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37-081-20564

Well Details

Well ID: 37-081-20564
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Country: United States
State: Pennsylvania
County: Lycoming
Municipality: Cogan House Township
Operator Name: ANADARKO E&P ONSHORE LLC
Well Pad ID: 148464
Farm/Lease Name: H LYLE LANDON A-6H
License Status:
Spud Date:
Permit Date: 2011-04-29
Well Type: GAS
Unconventional Well: Y
Configuration: Vertical Well
Conservation: No
Latitude: 41.412319
Longitude: -77.204742

For data sources see[1][2][3]

Well History

Date Event
2011-04-29 New Permit Application
2011-09-30 Drilling Completion
2011-09-30 Performed Spud Operation
2012-11-24 Drilling Completion
2013-05-23 FULLY PLUGGED
2013-05-23 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2011 ANADARKO E&P ONSHORE LLC 0.00 0 0.00 0 0.00 0
2012 ANADARKO E&P ONSHORE LLC 0.00 0 0.00 0 0.00 0

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2008906 Primary Facility 2011-10-06 Drilling/Alteration No Violations Noted
2063655 Primary Facility 2012-04-30 Routine/Complete Inspection No Violations Noted
2101650 Primary Facility 2012-09-19 Drilling/Alteration No Violations Noted
2124930 Primary Facility 2012-12-19 Drilling/Alteration No Violations Noted
2325611 Primary Facility 2014-11-25 Incident- Response to Accident or Event No Violations Noted On 11/22/2014 Mark Barbier (Anadarko) reported approximately 20 barrels of produced fluid and associated production gas was discharged (uncontrolled to the atmosphere) from the 4H well due to a pipe joint failure on the wellhead. According to the call, the well was shut in manually by Anadarko personnel.
2575434 Primary Facility 2017-03-21 Routine/Complete Inspection No Violations Noted Routine inspection of unvonventional well pad in production. A-6H well is plugged with no detectable methane emissions. Bubbling noted on location, later discovered to be a phenomenon of the thawing ground. Methane emissions not detected by GES during sampling of location.
2578539 Primary Facility 2017-03-23 Routine/Complete Inspection No Violations Noted Routine inspection of plugged well. 0% methane detected at time of inspection. No violations noted at time of inspection.
2581726 Primary Facility 2017-03-28 Follow-up Inspection No Violations Noted Follow up inspection of an unconventional well pad in production. Some bubbling still noted on the pad. 0% combustible gas emissions detected at time of inspection. No violations noted at time of inspection.
2584273 Primary Facility 2017-04-12 Follow-up Inspection No Violations Noted Follow up inspection of location and wells following discovery of a bubbling phenomenon on location. Phenomenon appears to have subsided, No methane detected during inspection. No violations noted at time of inspection.
2590078 Primary Facility 2017-05-03 Routine/Complete Inspection No Violations Noted Routine inspection of plugged well. No violations noted at time of inspection.
2643965 Primary Facility 2017-10-04 Routine/Complete Inspection No Violations Noted Weather was 57° and sunny at time of inspection. Well is plugged with a candycane style vent. Well vent had 0% combustible gas detected at time of inspection.
2687535 Primary Facility 2018-01-22 Incident- Response to Accident or Event No Violations Noted Spill response inspection; 1/22/2018.

Mark Barbier (ARD Operating) called the Department at 18:01 on 1/20/2018 to report the release of 176 gallons of a 30% methanol/water solution. The methanol/water mixture was released from a failed ball valve on the 4H(081-20563). 250 gallons of the released methanol/water mixture and melt water was vacuumed from the 3H well cellar later that night.

At approximately 13:45 on 1/22/2018, I met onsite with Mark Barbier and Rick Hall (both ARD). They showed me the failed valve leading to the 4H well and the excavated flow path into the 3H cellar. Material from the flow path across several feet of the pad surface had been excavated and placed in a overpack drum for disposal. The material under the excavation was frozen solid. I was only able to drive a digging bar 1/4 inch into the frozen surface. Water was streaming into the well cellars from the well pad surface due to warming temperatures and runoff. I was told the cellar would continue to be vacuumed. The conditio

2844660 Primary Facility 2019-02-26 Routine/Complete Inspection No Violations Noted Five wells staged for production. One well plugged. No free standing liquid on a day temperatures were below freezing. No leaks.

For data sources see[6]

References