If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-121-22213 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":39.68,"lon":-81.46,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Enoch Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: CROCK R | |
License Status: Final Restoration | |
License Date: 2014-05-07 | |
Spud Date: 1979-11-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-01-19 | |
Well Total Depth: 6222.00 ft | |
Configuration: Vertical | |
Latitude: 39.680000 | |
Longitude: -81.460000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1979-11-13 | 2143 CARLESS RESOURCES INC GeoDate 11/13/79 |
Original Spud | 1979-11-20 | |
Completed | 1980-01-19 | |
Reached Total Depth | 1980-01-19 | |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-05-07 | Proposed Formations:CLINTON, Issued Date:5/7/2014, Expired Date:5/6/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-07-29 | |
Construction Permit Expires | 2016-05-06 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 6017 | 6035 | 9 |
6017 | 6035 | 9 | |
6017 | 6035 | 9 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 58850 Gal | 55000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1986 | ZILKHA ENERGY INC | 3123.00 | 0.00 | 268 |
1987 | ZILKHA ENERGY INC | 2830.00 | 0.00 | 150 |
1988 | CARLESS RESOURCES INC | 2218.00 | 0.00 | 365 |
1989 | CARLESS RESOURCES INC | 1684.00 | 0.00 | 365 |
1990 | CARLESS RESOURCES INC | 2246.00 | 0.00 | 365 |
1991 | CARLESS RESOURCES INC | 1945.00 | 0.00 | 365 |
1992 | CARLESS RESOURCES INC | 1256.00 | 0.00 | 365 |
1993 | CARLESS RESOURCES INC | 2001.00 | 0.00 | 365 |
1994 | CARLESS RESOURCES INC | 1110.00 | 0.00 | 365 |
1995 | CARLESS RESOURCES INC | 1152.00 | 0.00 | 365 |
1996 | CARLESS RESOURCES INC | 1024.00 | 0.00 | 365 |
1997 | CARLESS RESOURCES INC | 1278.00 | 0.00 | 365 |
1998 | EXCO - NORTH COAST ENERGY INC | 1698.00 | 209.00 | 365 |
1999 | EXCO - NORTH COAST ENERGY INC | 1392.00 | 0.00 | 365 |
2000 | EXCO - NORTH COAST ENERGY INC | 1137.00 | 0.00 | 365 |
2001 | EXCO - NORTH COAST ENERGY INC | 1354.00 | 27.00 | 365 |
2002 | EXCO - NORTH COAST ENERGY INC | 1115.00 | 0.00 | 365 |
2003 | EXCO - NORTH COAST ENERGY INC | 1211.00 | 0.00 | 365 |
2004 | EXCO - NORTH COAST ENERGY INC | 988.00 | 0.00 | 365 |
2005 | EXCO - NORTH COAST ENERGY INC | 825.00 | 0.00 | 365 |
2006 | EXCO - NORTH COAST ENERGY INC | 942.00 | 0.00 | 365 |
2007 | EXCO - NORTH COAST ENERGY INC | 910.00 | 0.00 | 365 |
2008 | EXCO - NORTH COAST ENERGY INC | 746.00 | 0.00 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 229.00 | 0.00 | 365 |
2010 | ENERVEST OPERATING LLC | 214.00 | 0.00 | 365 |
2011 | ENERVEST OPERATING LLC | 7.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 58.00 | 150 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1434966379 | 2015-7-23 0:00: | PB | No Violations | 4.00 |
-1445302735 | 2015-7-28 0:00: | PB | No Violations | |
-1445927518 | 2015-10-5 0:00: | FR | No Violations | 2.00 |
1434966379 | 2015-07-23 | Plug / Plug Back | No Violations | I received a phone call from Chip Smith, owner of Chipco, indicating that a service rig was moving onto location. Upon arrival I found Chipco rig four working the 1.5 tubing. The rig crew ran sand line tools to a depth of 5180 and could not get any deeper. Circulation could not established The decision was made to cut the tubing. Appalachian Well Surveys cut the tubing at 5180. |
1438102768 | 2015-07-27 | Plug / Plug Back | No Violations | I am onsite to witness plugging operations. Greenes Welding installed a hot tap on the wellhead to allow the pressure to be released. Chipco pumped a 60 sack 15.6 pound per gallon class A cement plug through 1.5 tubing from 4370 to 4170. The service rig crew then pulled the tubing out of the well. A casing ripper was utilized to cut the 4.5 casing at the first point of free pipe at 3102. |
1445302735 | 2015-07-28 | Plug / Plug Back | No Violations | I am onsite to witness plugging operations. Chipco pumped a 200 60 sack class A cement plug through the 4.5 casing at 3102. Circulation was gained and approximately 90 barrels of oil was circulated out of the hole. The casing was pulled up to 1859 and a 200 class A plug was placed through 4.5 casing. The casing was pulled up to 200 from surface and a class A plug was circulated back to surface. The cement stayed at the surface. Chipco was instructed to reclaim the site in accordance with 1509.072(B). |
1445927518 | 2015-10-05 | Final Restoration | No Violations | My inspection today finds the well site meets the final restoration requirements of 1509.072(B). |
1711842866 | 2015-07-24 | Plug / Plug Back | No Violations | Chipco set a 30 sack 15.6 pound per gallon cement plug at 5180 through 1.5 tubing. The service rig crew pulled the tubing out of the well and Appalachian Well Surveys perforated the casing at 4340-4360 100 below the top of the Big Lime with 20 shots in 20. |
For data sources see[9]