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34-055-22027

Well Details

Well ID: 34-055-22027
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-08-23
Unconventional:
Horizontal:
Producing: No
Violations: 0
Latitude: 41.3996708387
Longitude: -81.0623269731

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION_COMMENT
-1189384314 2008-10-06 Spoke with Mike on site, tool pusher for Direct Drilling. Big Sky has fished out all three cones from the drill bit. They are tripping back into the hole to start drilling. Operator has 1300' left to finish drilling. Lease road is stable. Site is muddy.
-869645774 2013-03-26 The well is equipped with a pump jack. The annulus is open and plumbed into the production tank. The tank battery and well is in good repair. The tank battery consists of a 210 BBL production tank, a 50 BBL poly brine tank, and a mechanical separator. The proper identification sign is located on the tank battery. The lease road is in stable condition.
1110164558 2008-10-02 Operator has fished out all collars and the bit. Operator is tripping string out with magnet. Cones broke off of the drill bit when string dropped. Operator is attempting to retrieve the three cones from the bit. Lease road is stable and in good repair. Pits are in good repair. Ground at the drill site is soft from recent rain events. Drainage controls are in place.
1219670017 2008-08-25 Pits are in good repair. Lease road is stable and constructed out of durable material. Operator has set CND pipe. Operator has TD surface hole at 400', can not run surface pipe at this time, three joints down, keep getting stuck, operator stated that they have been in and out of the hole three times. Operator is pulling surface pipe out of the hole at the time of inspection. Permit is in the dog house.
1220361502 2008-08-29 No one on site at the time of inspection. Drill rig mast has broken in half. Top half of the mast is in the work pit. Called Cy Brennan from North Coast Energy Inc. Rig broke down last night between 8:00pm and 8:30 pm, North Coast Energy didn't find out until about accident until 8:30am 08/29/2008.
1220539462 2008-08-28 Rig dill depth 2200' Lease road is stable. Permit posted in the dog house. Picked up Surface and CND paper work. Spoke to daylight drilled, the surface cement went well, the cement has fallen. BOP had a lot of movement, operator had the BOP chained down. Operator was repairing the blow line during inspection, blow line was leaking at the BOP. The day light driller thought that it may have come lose, from the movement of the BOP. I suggested to the driller when they add a Kelly they may want to shim the surface hole to try and stop vibration. Driller said that they would tighten the chains. Surface hole will need to be grouted from the top during long string or bag cement brought on site and worked in between CND and surface. Pits were in good repair. Operator was drilling on air.
151067549 2008-09-25 Big Sky moving over the hole to fish drill collars out of the hole. Operator is pumping any water that is left in the work pit into the blow pit. Operator is going to reline the work pit before they begin work. Lease road and site are in good repair.
1924453455 2008-08-30 Met with Cy Brennan from North Coast, Mike McFadden tool pusher Direct drilling and owner of Direct drilling. Operator has placed safety fence around site. Insurance adjuster will be on site Tuesday, operator will be bringing a crane on site to pull rig off. Spoke to operator regarding hole, they will bring another rig on site to remove drill string and finish hole.
1968100399 2008-10-07 Operator has finished tripping into hole. Operator is working repairing air unit. Should be drilling by this afternoon. Pits are in good repair.
483659625 2009-10-26 Affected area has been returned to soy bean fields. Tank battery has one 210bbl tank and mechanical separator. Lease road is stable. Identification sign is up. No leaks noted. Clay soils from the end of the lease road to the well are very soft.