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34-111-24531

Well Details

Well ID: 34-111-24531
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-12-10
Unconventional:
Configuration:
Well Status: Drilling
Violations: 0
Latitude: 39.82658123
Longitude: -81.28450075

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1328166935 2014-12-11 The said well was spudded on 12/10/2014 by Express Energys top hole rig with a 32 x 100' conductor borehole being drilled and 100' of 26 conductor pipe being set. Express Energy's cement service is on location to cement the casing using 330 sacks of class A-2% calcium .50 pps flake with 100% open hole cement excess ran and circulation established prior to cementing and the cement displaced with 55 barrels of fresh water and good cement returns witnessed to surface.
1419002908 2014-12-19 Status check inspection on the drilling process found Sidewinder Drilling rig 59 on location drilling the surface borehole @ 244' on air. Spud and standby notification was received on 12/08/14 by the company man for a surface casing cement job that evening. Efforts to contact the rig by phone and e-mail for a status update were not possible so I made a field visit for a status check @ 5:45 am.
1419175521 2014-12-21 12/20/14 The surface casing was ran and cemented to with Sidewinder Drilling rig 59 on location and Allied Cement Services cementing the casing using 932 sacks of class A 2% calcium .25 pps flake and 25 barrels of 6% gel ran ahead with 40 barrels of good cement returns documented to surface and the casing pressure tested to 500 psi upon the landing of the plug. The job was not witnessed due to having a migraine headache and all other inspectors being occupied.
160116292 2014-12-21 Sidewinder rig#59 on well and they were at 480' waiting on cement to set they had run 465' of 18.625 and cement it in place.
1733132424 2015-04-21 Status check inspection on the current drilling process found Patterson Drilling rig # 340 on location drilling the 8.750 production borehole at a depth of 7,383' with the current bit position located just below the 9.625 2nd intermediate casing string in the vertical position preparing to begin drilling the curve section on fluid.
743709478 2014-12-28 Status check inspection of the drilling process found Sidewinder Drilling rig 59 on the hole with the 13.375 1st intermediate casing string being set to 2,220'. They have nippled up and tested the Blow Out Preventer and drilled out from under the 13.375 and are sitting on bottom with directional tools awaiting directional drilling orders from Antero's management.
799233589 2015-01-04 Status check inspection on the current drilling process found Sidewinder rig 59 on location with the 9.625 casing string recently set and cemented. The rig is skidding to the Biedenbach #3 well.
-889575595 2015-04-29 Status check inspection on the current drilling process found Patterson Drilling rig # 340 on location drilling the 8.750 production borehole at a depth of 14,085' in the directional azimuth of 149 degrees and inclination of 89.48 degrees with a true vertical depth of 8,484' using 14.03 mud weight and implementing managed pressure drilling controlling 1769 units of 3rd party gas and holding 282 psi annular pressure on the drill string at surface through the choke. The company has experienced several fluid gains and has contacted me regularly while working gas influx out of the well bore through flaring.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.