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Well ID: 34-163-20043 | Loading map...
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Country: United States | |
State: Ohio | |
County: Vinton | |
Municipality: Knox Township | |
Operator Name: HOCKING HILLS ENERGY AND WELL | |
Well Pad ID: | |
Farm/Lease Name: CLINE MYRTLE | |
License Status: Plugged and Abandoned | |
License Date: 2015-03-12 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.240000 | |
Longitude: -82.310000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1987-06-09 | 566 GRIM PAUL A |
Change of Owner | 2001-11-21 | Operator changed from 566, GRIM PAUL A to 5755, CHIEFTAIN ENERGY CORP. |
APP | 2015-03-12 | Proposed Formations:BEREA, Issued Date:3/12/2015, Expired Date:3/11/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2017-02-10 | INFO. ON THIS WELL CARD REPRESENTS ALL AVAILABLE INFORMATION ON FILE AT THE DIV. OF GEOLOGICAL SURVEY AND GAS 12/31/1987. |
Construction Permit Expires | 2017-03-11 | INFO. ON THIS WELL CARD REPRESENTS ALL AVAILABLE INFORMATION ON FILE AT THE DIV. OF GEOLOGICAL SURVEY AND GAS 12/31/1987. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ISON PROD SERVICES INC | 0.00 | 10.00 | 30 |
2006 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 365 |
2007 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2008 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2009 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2010 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2011 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2012 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2013 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
2014 | HOCKING HILLS ENERGY AND WELL | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | ISON PROD SERVICES INC | Brine | 100 | 30 |
2006 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 365 |
2007 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2008 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2009 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2010 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2011 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2012 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2013 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
2014 | HOCKING HILLS ENERGY AND WELL | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1424978562 | 2013-7-16 0:00: | PW | No Violations | 1.50 |
-1527045129 | 2015-1-21 0:00: | PW | No Violations | |
-172342757 | 2015-2-5 0:00:0 | PW | No Violations | 2.00 |
-50740456 | 2015-10-16 0:00 | PB | No Violations | |
-65384448 | 2019-6-5 0:00:0 | PW | No Violations | 0.80 |
-736388954 | 2012-9-19 0:00: | PW | No Violations | 1.00 |
-784671462 | 2015-11-25 0:00 | FR | No Violations | 3.00 |
-861529050 | 2013-7-16 0:00: | PW | No Violations | 1.00 |
-871707182 | 2014-4-10 0:00: | PW | No Violations | 1.00 |
-996440103 | 2019-7-1 0:00:0 | PW | No Violations | 1.80 |
0050740456 | 2015-10-16 | Plug / Plug Back | No Violations | 82 of 5 casing was retrieved. The casing parted. Tubing was ran down to 82 and circulated. This did not allow the tubing to drop. A pointed bit was ran down on tool to try and make a opening in the casing. The bit came back with damage on the end suggesting it was hitting the edge of the 5 casing. Kilbarger ran a impression block to determine what the condition of the pipe was in. The impression block showed the pipe had a curl. 1 tubing will be ran on 10-19-15 to try and get the tubing past the obstruction. |
0172342757 | 2015-02-05 | Production Wells | No Violations | Compliance notice follow-up. I met Hocking Hills Energy supervisor Doug Kitchen at the well head. The well has a old motor and tank. The site is overgrown with trees. I informed Doug of the need to plug the well. |
0724491065 | 2015-10-19 | Plug / Plug Back | No Violations | Kilbarger rig 7 has ran 1 tubing to 200. At this depth the tubing would not drop any further. The tubing was retrieved and a opening tool was ran down to try and open the casing. The casing was opened with the tool. 1 tubing was ran down to 1052. Formation Cementing on site at 1700 hours. 40 sack bottom plug set. 100 sack plug set 400 to surface. |
0736388954 | 2012-09-19 | Production Wells | No Violations | No change since last inspection. Accompanied by company representative Bill Wray. |
0784671462 | 2015-11-25 | Final Restoration | No Violations | Final restoration inspection. The well has been plugged. The well site has vegetative growth. The roadway does not have vegetative growth. Flow line remains. I have spoken with well owner Doug Kitchen concerning the remainder of the restoration. He stated the flow line would be removed and the roadways seeded by 2-1-16. |
0861529050 | 2013-07-16 | Production Wells | No Violations | I accompanied Andrew Thomas on this inspection, the well has not been plugged and remains idle. |
0871707182 | 2014-04-10 | Production Wells | No Violations | This is a follow-up inspection for the well being idle. Andy Thomas and Kip Thompson inspected this well before and wrote it up for not the well not being able to produce. The violation was issued on 1/11/2012. The well is still idle and there has been no attempt to put the well back into production. I will contact Kip Thompson and let him know about the situation. |
1326892823 | 2012-01-11 | Production Wells | Violations Noted | Well has no form of identification on it. Rods and tubing present. No pumping unit on well. Electric wires and box present, but are laying on the ground. Production records stated zero since 2006. Production lines are severed in several different places. Well is incapable of production. Well needs to be placed in production or plugged. Photos were taken during inspection. |
1335741100 | 2018-01-18 | Plug / Plug Back | No Violations | On the day of this follow up inspection, I found that all the pipe, electric lines and parts from the wellhead are still on site with no changes. I called Hocking Hills Energys Doug Kitchen about the clean up and reminded him that remediation was past due and Doug told me soon as the snow melts down and they finish the well there are drilling he would send out his crew to clean up the remaining remnants of the well site. |
1424978562 | 2013-07-16 | Production Wells | No Violations | Status of well has not changed since last inspection. It is still idle. No attempt has been made to gain compliance. Accompanied by Inspector Kip Thompson. |
1444920531 | 2015-10-15 | Plug / Plug Back | No Violations | Kilbarger rig 7 has pulled the tubing and rods. No information regarding the casing program. 1173 of tubing was retrieved. |
1445525153 | 2015-10-22 | Plug / Plug Back | No Violations | Equipment has been removed. Flow line has not been removed and seeding has been done. I have contacted Doug Kitchen to remind him of the need to finish the restoration. |
1507727095 | 2017-10-11 | Production Wells | No Violations | On the day of this inspection, I found an oil and gas well that has been plugged. I walked around the well site and found a flowline and electric power wire on the ground. I also found the top of a wellhead that was down the hill from well site that was not attached to anything. Talked to Hocking Hills Energys Doug Kitchen he said that they would have the well site cleaned up in the following two weeks from the time of my inspection. |
1510060420 | 2017-11-07 | Final Restoration | Violations Noted | On the day of this inspection, I found oil and gas well that had been plugged. The plugged well site still has piping and an electric line with remnants of a pumping unit that is down hill of the well site at time of my inspection. Oil and gas site restoration did not meet 1509.072B requirements at time of my inspection. I talked with Doug Kitchen of Hocking Hills Energy, Doug said he would get the well site in compliance and would call me soon as piping and other remnants were cleaned up. |
1527045129 | 2015-01-21 | Production Wells | No Violations | Compliance Follow-up 1326892823: The well is incapable of production. Well has no form of identification. There are pumping remnants on the ground and there are rods and tubing in the well. Electric wires and box present, but are laying on the ground. There has been no resolution to any of the issues. I talked to Dave Poling with Hocking Hills Energy and explained the issues. He will work with the Vinton County Inspector, Kip Thompson, on a timeline to plug or produce the wells. |
2061897430 | 2012-01-11 | Production Wells | No Violations | FOLLOW UP TO NOV # 1326892823 Well has no form of identification on it. Rods and tubing present. No pumping unit on well. Electric wires and box present, but are laying on the ground. Production records stated zero since 2006. Production lines are severed in several different places. Well is incapable of production. Well needs to be placed in production or plugged. Photos were taken during inspection. |
724491065 | 2015-10-19 0:00 | PB | No Violations | 10.50 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1326892823 | US-OH-109331 | 2012-01-18 | Failure to legibly identify well | |
1326892823 | US-OH-109332 | 2012-01-18 | Well shall be plugged | |
1326892823 | US-OH-109333 | 2012-01-18 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1510060420 | US-OH-114203 | 2017-11-21 | NONE3 | Failure to complete final restoration within six months |
For data sources see[7]