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34-153-23137

Well Details

Well ID: 34-153-23137
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Country: United States
State: Ohio
County: <County>
Municipality:
Operator Name: DOMINION EAST OHIO
Well Pad ID:
Farm/Lease Name: GLICK
License Status: Storage Well
License Date: 2011-06-07
Spud Date: 2011-12-03
Spud Drilling Contractor: KILBARGER DRLG
Final Drill Date: 2011-12-17
Well Total Depth: 4204.00 ft
Configuration: Vertical
Latitude: 40.940000
Longitude: -81.530000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2011-06-07 Proposed Formations:CLINTON, Issued Date:6/7/2011, Expired Date:6/6/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:SO, Proposed Well Class:STOR
Reached Total Depth 2011-12-17
Construction Permit Expires 2012-06-06
Completion Report Received 2013-11-12
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2013-11-15 4039 4060 60
4039 4060 60
4039 4060 60

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-01-25 H2O 15 57948 Gal 62400 Universal Well Services Inc.

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1061767981 2016-5-19 0:00: PL No Violations
-1097793910 2011-12-2 0:00: UD No Violations
-1098948624 2012-1-11 0:00: UD No Violations
-1297263145 2011-12-14 0:00 UD No Violations
-1379460900 2012-1-26 0:00: SO No Violations
-1532719012 2011-12-22 0:00 UD No Violations
-1893142174 2011-12-22 0:00 PB No Violations
-2009896275 2014-10-9 0:00: SO No Violations 0.30
-388953942 2011-12-12 0:00 UD No Violations
-604271270 2016-5-19 0:00: SO No Violations
-708927146 2011-11-15 0:00 UD No Violations
-895850752 2015-7-30 0:00: SO No Violations
0199080689 2012-07-10 Preliminary Restoration No Violations Preliminary Restoration is approved.
0388953942 2011-12-12 Urban Drill / Deepen / Reopen No Violations Kilbarger Rig 17 is drilling ahead on fluid at 3800. The pits are fenced, lined and in good condition.
0604271270 2016-05-19 Storage Well No Violations I conducted a status check on this well. The well site is equipped with:



The lease access is stable and drivable. No violations found.

0708927146 2011-11-15 Urban Drill / Deepen / Reopen No Violations Dominion has a contractor on site to clear stumps before Daley Excavating starts grading the location. The lease road has been installed and the required identification is posted.
0826620143 2018-06-15 Storage Well No Violations I did a status check inspection for this storage well. The well is equipped with a master gate valve, two side gate valves and a meter run. The diked tank battery consists of a steel tank. The well is legibly identified. No compliance issues are cited at this time.
0895850752 2015-07-30 Storage Well No Violations I conducted a status check on this well. The well is equipped with a master gate valve and a side gate valve that were inspected by a third party company on 6/2015. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) tank drains on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. There is a mechanical separator. The lease road is stable and drivable. No violations found.
1061767981 2016-05-19 Preliminary Restoration No Violations I conducted a preliminary restoration inspection on this well. The well is equipped with a master gate valve and a side gate valve. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) tank drains on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. The lease access is stable. Preliminary restoration passed.
1085596361 2011-01-09 Storage Well No Violations Change in inspection type from Urban Drill to Storage well. Dominion personnel are on site to install the wellhead assembly. The pits are pumped down, fenced, lined and in good condition. Solidification is now scheduled for tomorrow morning.
1097793910 2011-12-02 Urban Drill / Deepen / Reopen No Violations Kilbarger Drilling Rig 17 is starting to move on location and should spud late tonight. No violations at this time.
1098948624 2012-01-11 Urban Drill / Deepen / Reopen No Violations The drilling pits have been solidified and covered over.
1240898917 2011-12-13 Urban Drill / Deepen / Reopen No Violations Kilbarger Rig 17 is hung in the hole at 3952. The plan is to back off the drill pipe/collars at the nearest free point and jar the remaining pipe out.
1297263145 2011-12-14 Urban Drill / Deepen / Reopen No Violations Kilbarger and Baker Tool have successfully jarred the stuck collars and are recovering them at this time. They should be back to drilling later tonight or early tomorrow morning.
1324655102 2011-12-15 Urban Drill / Deepen / Reopen No Violations Kilbarger Drilling Rig 17 is back to drilling on fluid at 4025. Anticipate reaching total depth tomorrow. The pits are fenced, lined and in good condition. The location and lease road have deteriorated due to activity and rainfall. Additional restoration work will be necessary when the time comes.
1325007117 2011-12-21 Urban Drill / Deepen / Reopen No Violations Kilbarger is hung in the hole and has had no success jarring. The plan now is to backoff at 4032 leaving one collar, changeover sub and bit in the hole and plug back 300+. The hole will then be deviated 50 to the west.
1325553260 2011-12-27 Urban Drill / Deepen / Reopen No Violations Kilbarger Rig 17 is going back to drilling and tagged the top of the kick plug at 3621. The hole will be deviated to the west approximately 50 and will bypass the lost hole, drill collar and bit. The drilling pits are fenced and lined. No violations at this time.
1326731757 2012-01-06 Urban Drill / Deepen / Reopen No Violations Kilbarger Rig 17 has moved off location. The pits are fenced, lined and in good condition. The pits are scheduled to be solidified next week.
1379460900 2012-01-26 Storage Well No Violations The drilling pits have been solidified and covered over and the well has been fraced. Universal is on site to monitor flowback volumes and pressures. No violations at this time.
1380893485 2012-01-12 Urban Drill / Deepen / Reopen No Violations Daley Excavating requested and received permission to excavate and line a new pit to place and solidify drilling mud contained in a frac tank.
1469981093 2017-07-26 Storage Well No Violations At the time of this inspection, the well site is equipped with:



The lease access is stable and drivable. No violations were observed.

1532719012 2011-12-22 Urban Drill / Deepen / Reopen No Violations Kilbarger reached total depth on 12/17, mixed mud and started out of the hole. After pulling 2-1/2 stands, the pipe hung in the hole. At this point they could circulate but could not move uphole or downhole. All attempts to free the pipe, including unloading the hole and jarring were unsuccessful. During these attempts, circulation was lost and not recovered. Dominion ran a free point and Kilbarger backed the collars off leaving one collar, changeover sub and bit in the hole. Dominion ran a gyro and found the hole was straight. Kilbarger is preparing to run open ended drill pipe into the hole in order to set a kickoff plug. After the plug is set (later tonight), directional drillers will deviate around the equipment still in the hole and Kilbarger will again attempt to complete the well.
1583950990 2020-3-11 0:00: SO No Violations 0.50
1807143360 2011-11-10 Urban Drill / Deepen / Reopen No Violations Dailey Excavating is building the lease road and location for this natrual gas storage well. Kilbarger Drilling Rig 17 will be moving on location after completing the Shreiner well. The required identification is posted at the entrance.
1893142174 2011-12-22 Plug / Plug Back No Violations Kilbarger Drilling reached TD at 4223 on December 17. After circulating for two hours, Kilbarger started out of the hole and became hung after pulling 2-1/2 stands (approximately 150). Kilbarger went back to bottom and circulated for another two hours and hung again at the same spot. This time, they could not move uphole or downhole. After jarring and working the pipe for two days, the rig broke down and the decision was made to plug back the well and deviate to the west. On December 21, Kilbarger backed off the bottom collar and prepared to spot a cement kickoff plug. On December 22, Universal spotted a 100 sack plug from 3987 to 3675. Universal broke and maintained circulation throughout the job. Plug down at 22:43 on December 22. Kilbarger tripped out of the hole to the bottom of surface casing and will shut down until December 27.
199080689 2012-7-10 0:00: PL No Violations
2009896275 2014-10-09 Storage Well No Violations I inspected Dominion East Ohio Gas storage well #1-S.The well is equipped with a master gate valve and a side gate valve. There was a sales line with a separator. There is a flow gate valve plumbed with a 3.00 line into a 100 BBL storage tank. All lids and hatches on the storage tank are closed and secure. There are two (2) pickup lines on the storage tank and they are secured with valves and bull plugs in place. The tank battery is diked. The well is properly identified with a clear, legibly marked well identification sign mounted on the storage tank. The storage equipment was surrounded by a locked, chain link fence with barb wire. The lease road is stoned and drivable. No violations found.
46582985 2019-10-8 0:00: SO No Violations 0.30
826620143 2018-6-15 0:00: SO No Violations 0.50

For data sources see[5]

References