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37-129-00708

Well Details

Well ID: 37-129-00708
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Bell Township
Operator Name: KRIEBEL MINERALS INC
Well Pad ID:
Farm/Lease Name: MCCREARY
License Status: Plugged and Abandoned
Spud Date:
Permit Date:
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.520556
Longitude: -79.520250

For data sources see[1][2][3]

Well History

Date Event
1938-01-01 Drilling Completion
1938-12-30 Old Well
2014-06-03 Performed Spud Operation
2019-05-16 Fully Plugged

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 DOME ACCOUNT 0.00 0 0.00 0 0.00 0
1999 KRIEBEL GAS INC 155 31 0.00 0 0.00 0
2000 KRIEBEL MINERALS INC 543 181 0.00 0 0.00 0
2001 KRIEBEL MINERALS INC 38 32 0.00 0 0.00 0
2006 KRIEBEL MINERALS INC 1479.00 346 0.00 0 0.00 0
2007 KRIEBEL MINERALS INC 755.00 365 0.00 0 0.00 0
2008 KRIEBEL MINERALS INC 729.00 349 0.00 0 0.00 0
2009 KRIEBEL MINERALS INC 637.00 332 0.00 0 0.00 0
2010 KRIEBEL MINERALS INC 1,284.00 365 0.00 0 0.00 0
2011 KRIEBEL MINERALS INC 1,151.00 334 0.00 0 0.00 0
2012 KRIEBEL MINERALS INC 1,026.00 333 0.00 0 0.00 0
2013 KRIEBEL MINERALS INC 764.00 295 0.00 0 0.00 0
2014 KRIEBEL MINERALS INC 912.00 321 0.00 0 0.00 0
2015 KRIEBEL MINERALS INC 735.00 318 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2014 KRIEBEL MINERALS INC Produced Fluid 82.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014 KRIEBEL MINERALS INC Produced Fluid 82 Bbl CENT WASTE TRT FAC NPDES PA0095273

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2449343 Primary Facility 2016-02-08 Site Restoration No Violations Noted Inspection performed in response to the receipt of the Well Site Restoration Report for the plugging of the above referenced well. At the time of inspection, plugging operations appear to have been completed and monument with permit number erected. Site appears to be restored and stable with no E&S issues in relation to site and/or access road. Since site is restored, Department recommends Operator remove silt fence down gradient of plugged well.

For data sources see[7]

References