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Difference between revisions of "37-015-21668"

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Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 37-015-21668
 
| Well ID: 37-015-21668
| style="height=100%; align=center" rowspan="14" | {{#display_map: 41.715355, -76.341091 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.715355, -76.341091 | width=100% | height=100% }}  
 
|-
 
|-
 
| County: [[Bradford County, Pennsylvania|Bradford]]
 
| County: [[Bradford County, Pennsylvania|Bradford]]
Line 9: Line 9:
 
| Municipality: [[Asylum Township, Bradford County, Pennsylvania|Asylum Township]]
 
| Municipality: [[Asylum Township, Bradford County, Pennsylvania|Asylum Township]]
 
|-
 
|-
| Operator Name: [[CHIEF OIL & GAS LLC|CHIEF OIL & GAS LLC]]
+
| Operator Name: [[CHIEF OIL & GAS LLC]]
 
|-
 
|-
| Well Pad ID: [[149071]]
+
| Well Pad ID: [[149071|149071]]
 
|-
 
|-
 
| Farm/Lease Name: PMG GOD UNIT A 3H
 
| Farm/Lease Name: PMG GOD UNIT A 3H
Line 25: Line 25:
 
| Horizontal: Yes
 
| Horizontal: Yes
 
|-
 
|-
| Producing: Yes
+
| Well Status: ACTIVE
 
|-
 
|-
| Violations: None
+
| Violations: 0
 
|-
 
|-
 
| Latitude: 41.715355
 
| Latitude: 41.715355
 
|-
 
|-
 
| Longitude: -76.341091
 
| Longitude: -76.341091
|-
 
|}
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | INSPECTION ID
 
!scope="col" | DATE
 
!scope="col" | DESCRIPTION
 
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
|-
 
| 1981671
 
| 2011-06-16
 
| No Violations Noted
 
| Rig Manager - Patterson 251.  Walk around site all OK.  3H completed.  Currently spudding 4H with Koder
 
|
 
|-
 
|-
 
| 1990558
 
| 2011-07-25
 
| No Violations Noted
 
| Conductor and surface casing cut off.  No visible bubbling.  0 psi on 9 5/8.  No gauge on 13 3/8.  Vented to tank.
 
|
 
|-
 
|-
 
| 2051589
 
| 2012-03-14
 
| No Violations Noted
 
| An incident occured at the site.  Was contacted by Ralph Larsen of Chief at 10:15AM.  Travelled to site w/ Kevin Costello, and Eric Rooney.  When we arrived on site we were informed that the situation had been handled.  The company Man on site was Bill Burton, and the Safety Manager was Allicia Cook.  Accident occured between 9 & 9:30AM.  While cleaning upplastic containment, Site Safe operator hooked on to line at wellhead and broke off 1/2" methanol injection line & pressure guage(see photos).  Everyone evacuated site including people in house above site. EMS, Wild Well, CUDD as well as appropiate DEP personel were contacted. Wysox FD and Cudd responded.  FD provided fresh water spray and Cudd person shut gate valve on B section of well head to stop flow of gas at about 12 noon.  There was no fire or fluids.  Gas was flowing out of 1/2" line for about 2 1/2 hrs. Pressure and vol. of gas are unknown.  When DEP personel arrived, FD was gone and CUDD was leaving.  DEP ER John Erich and Dennis Wolfe also responded.  Left site at about 2PM.
 
|
 
|-
 
|-
 
| 2103169
 
| 2012-09-12
 
| No Violations Noted
 
| Well is producing, 1929 psi.
 
Cellar has gravel in it. but some water, no bubbles.
 
4 annular vent - 2 are blue (5 1/2 x 9 5/8")  1 has 150 psi
 
                            1 rust colored  0 psi
 
                            1 yellow - pressure guage not functional
 
2 other producing wells on site  - 1H & 4H
 
|
 
 
|-
 
|-
 
|}
 
|}
Line 84: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2011-1
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2011-2
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2012-1
 +
| style="text-align:right;" | 691071.33
 +
| style="text-align:right;" | 120.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 
|-
 
|-
 
| 2012-2
 
| 2012-2
Line 94: Line 80:
 
|-
 
|-
 
|-
 
|-
| 2012-1
+
| 2013-1
| style="text-align:right;" | 691071.33
+
| style="text-align:right;" | 1098909.0
| style="text-align:right;" | 120.0
+
| style="text-align:right;" | 181.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2013-2
 +
| style="text-align:right;" | 914765.0
 +
| style="text-align:right;" | 180.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2014-1
 +
| style="text-align:right;" | 660019.0
 +
| style="text-align:right;" | 181.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 103: Line 107:
 
|-
 
|-
 
|-
 
|-
| 2011-2
+
| 2014-2
 +
| style="text-align:right;" | 227472.0
 +
| style="text-align:right;" | 113.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2015-02
 +
| style="text-align:right;" | 0.01
 +
| style="text-align:right;" | 1.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 112: Line 125:
 
|-
 
|-
 
|-
 
|-
| 2011-1
+
| 2015-01
 +
| style="text-align:right;" | 15255.0
 +
| style="text-align:right;" | 8.0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 +
|-
 +
|-
 +
| 2015-03
 +
| style="text-align:right;" | 80835.33
 +
| style="text-align:right;" | 31.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
Line 121: Line 143:
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Production Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Production
 +
| accessdate = 2015-05-27 }}</ref>
 
== Waste Data ==
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 133: Line 161:
 
!scope="col" | FACILITY STATE
 
!scope="col" | FACILITY STATE
 
|-
 
|-
| 2012-2
+
| 2011-1
| PRODUCED FLUID
+
| DRILL CUTTINGS
| style="text-align:right;" | 606.3
+
| style="text-align:right;" | 1.0
| Bbl
+
| Tons
| REUSE OTHER THAN ROAD SPREADING
+
| LANDFILL
|  
+
| 301626
| REUSE FOR HYDRAULIC FRACTURING
+
| WHITE PINES LANDFILL
|  
+
| MILLVILLE
|  
+
| PA
 
|-
 
|-
 
|-
 
|-
Line 152: Line 180:
 
| SUNBURY GENERATION WASTE WATER TRMT FAC
 
| SUNBURY GENERATION WASTE WATER TRMT FAC
 
| SHAMOKIN DAM
 
| SHAMOKIN DAM
| PA
 
|-
 
|-
 
| 2011-1
 
| DRILL CUTTINGS
 
| style="text-align:right;" | 1102.65
 
| Tons
 
| LANDFILL
 
| 301626
 
| WHITE PINES LANDFILL
 
| MILLVILLE
 
 
| PA
 
| PA
 
|-
 
|-
Line 179: Line 196:
 
| 2012-1
 
| 2012-1
 
| PRODUCED FLUID
 
| PRODUCED FLUID
| style="text-align:right;" | 1854.0
+
| style="text-align:right;" | 1.0
 +
| Bbl
 +
| REUSE OTHER THAN ROAD SPREADING
 +
|
 +
| REUSE FOR HYDRAULIC FRACTURING
 +
|
 +
|
 +
|-
 +
|-
 +
| 2012-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 606.3
 +
| Bbl
 +
| REUSE OTHER THAN ROAD SPREADING
 +
|
 +
| REUSE FOR HYDRAULIC FRACTURING
 +
|
 +
|
 +
|-
 +
|-
 +
| 2013-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 393.5
 
| Bbl
 
| Bbl
 
| REUSE OTHER THAN ROAD SPREADING
 
| REUSE OTHER THAN ROAD SPREADING
 
|  
 
|  
 
| REUSE FOR HYDRAULIC FRACTURING
 
| REUSE FOR HYDRAULIC FRACTURING
 +
|
 +
|
 +
|-
 +
|-
 +
| 2013-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 201.0
 +
| Bbl
 +
| REUSE OTHER THAN ROAD SPREADING
 +
|
 +
| REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
 +
|
 +
|
 +
|-
 +
|-
 +
| 2014-1
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 279.0
 +
| Bbl
 +
| REUSE OTHER THAN ROAD SPREADING
 +
|
 +
| REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
 +
|
 +
|
 +
|-
 +
|-
 +
| 2014-2
 +
| PRODUCED FLUID
 +
| style="text-align:right;" | 298.55
 +
| Bbl
 +
| REUSE OTHER THAN ROAD SPREADING
 +
|
 +
| REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
 +
|
 +
|
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Oil and Gas Historical Waste Report
 +
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Waste
 +
| accessdate = 2015-05-26 }}</ref>
 +
== Inspection Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | INSPECTION ID
 +
!scope="col" | DATE
 +
!scope="col" | DESCRIPTION
 +
!scope="col" | COMMENT
 +
!scope="col" | VIOLATION ID
 +
!scope="col" | VIOLATION CODE
 +
!scope="col" | VIOLATION_COMMENT
 +
|-
 +
| 1981671
 +
| 2011-06-16
 +
| No Violations Noted
 +
| Rig Manager - Patterson 251.  Walk around site all OK.  3H completed.  Currently spudding 4H with Koder
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1990558
 +
| 2011-07-25
 +
| No Violations Noted
 +
| Conductor and surface casing cut off.  No visible bubbling.  0 psi on 9 5/8.  No gauge on 13 3/8.  Vented to tank.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2051589
 +
| 2012-03-14
 +
| No Violations Noted
 +
| An incident occured at the site.  Was contacted by Ralph Larsen of Chief at 10:15AM.  Travelled to site w/ Kevin Costello, and Eric Rooney.  When we arrived on site we were informed that the situation had been handled.  The company Man on site was Bill Burton, and the Safety Manager was Allicia Cook.  Accident occured between 9 & 9:30AM.  While cleaning upplastic containment, Site Safe operator hooked on to line at wellhead and broke off 1/2" methanol injection line & pressure guage(see photos).  Everyone evacuated site including people in house above site. EMS, Wild Well, CUDD as well as appropiate DEP personel were contacted. Wysox FD and Cudd responded.  FD provided fresh water spray and Cudd person shut gate valve on B section of well head to stop flow of gas at about 12 noon.  There was no fire or fluids.  Gas was flowing out of 1/2" line for about 2 1/2 hrs. Pressure and vol. of gas are unknown.  When DEP personel arrived, FD was gone and CUDD was leaving.  DEP ER John Erich and Dennis Wolfe also responded.  Left site at about 2PM.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2103169
 +
| 2012-09-12
 +
| No Violations Noted
 +
| Well is producing, 1929 psi.
 +
Cellar has gravel in it. but some water, no bubbles.
 +
4 annular vent - 2 are blue (5 1/2 x 9 5/8")  1 has 150 psi
 +
                            1 rust colored  0 psi
 +
                            1 yellow - pressure guage not functional
 +
2 other producing wells on site  - 1H & 4H
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2306435
 +
| 2014-09-19
 +
| No Violations Noted
 +
| While in the process of surveying the site
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 2308786
 +
| 2014-09-26
 +
| No Violations Noted
 +
| I met with (2) employees of Mr. Dirt
 +
|
 
|  
 
|  
 
|  
 
|  
 
|-
 
|-
 
|}
 
|}
==References==
+
For data sources see<ref>{{cite web
{{Reflist}}
+
| title = Oil and Gas Historical Inspection Report
 
+
| publisher = [[Pennsylvania Department of Environmental Protection]]
 +
| date = 2015-05-26
 +
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources#Inspections
 +
| accessdate = 2015-05-27 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 20:27, 26 June 2015

Well Details

Well ID: 37-015-21668
Loading map...
County: Bradford
Municipality: Asylum Township
Operator Name: CHIEF OIL & GAS LLC
Well Pad ID: 149071
Farm/Lease Name: PMG GOD UNIT A 3H
First Permit Date: 2011-05-18
Last Permit Date: 2011-05-18
Spud Date: 2011-05-21
Unconventional: Yes
Horizontal: Yes
Well Status: ACTIVE
Violations: 0
Latitude: 41.715355
Longitude: -76.341091

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2011-1 0.0 0.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2012-1 691071.33 120.0 0.0 0.0 0.0 0.0
2012-2 1100540.0 184.0 0.0 0.0 0.0 0.0
2013-1 1098909.0 181.0 0.0 0.0 0.0 0.0
2013-2 914765.0 180.0 0.0 0.0 0.0 0.0
2014-1 660019.0 181.0 0.0 0.0 0.0 0.0
2014-2 227472.0 113.0 0.0 0.0 0.0 0.0
2015-02 0.01 1.0 0.0 0.0 0.0 0.0
2015-01 15255.0 8.0 0.0 0.0 0.0 0.0
2015-03 80835.33 31.0 0.0 0.0 0.0 0.0

For data sources see[1]

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2011-1 DRILL CUTTINGS 1.0 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2011-1 FRACING FLUID WASTE 65.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0008451 SUNBURY GENERATION WASTE WATER TRMT FAC SHAMOKIN DAM PA
2012-1 FRACING FLUID WASTE 157.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 PRODUCED FLUID 1.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-2 PRODUCED FLUID 606.3 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2013-1 PRODUCED FLUID 393.5 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2013-2 PRODUCED FLUID 201.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-1 PRODUCED FLUID 279.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY
2014-2 PRODUCED FLUID 298.55 Bbl REUSE OTHER THAN ROAD SPREADING REUSE WITHOUT PROCESSING AT A PERMITTED FACILITY

For data sources see[2]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
1981671 2011-06-16 No Violations Noted Rig Manager - Patterson 251. Walk around site all OK. 3H completed. Currently spudding 4H with Koder
1990558 2011-07-25 No Violations Noted Conductor and surface casing cut off. No visible bubbling. 0 psi on 9 5/8. No gauge on 13 3/8. Vented to tank.
2051589 2012-03-14 No Violations Noted An incident occured at the site. Was contacted by Ralph Larsen of Chief at 10:15AM. Travelled to site w/ Kevin Costello, and Eric Rooney. When we arrived on site we were informed that the situation had been handled. The company Man on site was Bill Burton, and the Safety Manager was Allicia Cook. Accident occured between 9 & 9:30AM. While cleaning upplastic containment, Site Safe operator hooked on to line at wellhead and broke off 1/2" methanol injection line & pressure guage(see photos). Everyone evacuated site including people in house above site. EMS, Wild Well, CUDD as well as appropiate DEP personel were contacted. Wysox FD and Cudd responded. FD provided fresh water spray and Cudd person shut gate valve on B section of well head to stop flow of gas at about 12 noon. There was no fire or fluids. Gas was flowing out of 1/2" line for about 2 1/2 hrs. Pressure and vol. of gas are unknown. When DEP personel arrived, FD was gone and CUDD was leaving. DEP ER John Erich and Dennis Wolfe also responded. Left site at about 2PM.
2103169 2012-09-12 No Violations Noted Well is producing, 1929 psi.

Cellar has gravel in it. but some water, no bubbles. 4 annular vent - 2 are blue (5 1/2 x 9 5/8") 1 has 150 psi

                            1 rust colored   0 psi
                            1 yellow - pressure guage not functional

2 other producing wells on site - 1H & 4H

2306435 2014-09-19 No Violations Noted While in the process of surveying the site
2308786 2014-09-26 No Violations Noted I met with (2) employees of Mr. Dirt

For data sources see[3]

References