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37-015-21668

Well Details

Well ID: 42-015-21668
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County: Bradford
Municipality: Asylum Township
Operator Name: CHIEF OIL & GAS LLC
Farm/Lease Name: PMG GOD UNIT A 3H
First Permit Date: 2011-05-18
Last Permit Date: 2011-05-18
Spud Date: 2011-05-21
Unconventional: Yes
Horizontal: Yes
Producing: Yes
Violations: None
Latitude: 41.715355
Longitude: -76.341091

Well Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1981671 2011-06-16 No Violations Noted Rig Manager - Patterson 251. Walk around site all OK. 3H completed. Currently spudding 4H with Koder
1990558 2011-07-25 No Violations Noted Conductor and surface casing cut off. No visible bubbling. 0 psi on 9 5/8. No gauge on 13 3/8. Vented to tank.
2051589 2012-03-14 No Violations Noted An incident occured at the site. Was contacted by Ralph Larsen of Chief at 10:15AM. Travelled to site w/ Kevin Costello, and Eric Rooney. When we arrived on site we were informed that the situation had been handled. The company Man on site was Bill Burton, and the Safety Manager was Allicia Cook. Accident occured between 9 & 9:30AM. While cleaning upplastic containment, Site Safe operator hooked on to line at wellhead and broke off 1/2" methanol injection line & pressure guage(see photos). Everyone evacuated site including people in house above site. EMS, Wild Well, CUDD as well as appropiate DEP personel were contacted. Wysox FD and Cudd responded. FD provided fresh water spray and Cudd person shut gate valve on B section of well head to stop flow of gas at about 12 noon. There was no fire or fluids. Gas was flowing out of 1/2" line for about 2 1/2 hrs. Pressure and vol. of gas are unknown. When DEP personel arrived, FD was gone and CUDD was leaving. DEP ER John Erich and Dennis Wolfe also responded. Left site at about 2PM.
2103169 2012-09-12 No Violations Noted Well is producing, 1929 psi.

Cellar has gravel in it. but some water, no bubbles. 4 annular vent - 2 are blue (5 1/2 x 9 5/8") 1 has 150 psi

                            1 rust colored   0 psi
                            1 yellow - pressure guage not functional

2 other producing wells on site - 1H & 4H

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2012-2 1100540.0 184.0 0.0 0.0 0.0 0.0
2012-1 691071.33 120.0 0.0 0.0 0.0 0.0
2011-2 0.0 0.0 0.0 0.0 0.0 0.0
2011-1 0.0 0.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-2 PRODUCED FLUID 606.3 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2011-1 FRACING FLUID WASTE 65.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0008451 SUNBURY GENERATION WASTE WATER TRMT FAC SHAMOKIN DAM PA
2011-1 DRILL CUTTINGS 1102.65 Tons LANDFILL 301626 WHITE PINES LANDFILL MILLVILLE PA
2012-1 FRACING FLUID WASTE 157.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING
2012-1 PRODUCED FLUID 1854.0 Bbl REUSE OTHER THAN ROAD SPREADING REUSE FOR HYDRAULIC FRACTURING

References