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37-005-01532

Well Details

Well ID: 37-005-01532
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Country: United States
State: Pennsylvania
County: Armstrong
Municipality: Washington Township
Operator Name: SENECA RESOURCES CO LLC
Well Pad ID:
Farm/Lease Name: NANCY B. MCCLATCHEY 4336
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.966250
Longitude: -79.574003

For data sources see[1][2][3]

Well History

Date Event
1901-01-01 Drilling Completion
1986-01-01 Old Well
2018-02-07 Begin Plugging
2018-02-14 Finished Plugging
2018-11-02 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 NATL FUEL GAS SUPPLY CORP 2094.00 365 0.00 0 0.00 0
1992 NATL FUEL GAS SUPPLY CORP 2,099.00 366 0.00 0 0.00 0
1996 SENECA RESOURCES CO LLC 1672 365 0.00 0 0.00 0
1997 SENECA RESOURCES CO LLC 1434 365 0.00 0 0.00 0
1998 SENECA RESOURCES CO LLC 1450 365 0.00 0 0.00 0
1999 SENECA RESOURCES CO LLC 1205 365 0.00 0 0.00 0
2000 SENECA RESOURCES CO LLC 1,419.00 365 0.00 0 0.00 0
2001 SENECA RESOURCES CO LLC 1377 365 0.00 0 0.00 0
2002 SENECA RESOURCES CO LLC 1321 365 0.00 0 0.00 0
2003 SENECA RESOURCES CO LLC 1373 364 0.00 0 0.00 0
2004 SENECA RESOURCES CO LLC 1276 364 0.00 0 0.00 0
2006 SENECA RESOURCES CO LLC 1377.00 365 0.00 0 0.00 0
2007 SENECA RESOURCES CO LLC 1256.00 365 0.00 0 0.00 0
2008 SENECA RESOURCES CO LLC 1373.00 365 0.00 0 0.00 0
2009 SENECA RESOURCES CO LLC 1369.00 365 0.00 0 0.00 0
2010 SENECA RESOURCES CO LLC 1,369.00 365 0.00 0 0.00 0
2011 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2012 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2013 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2014 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2015 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2016 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2017 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0
2018 SENECA RESOURCES CO LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2018 SENECA RESOURCES CO LLC Produced Fluid 30.00 Bbl RESIDUAL WASTE PROCESSING FACILITY WMGR123NW005

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2690904 Primary Facility 2018-02-05 Plugging(Includes Plugged/Mined Through) No Violations Noted As per a request from the operator, I met with the operator to review the staging of the equipment and the proposed plugging prognosis for this well. The plan as proposed looks ok, the well has been prepped for plugging and the operator plans on bringing the rig in to commence plugging shortly. I will return to provide oversight inspection when the plugging commences.
2693131 Primary Facility 2018-02-12 Plugging(Includes Plugged/Mined Through) No Violations Noted The Operator ran 70 sks of cement from 1010' to 600' on Friday 2/9/2018. The Operator tagged cement at 647' on Saturday 2/10/2018 and added 9 more sks of cement. After waiting on cement Operator ran the CBL and cut the 3 1/2" casing at 550', pulled the 3" and then perfed the rotten 6" casing utilizing 3 shots per perf at 350', 300', 250' and 200'. The Operator returned on Sunday 2/11/2018 and ran an additional 162 sks of cement for the second plug. The Operator returned on Monday 2/12/2018, tagged the cement top at 116' and was in the process of cementing to surface at the time of my inspection. All equipment on site looked ok.

For data sources see[7]

References