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37-129-24505

Well Details

Well ID: 37-129-24505
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Country: United States
State: Pennsylvania
County: Westmoreland
Municipality: Murrysville Borough
Operator Name: K PETROLEUM INC
Well Pad ID:
Farm/Lease Name: DAUGHERTY 61AC
License Status: ACTIVE
Spud Date:
Permit Date: 2001-05-19
Well Type: GAS
Unconventional Well: N
Configuration: Vertical Well
Conservation: No
Latitude: 40.470864
Longitude: -79.641220

For data sources see[1][2][3]

Well History

Date Event
2001-05-19 New Permit Application
2001-11-27 Performed Spud Operation
2001-11-30 Drilling Completion
2002-05-08 NEWLY DRILLED

For data sources see[4]


Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2001 PENTEX ENERGY INC 5113 30 0.00 0 0.00 0
2002 PENTEX ENERGY INC 36692 333 0.00 0 0.00 0
2003 PENTEX ENERGY INC 33695 365 0.00 0 0.00 0
2004 LINN OPR LLC 467 30 0.00 0 0.00 0
2006 LINN OPR INC 9539.00 365 0.00 0 0.00 0
2007 LINN OPR INC 537.00 335 0.00 0 0.00 0
2008 XTO ENERGY INC 664.00 365 0.00 0 0.00 0
2009 XTO ENERGY INC 741.00 365 0.00 0 0.00 0
2010 XTO ENERGY INC 1,121.00 365 0.00 0 0.00 0
2011 XTO ENERGY INC 1,061.00 365 0.00 0 0.00 0
2012 XTO ENERGY INC 1,410.00 354 0.00 0 0.00 0
2013 XTO ENERGY INC 2,432.00 330 0.00 0 0.00 0
2014 XTO ENERGY INC 2,332.00 318 0.00 0 0.00 0
2015 XTO ENERGY INC 2,105.00 302 0.00 0 0.00 0
2016 K PETROLEUM INC 0.00 0 0.00 0 0.00 0
2017 K PETROLEUM INC 8.00 365 0.00 0 0.00 0
2018 K PETROLEUM INC 593.08 365 0.00 0 0.00 0

For data sources see[5]

Waste Data

Period Operator Waste Type Quantity Disposal Method Waste Facility ID
2001 PENTEX ENERGY INC Drilling 105.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2002 PENTEX ENERGY INC Brine 100.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472

For data sources see[6]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
1324318 Primary Facility 2004-03-30 Site Restoration No Violations Noted equipped/restored/tag ok/no tank
2479375 Primary Facility 2016-04-27 Routine/Complete Inspection No Violations Noted At the time of inspection well appears equipped for production. Well tag present and affixed in a permanent manner. No E&S issues in relation to site and/or access road.
2743974 Primary Facility 2018-06-18 Routine/Complete Inspection No Violations Noted Gas well shown in picture 1 is operated by KPI oil and Gas. KPI purchased several wells (60 to 80) wells from XTO about two years ago. In this area, five wells were connected to a compressor station located 600 ft east of the wellhead. Former operator XTO ran a compressor connected five wells in this field. Each well meter located in compressor building along with gas driven compressor. When KPI took over site, the compressor was removed from site. On June 16, 2018 at 11:23 am, Steve Nowakowski, KPI received a call from landowner of a fire at former compressor station. Refer to photo 6. Landowner called 911 also. Fire department arrived at 11:53 am and spread around fire to prevent spreading of fire. At 12:30 pm, Steve arrived and to told fire department to spray water on fire to extinguish fire. Several water sprays were made to cool off plumbing so,Steve could turn off ball valve on main line to shut gas off to fire area. Refer to photos 2to 5. Currently, main line is still shut in mode until

For data sources see[7]

References