction Wells No Violations My inspection revealed that the equipment of the tank battery was placed in the tank battery area on fresh material. I did not see any indications of residual oil or contamination. The re - construction of the tank battery equipment was not complete at the time of my inspection. The disturbed area was rough graded, seeded and strawed in order to minimize erosion. Final landscaping will take place when favorable weather conditions occur per my conversation with Don Nething of OVE.
1686255593 2007-06-18 Drill / Deepen / Reopen No Violations Wildcat Drilling is on site and should spud the well later today. The pits are being dug. No violations at this time.
2013608556 2019-02-28 UrbanProduction Wells No Violations Personnel on location for the remediation included Daley Excavating, Swinehart Steaming Services and personnel from Ohio Valley Energy. DOGRM was represented ( at various times ) by Rob Leidy ( Radiation Group ) Andrew Adgate and Fred Romeo ( Emergency Response ) and Bob Roush ( Summit County DOGRM Inspector ). The tank battery equipment was dismantled and steamed clean of all contamination. An area of bermed containment was constructed on which one (1) 140 barrel stock tank, one (1) 35 barrel poly brine tank, one (1) 2408 horizontal separator and ancillary equipment was placed. An excavator stockpiled the tank pad gravel in order to steam the rock prior to removal. A vacuum truck worked inside the tank battery dike to remove the free liquids caused by the steaming procedure. The activity continued until approximately 5:00 pm when the threat of rain shut down the operations. OVE personnel decided to shut down over the wekend because of weather concerns. Site was secured.

For data sources see[9]

References