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34-121-24540

Well Details

Well ID: 34-121-24540
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County:
Municipality:
Operator Name:
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2014-10-02
Unconventional:
Configuration:
Well Status: Drilling
Violations: 0
Latitude: 39.86487378
Longitude: -81.37069233

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1889118535 2014-10-30 My inspection today finds the drilling rig, Sidewinder 54, is drilling a 17.5 hole at a depth of 1397' at an average rate of 80' per hour. The company man indicated that a substantial water flow was encountered at 1200'.
-834619967 2014-10-26 I am onsite to witness the surface casing cementing operations. I tested the cement mix water for chlorides with a low range Quantab at 2.8 or (82) parts per million. Sidewinder Drilling Rig 54 ran 397' of 18.625 J-55 casing. Four centralizers were utilized to provide sufficient standoff and foster effective circulation of cement. Allied Oil and Gas Services cemented the casing in place with 155 barrels of class A cement with 20 barrels of cement circulating to surface. The latch down plug landed at 270 psi. The casing was pressured up to 770 psi. The casing pressure test was passed.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.