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37-063-36114

Well Details

Well ID: 37-063-36114
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Black Lick Township
Operator Name: ALLIANCE PETRO CO LLC
Well Pad ID:
Farm/Lease Name: H P WILLIAMS 4
License Status:
Spud Date: 2009-05-20
Permit Date: 2008-07-03
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.473077
Longitude: -79.263905

For data sources see[1][2][3]

Well History

Date Event
2008-07-03 New Permit Application
2009-05-20 Performed Spud Operation
2009-05-28 Drilling Completion
2009-06-04 Perforation
2009-10-08 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2009 PHILLIPS EXPLORATION INC 6082.00 365 0.00 0 0.00 0
2010 PHILLIPS EXPLORATION INC 26,177.00 365 0.00 0 0.00 0
2011 PHILLIPS EXPLORATION INC 14,751.00 364 0.00 0 0.00 0
2012 XTO ENERGY INC 12,611.00 366 0.00 0 0.00 0
2013 XTO ENERGY INC 8,655.00 365 0.00 0 0.00 0
2014 XTO ENERGY INC 8,717.00 354 0.00 0 0.00 0
2015 XTO ENERGY INC 5,747.00 365 0.00 0 0.00 0
2016 XTO ENERGY INC 5,020.00 366 0.00 0 0.00 0
2017 ALLIANCE PETRO CO LLC 3,336.00 334 0.00 0 0.00 0
2018 ALLIANCE PETRO CO LLC 4,358.00 365 0.00 0 0.00 0
2019 ALLIANCE PETRO CO LLC 5,165.00 303 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2010 PHILLIPS EXPLORATION INC Produced Fluid 5.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095443
2010 PHILLIPS EXPLORATION INC Produced Fluid 41.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE 301353
2010 PHILLIPS EXPLORATION INC Produced Fluid 6.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2010 PHILLIPS EXPLORATION INC Produced Fluid 1.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026034
2010 PHILLIPS EXPLORATION INC Produced Fluid 2.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472
2010 PHILLIPS EXPLORATION INC Produced Fluid 6.00 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026310
2010 PHILLIPS EXPLORATION INC Produced Fluid 1.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2011 PHILLIPS EXPLORATION INC Produced Fluid 60.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2015 XTO ENERGY INC Produced Fluid 32 Bbl CENT WASTE TRT FAC NPDES PA0095273
2015 XTO ENERGY INC Produced Fluid 32.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1804242 Primary Facility 2009-05-29 Routine/Complete Inspection No Violations Noted Well site appears to be in production. The site is well vegetated and there is no accelerated erosion and sedimentation noted on the access road or well site. Operator should continue to monitor the access road and well site for erosion and sedimentation.
1804578 Primary Facility 2009-06-11 Routine/Complete Inspection No Violations Noted Site ID sign in place. E&S plan on site.
1808391 Primary Facility 2009-06-12 Routine/Complete Inspection No Violations Noted id & e/s plan on site, drilling complete, site not reclaimed, 3 lioned pits with adequate freeboard
1812449 Primary Facility 2009-06-30 Drilling/Alteration No Violations Noted drilling complete - not equipped/pits ok/E&S ok/ID ok
1839374 Primary Facility 2009-10-27 Routine/Complete Inspection No Violations Noted At the time of inspection, the well was in production. The site ID sign and E&S plan were available for review. Contractors were actively reclaiming the well pad. The filter fabric fence was installed and functioning correctly. No accelerated E&S issues were noted in relation to well site or access road. Reminder that once the site has been structurally reclaimed the area should be permanently fertilized, seeded, and mulched to minimize and eliminate erosion and sedimentation concerns.
1908024 Primary Facility 2010-08-18 Complaint Inspection No Violations Noted At the time of inspection, Dan Rice of PC was onsite. Well completed on 05/28/09. This inspection was a result of a complaint filed with dept on Aug 16, 2010 of runoff from the site onto private property. Upon inspection, observed the installation of two diversion ditches around well site that led to a culvert pipe below pad that drains through a wooded area into another existing culvert. Operator and dept agreed that additional measures to ensure runoff does not occur during rain events on nearby private properties should be completed. Operator plans to rock ditches (to reduce flow), install a sediment trap (to resist erosion), and if possible divert runoff away from area near residence to opposite side of well. At the time of inspection, there was no evidence of accelerated erosion off the well site on complainant¿s property.

For data sources see[7]

References