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Well ID: 37-033-20025 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Clearfield | |
Municipality: Huston Township | |
Operator Name: PHOENIX ENERGY PROD INC | |
Well Pad ID: | |
Farm/Lease Name: PA DEPT OF F & W | |
License Status: Plugged and Abandoned | |
Spud Date: 1957-01-31 | |
Permit Date: | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 41.144647 | |
Longitude: -78.574421 |
Date | Event |
---|---|
1957-01-31 | Performed Spud Operation |
1957-03-28 | Drilling Completion |
1957-03-28 | Newly Drilled |
2017-06-30 | Finished Plugging |
2019-02-19 | Partially Plugged |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1989 | 60.00 | 0 | 0.00 | 0 | 0.00 | 0 | |
1990 | 17.00 | 0 | 0.00 | 0 | 0.00 | 0 | |
1992 | DOMINION ENERGY TRANS INC | 23.00 | ? | 0.00 | 0 | 0.00 | 0 |
1996 | DOMINION ENERGY TRANS INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1997 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
1998 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2000 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2001 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2002 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2003 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2004 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2006 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2007 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2010 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2011 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2012 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2013 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2014 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | PHOENIX ENERGY PROD INC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2562744 | Primary Facility | 2017-02-16 | Routine/Complete Inspection | No Violations Noted | Inspection of EQT’s PA DFW #4 gas well in Huston Twp. Clearfield County conducted February 16, 2017 at 11:15 am. At the time of inspection; the location was snow covered. The well was shut-in with master valve atop production csg spool w/ one wing valve. The well is not tied into production. There was an (0-10,000 PSI) analog pressure gauge on top of the well, isolated by a needle valve, read no pressure. The cellar was dug out slightly, no gas detected. There was a metal tubing coming out the cellar tied into the backside of production csg as a vent; no gas detected. The operator has tentative plans to plug this well in the spring. |
2604470 | Primary Facility | 2017-06-13 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s PA DFW #4 gas well in Huston Twp. Clearfield County conducted June 13, 2017 at 11:15 am. Penn Mechanical had a rig and equipment on location in preparation for plugging ops. Well has been blown down. No gas behind the 7” was observed. I reviewed procedure with the contractor. No issues. |
2605808 | Primary Facility | 2017-06-19 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s PA DFW #4 gas well in Huston Twp. Clearfield County conducted June 19, 2017 at 10:30 am. Penn Mechanical had a rig and equipment on location for plugging ops. CIBP has been set in 7” (6960’) w/ 100’ CMT plug on top. The 7” was logged, TOC ~5500’, where they will make attempt to cut and pull csg above that point. No issues. |
2607009 | Primary Facility | 2017-06-22 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s PA DFW #4 gas well in Huston Twp. Clearfield County conducted June 22, 2017 at 12 pm. Penn Mechanical had a rig and equipment on location for plugging ops. After cut was made the rig was not able to pull 7” and there was reportedly 0 stretch well they pulled well over string weight. I discussed the procedure to squeeze the cut in the 7” and cmt plug inside casing. No major issues. |
2609963 | Primary Facility | 2017-07-03 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Inspection of EQT’s PA DFW #4 plugged gas well in Huston Twp. Clearfield County conducted June 30, 2017 at 2:00 pm. The rig is off location following plugging. The well has marked monument with vent pipe in place. No gas was detected at the vent. No issues. |
2628612 | Primary Facility | 2017-08-24 | Administrative/File Review | No Violations Noted | August 24, 2017: Certificate of Well Plugging for the PA Tract 63 #4 (033-20025) has been received, reviewed, signed, and sent to file. |
2683833 | Primary Facility | 2018-01-18 | Plugging(Includes Plugged/Mined Through) | No Violations Noted | Routine inspection of a plugged gas well. The well has a 2" tee vent pipe with marker as a monument. There was no visual or audible flow at the vent. There were no obvious issues or concerns observed. |
For data sources see[6]