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37-063-27075

Well Details

Well ID: 37-063-27075
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: West Mahoning Township
Operator Name: DE LTD FAMILY PARTNERSHIP
Well Pad ID:
Farm/Lease Name: EDWARD STEFFY 1
License Status: ACTIVE
Spud Date: 1982-06-15
Permit Date: 1982-07-10
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.879832
Longitude: -79.181230

For data sources see[1][2][3]

Well History

Date Event
1982-06-15 Performed Spud Operation
1982-07-01 Perforation
1982-07-02 Drilling Completion
1982-07-10 New Permit Application
1996-05-22 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 JC ENTERPRISES 4385.00 341 0.00 0 0.00 0
1992 JC ENTERPRISES 3774.00 365 0.00 0 0.00 0
1993 JC ENTERPRISES 2396.23 266 0.00 0 0.00 0
1994 JC ENTERPRISES 3237.57 338 0.00 0 0.00 0
1995 JC ENTERPRISES 2148.14 303 0.00 0 0.00 0
1996 JC ENTERPRISES 2257.83 365 0.00 0 0.00 0
1997 JC ENTERPRISES 1623.86 307 0.00 0 0.00 0
1998 JC ENTERPRISES 1836.54 331 0.00 0 0.00 0
1999 DE LTD FAMILY PARTNERSHIP 2027.98 349 0.00 0 0.00 0
2000 DE LTD FAMILY PARTNERSHIP 2119.05 337 0.00 0 0.00 0
2001 DE LTD FAMILY PARTNERSHIP 1937 366 0.00 0 0.00 0
2002 DE LTD FAMILY PARTNERSHIP 1998.07 365 0.00 0 0.00 0
2003 DE LTD FAMILY PARTNERSHIP 1861 353 0.00 0 0.00 0
2004 DE LTD FAMILY PARTNERSHIP 369 365 0.00 0 0.00 0
2005 DE LTD FAMILY PARTNERSHIP 2035.07 365 0.00 0 0.00 0
2006 DE LTD FAMILY PARTNERSHIP 2,000.00 372 0.00 0 0.00 0
2008 DE LTD FAMILY PARTNERSHIP 1627.00 360 0.00 0 0.00 0
2009 DE LTD FAMILY PARTNERSHIP 1566.00 326 0.00 0 0.00 0
2010 DE LTD FAMILY PARTNERSHIP 1,642.06 324 0.00 0 0.00 0
2011 DE LTD FAMILY PARTNERSHIP 1,262.11 304 0.00 0 0.00 0
2012 DE LTD FAMILY PARTNERSHIP 1,127.31 294 0.00 0 0.00 0
2013 DE LTD FAMILY PARTNERSHIP 864.24 276 0.00 0 0.00 0
2014 DE LTD FAMILY PARTNERSHIP 993.2 292 0.00 0 0.00 0
2015 DE LTD FAMILY PARTNERSHIP 2,006.03 337 0.00 0 0.00 0
2016 DE LTD FAMILY PARTNERSHIP 1,831.66 361 0.00 0 0.00 0
2017 DE LTD FAMILY PARTNERSHIP 1,542.83 362 0.00 0 0.00 0
2018 DE LTD FAMILY PARTNERSHIP 1,607.25 362 0.00 0 0.00 0
2019 DE LTD FAMILY PARTNERSHIP 887.89 334 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
1996 JC ENTERPRISES Brine 11.54 Bbl Municipal Sewage Treatment Plant PA 26310
2006 DE LTD FAMILY PARTNERSHIP Brine 50.00 Bbl Municipal Sewage Treatment Plant PA0101508
2016 DE LTD FAMILY PARTNERSHIP Produced Fluid 5.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2016 DE LTD FAMILY PARTNERSHIP Produced Fluid 5 Bbl CENT WASTE TRT FAC NPDES PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2116520 Primary Facility 2012-11-14 Routine/Complete Inspection No Violations Noted
2623275 Primary Facility 2017-08-08 Routine/Complete Inspection No Violations Noted At time of inspection, well drilled and appears equipped for production. Department observed a hissing noise that appears to be coming from the wellhead. Faint gas odor also observed. This concern will be forwarded to an OGI for the appropriate follow-up.
2638235 Primary Facility 2017-09-21 Routine/Complete Inspection Pending 9/21/17 - Annulus appears to be in production. Well is leaking, seems to be packing in well head. I spoke with DE Rep. Brian and he will get it fixed.
2826203 Primary Facility 2019-01-11 Routine/Complete Inspection No Violations Noted On 1/11/19 at 0937 hrs., I conducted a routine inspection of DE Ltd. Family Partnership's Ed Steffy 1 well (API 063-27075) in West Mahoning Twp., Indiana Co. Snow cover prevented proper evaluation of site stabilization. The well pad appears to be restored and permanently stabilized. The well is properly labeled and equipped for production. A well tag is present at the well head. There are no violations noted for this inspection.

For data sources see[7]

References